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Difference between revisions of "34-081-61058"

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| County: [[Jefferson_County,_Ohio|Jefferson]]
 
| County: [[Jefferson_County,_Ohio|Jefferson]]
 
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| Municipality: [[Knox_Township,_Jefferson_County,_Ohio|Knox Township]]
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| Municipality: [[Knox Township,_Jefferson_County,_Ohio|Knox Township]]
 
|-
 
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| Operator Name: [[FIRSTENERGY GENERATION LLC]]
 
| Operator Name: [[FIRSTENERGY GENERATION LLC]]

Revision as of 09:44, 15 August 2019

Well Details

Well ID: 34-081-61058
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Country: United States
State: Ohio
County: Jefferson
Municipality: Knox Township
Operator Name: FIRSTENERGY GENERATION LLC
Well Pad ID:
Farm/Lease Name: RUSSELL WT
License Status: Final Restoration
License Date: 2013-07-03
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 40.505329556
Longitude: -80.68893171

For data sources see[1]

Well History

Well Status Well Status Date Comment
Change of Owner 2013-06-20 Operator changed from 9998, HISTORIC OWNER to 9152, FIRSTENERGY GENERATION LLC. WELL TRANSFERRED PER OWNERSHIP AFFIDAVIT. SEE OWNER FILE FOR DOCUMENTATION. WELL TO BE PLUGGED BY A TEMPORARY OWNER.
APP 2013-07-03 Proposed Formations:BEREA, Issued Date:7/3/2013, Expired Date:7/3/2015 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2013-09-26
Construction Permit Expires 2015-07-03
Record Last Modified 2017-02-10

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0408423909 2015-03-18 Final Restoration No Violations On the date of inspection I am accompanied by SE Regional Manager Brent Bear to inspect the plugged and abandoned well for Final Restoration. The well passes Final Restoration per ORC 1509.072(B).
1380495823 2013-09-25 Plug / Plug Back No Violations We pulled 1362 of 2 tubing and 1095 of 1 tubing from the gas escape packer which was set at 1095. We ran a 125 sack first cement plug and will log the hole tomorrow to determine what can be done with the 6 5/8 casing/
1866939236 2013-09-26 Plug / Plug Back No Violations I was onsite to witness Appalachian well services log the 6 5/8 casing. We found 450 of free pipe but decided to shoot it off at 250 and pull the casing. The cement was tagged at 649 from the previous first cement stage. We were able to pull 250 of 6 5/8 casing and ran into the hole with 595 of 2 3/8 tubing to set the final cement plug. The well circulated and the plug was brought to surface.
1944144021 2013-09-27 Plug / Plug Back No Violations Checked the cement level of the last plug. Cement fell 27 and will be topped off when 61059 is cemented the start of next week.

For data sources see[3]

References