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Difference between revisions of "37-003-01265"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-003-01265
 
| Well ID: 37-003-01265
| style="height=100%; align=center" rowspan="14" | {{#display_map: 40.531917, -80.114583 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.531917, -80.114583 | width=100% | height=100% }}
 
|-
 
|-
 
| Country: United States
 
| Country: United States
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| License Status: Plugged OG Well
 
| License Status: Plugged OG Well
 
|-
 
|-
| Spud Date: 1/1/1800
+
| Spud Date: 1800-01-01
 
|-
 
|-
 
| Permit Date:  
 
| Permit Date:  
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  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | accessdate = 2019-05-21 }}</ref>
 
  | accessdate = 2019-05-21 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Job Number
 +
!scope="col" | Job Start Date
 +
!scope="col" | Job End Date
 +
!scope="col" | True Vertical Depth (ft)
 +
!scope="col" | Total Water Volume (gal)
 +
!scope="col" | Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Job Number
 +
!scope="col" | Trade Name
 +
!scope="col" | Supplier
 +
!scope="col" | Purpose
 +
!scope="col" | Ingredient Name
 +
!scope="col" | CAS Number
 +
!scope="col" | Additive Percentage by Mass
 +
!scope="col" | Job Percentage by Mass
 +
!scope="col" | Mass Used (lb)
 +
|-
 +
|}-->
 +
 
<!--== Production Data ==
 
<!--== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
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{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | Period
 
!scope="col" | Period
 +
!scope="col" | Operator
 
!scope="col" | Waste Type
 
!scope="col" | Waste Type
 
!scope="col" | Quantity
 
!scope="col" | Quantity
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| 2374244
 
| 2374244
 
| Primary Facility
 
| Primary Facility
| 05/29/2015
+
| 2015-05-29
 
| Follow-up Inspection
 
| Follow-up Inspection
 
| No Adverse Event or Action Reported
 
| No Adverse Event or Action Reported
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| 2415221
 
| 2415221
 
| Primary Facility
 
| Primary Facility
| 10/01/2015
+
| 2015-10-01
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Adverse Event or Action Reported
 
| No Adverse Event or Action Reported
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| 2415224
 
| 2415224
 
| Primary Facility
 
| Primary Facility
| 10/13/2015
+
| 2015-10-13
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| In Compliance with Schedule
 
| In Compliance with Schedule
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| 2415522
 
| 2415522
 
| Primary Facility
 
| Primary Facility
| 10/14/2015
+
| 2015-10-14
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| In Compliance with Schedule
 
| In Compliance with Schedule
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| 2416740
 
| 2416740
 
| Primary Facility
 
| Primary Facility
| 10/19/2015
+
| 2015-10-19
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| In Compliance with Schedule
 
| In Compliance with Schedule
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| 2417599
 
| 2417599
 
| Primary Facility
 
| Primary Facility
| 10/20/2015
+
| 2015-10-20
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| In Compliance with Schedule
 
| In Compliance with Schedule
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| 2417601
 
| 2417601
 
| Primary Facility
 
| Primary Facility
| 10/21/2015
+
| 2015-10-21
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| In Compliance with Schedule
 
| In Compliance with Schedule
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| 2418541
 
| 2418541
 
| Primary Facility
 
| Primary Facility
| 10/07/2015
+
| 2015-10-07
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
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| 2426766
 
| 2426766
 
| Primary Facility
 
| Primary Facility
| 11/04/2015
+
| 2015-11-04
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
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| 2427256
 
| 2427256
 
| Primary Facility
 
| Primary Facility
| 11/23/2015
+
| 2015-11-23
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Adverse Event or Action Reported
 
| No Adverse Event or Action Reported
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| 2436755
 
| 2436755
 
| Primary Facility
 
| Primary Facility
| 12/30/2015
+
| 2015-12-30
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| In Compliance with Schedule
 
| In Compliance with Schedule
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  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | accessdate = 2019-05-21 }}</ref>
 
  | accessdate = 2019-05-21 }}</ref>
<!--== Fracking Activities ==
 
==== Fracking Jobs ====
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | Job Number
 
!scope="col" | Job Start Date
 
!scope="col" | Job End Date
 
!scope="col" | True Vertical Depth (ft)
 
!scope="col" | Total Water Volume (gal)
 
!scope="col" | Total Non-Water Volume (gal)
 
|-
 
|}-->
 
<!--==== Fluid Composition Data ====
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | Job Number
 
!scope="col" | Trade Name
 
!scope="col" | Supplier
 
!scope="col" | Purpose
 
!scope="col" | Ingredient Name
 
!scope="col" | CAS Number
 
!scope="col" | Additive Percentage by Mass
 
!scope="col" | Job Percentage by Mass
 
!scope="col" | Mass Used (lb)
 
|-
 
|}-->
 
 
 
==References==
 
==References==
 
<references/>
 
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Pennsylvania Wells]]
 
[[Category:Pennsylvania Wells]]

Revision as of 04:42, 19 August 2019

Well Details

Well ID: 37-003-01265
Loading map...
Country: United States
State: Pennsylvania
County: Allegheny
Municipality: Kilbuck Township
Operator Name: UNKNOWN OPR
Well Pad ID:
Farm/Lease Name: W P C 1
License Status: Plugged OG Well
Spud Date: 1800-01-01
Permit Date:
Unconventional Well: N
Configuration: Vertical Well
Latitude: 40.531917
Longitude: -80.114583

For data sources see[1][2][3]


Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2374244 Primary Facility 2015-05-29 Follow-up Inspection No Adverse Event or Action Reported Met w/ Andy Zadnik (WPC) to inspect well. Well intact and not currently leaking o/g/w. WPC hopes to get well plugged this summer
2415221 Primary Facility 2015-10-01 Plugging(Includes Plugged/Mined Through) No Adverse Event or Action Reported Checked wellsite for location preparation for pending plugging. No activity yet.
2415224 Primary Facility 2015-10-13 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule Rig on well, got all tubing pulled. Attempted to release packer on 5" casing, would not release. Wireline TIH w/ casing cutter, attempted to get to point above packer @ 1312 feet, but repeatedly set down on obstruction @ 1258 feet. Pulled cutter up to 1250 feet & cut casing. Will attempt to pull 5" tomorrow.
2415522 Primary Facility 2015-10-14 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule Pulled all 1250 feet of 5" casing from hole. Will run bond log tomorrow AM.
2416740 Primary Facility 2015-10-19 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule Allegheny Well Services (plugging contractor sub-contracted by Nicks Well Plugging) set two 11 bbl. plugs, 105 sacks total from 1530 feet (TD) to ~870 feet (calculated). WOC, then pulled 6 1/4" casing, appears to have parted @ ~220 feet (wireline). Perfed 6 1/4" casing, 5 shots each @ 800'-805', 700'-705', 600'-605', 500'-505', 400'-405'.
2417599 Primary Facility 2015-10-20 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule Allegheny Well Services pumped final cement plug to surface, moved rig off location.
2417601 Primary Facility 2015-10-21 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule Site is being being prepared for reclamation.
2418541 Primary Facility 2015-10-07 Plugging(Includes Plugged/Mined Through) No Violations Noted AN ACCESS ROAD IS BEING CLEARED TO ALLOW PLUGGING OPS TO BEGIN.
2426766 Primary Facility 2015-11-04 Plugging(Includes Plugged/Mined Through) No Violations Noted A SMALL TRACK HOE HAS STARTED RESTORATION OF THIS SITE. THE WELL IS PLUGGED.
2427256 Primary Facility 2015-11-23 Plugging(Includes Plugged/Mined Through) No Adverse Event or Action Reported Site is rough-graded, with final restoration left to do.
2436755 Primary Facility 2015-12-30 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule Location is graded, seeded and mulched. Marker is buried.
2447059 Primary Facility 2016-02-03 Follow-up Inspection No Adverse Event or Action Reported Inspected site in response to an anonymous call-in that was reported to Rich Freese stating that "there are abandoned well sites that are contaminating a creek." The caller stated that "animals, fish and plants have been affected by the oil coming from the wells. There could also be abandoned barrels and drums leaking unknown oils or chemicals into the creek." Western Pennsylvania Conservancy was stated as the suspected responsible party. I inspected all five wellsites on the property and all nearby streams for leaking oil, but did not find a trace.There was no indication of animals, fish or plants affected by anything. It is important to note that there are no longer any wellhead, tanks or associated production equipment at the WPC #1, which was plugged in October 2015.

For data sources see[4]

References