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{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
!scope="col" | Period | !scope="col" | Period | ||
| + | !scope="col" | Operator | ||
!scope="col" | Waste Type | !scope="col" | Waste Type | ||
!scope="col" | Quantity | !scope="col" | Quantity | ||
| Line 127: | Line 128: | ||
!scope="col" | Waste Facility ID | !scope="col" | Waste Facility ID | ||
|- | |- | ||
| − | | 2015 | + | | 2015 |
| + | | | ||
| Drill Cuttings (in Tons) | | Drill Cuttings (in Tons) | ||
| style="text-align: right;" | 651.56 Tons | | style="text-align: right;" | 651.56 Tons | ||
| Line 133: | Line 135: | ||
| PAD059087072 | | PAD059087072 | ||
|- | |- | ||
| − | | 2015 | + | | 2015 |
| + | | | ||
| Drill Cuttings (in Tons) | | Drill Cuttings (in Tons) | ||
| style="text-align: right;" | 313.20 Tons | | style="text-align: right;" | 313.20 Tons | ||
| Line 139: | Line 142: | ||
| 301071 | | 301071 | ||
|- | |- | ||
| − | | 2015 | + | | 2015 |
| + | | | ||
| Drilling Fluid Waste (in Barrels) | | Drilling Fluid Waste (in Barrels) | ||
| style="text-align: right;" | 458.00 Bbl | | style="text-align: right;" | 458.00 Bbl | ||
| Line 145: | Line 149: | ||
| | | | ||
|- | |- | ||
| − | | 2016 | + | | 2016 |
| − | | | + | | [[VANTAGE ENERGY APPALACHIA II LLC]] |
| − | | style="text-align: right;" | | + | | Servicing Fluid (in Barrels) RWC 808 |
| + | | style="text-align: right;" | 23.00 Bbl | ||
| REUSE OTHER THAN ROAD SPREADING | | REUSE OTHER THAN ROAD SPREADING | ||
| | | | ||
|- | |- | ||
| − | | 2016 | + | | 2016 |
| − | | | + | | [[VANTAGE ENERGY APPALACHIA II LLC]] |
| − | | style="text-align: right;" | | + | | Other Oil & Gas Wastes (in Barrels) RWC 899 |
| + | | style="text-align: right;" | 17.00 Bbl | ||
| REUSE OTHER THAN ROAD SPREADING | | REUSE OTHER THAN ROAD SPREADING | ||
| | | | ||
| Well ID: 37-059-26985 | Loading map...
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| Country: United States | |
| State: Pennsylvania | |
| County: Greene | |
| Municipality: Gray Township | |
| Operator Name: RICE DRILLING B LLC | |
| Well Pad ID: 152172 | |
| Farm/Lease Name: GRECOE 10H | |
| License Status: Plugged OG Well | |
| Spud Date: 2015-11-17 | |
| Permit Date: 2015-11-09 | |
| Unconventional Well: Y | |
| Configuration: Horizontal Well | |
| Latitude: 39.920136 | |
| Longitude: -80.379994 |
| Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
|---|---|---|---|---|---|---|---|
| 2015 | VANTAGE ENERGY APPALACHIA II LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2016 | VANTAGE ENERGY APPALACHIA II LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
| 2017 | VANTAGE ENERGY APPALACHIA II LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[4]
| Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
|---|---|---|---|---|---|
| 2015 | Drill Cuttings (in Tons) | 651.56 Tons | LANDFILL | PAD059087072 | |
| 2015 | Drill Cuttings (in Tons) | 313.20 Tons | RESIDUAL WASTE TRANSFER FACILITY | 301071 | |
| 2015 | Drilling Fluid Waste (in Barrels) | 458.00 Bbl | REUSE OTHER THAN ROAD SPREADING | ||
| 2016 | VANTAGE ENERGY APPALACHIA II LLC | Servicing Fluid (in Barrels) RWC 808 | 23.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
| 2016 | VANTAGE ENERGY APPALACHIA II LLC | Other Oil & Gas Wastes (in Barrels) RWC 899 | 17.00 Bbl | REUSE OTHER THAN ROAD SPREADING |
For data sources see[5]
| Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|---|
| 2431473 | Primary Facility | 2015-11-24 | Drilling/Alteration | No Violations Noted | |
| 2442362 | Primary Facility | 2015-12-10 | Drilling/Alteration | No Violations Noted | Decker Rig #8. Tripping into the hole. Surface casing (18 5/8”) set and cemented to surface on 12/8/2015. Coal protective casing (13 3/8”) set and cemented to surface on 12/10/15. Review casing/cementing information. Conduct site inspection. Operator performing containment maintenance/repair. |
| 2442373 | Primary Facility | 2015-12-28 | Drilling/Alteration | No Violations Noted | Decker Rig #8. Operator unable to drill intermediate section of borehole (sidetrack) due to formation conditions and stuck tools. Unable remove fish. Operator set a cement plug in the intermediate section of the borehole. Top of cement plug 1,427’ (est). |
| 2442384 | Primary Facility | 2015-12-17 | Drilling/Alteration | No Violations Noted | Decker Rig #8. Operator was unable to retrieve stuck BHA due to formation conditions. A cement kick plug was set from 2,100’ to 1,600’ on 12/15/2015. Operator sidetracked and is re-drilling the intermediate portion of the borehole. Operator currently stuck in hole. |
| 2480006 | Primary Facility | 2016-03-30 | Routine/Complete Inspection | No Violations Noted | Operator did not complete drilling of the well. Operator plans to abandoned well and plug the well. |
| 2508543 | Primary Facility | 2016-08-02 | Routine/Complete Inspection | No Violations Noted | Well drilled. Well for hydrualic fracturing operations to begin. |
| 2513501 | Primary Facility | 2016-08-24 | Routine/Complete Inspection | No Violations Noted | Operator encountered difficulties during drilling. Well scheduled to be plugged. |
| 2518393 | Primary Facility | 2016-09-06 | Routine/Complete Inspection | No Violations Noted | Operator encountered problems during drilling. Well to be plugged. |
For data sources see[6]