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Difference between revisions of "37-059-26985"

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| style="text-align: right;" | 313.20 Tons
 
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| 2016
| Other Oil & Gas Wastes (in Barrels) RWC 899
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| [[VANTAGE ENERGY APPALACHIA II LLC]]
| style="text-align: right;" | 17.00 Bbl
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| Servicing Fluid (in Barrels) RWC 808
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| REUSE OTHER THAN ROAD SPREADING
 
| REUSE OTHER THAN ROAD SPREADING
 
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| 2016-M04
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| 2016
| Servicing Fluid (in Barrels) RWC 808
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| [[VANTAGE ENERGY APPALACHIA II LLC]]
| style="text-align: right;" | 23.00 Bbl
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| Other Oil & Gas Wastes (in Barrels) RWC 899
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| style="text-align: right;" | 17.00 Bbl
 
| REUSE OTHER THAN ROAD SPREADING
 
| REUSE OTHER THAN ROAD SPREADING
 
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Revision as of 14:18, 19 August 2019

Well Details

Well ID: 37-059-26985
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Country: United States
State: Pennsylvania
County: Greene
Municipality: Gray Township
Operator Name: RICE DRILLING B LLC
Well Pad ID: 152172
Farm/Lease Name: GRECOE 10H
License Status: Plugged OG Well
Spud Date: 2015-11-17
Permit Date: 2015-11-09
Unconventional Well: Y
Configuration: Horizontal Well
Latitude: 39.920136
Longitude: -80.379994

For data sources see[1][2][3]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2015 VANTAGE ENERGY APPALACHIA II LLC 0.00 0 0.00 0 0.00 0
2016 VANTAGE ENERGY APPALACHIA II LLC 0.00 0 0.00 0 0.00 0
2017 VANTAGE ENERGY APPALACHIA II LLC 0.00 0 0.00 0 0.00 0

For data sources see[4]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2015 Drill Cuttings (in Tons) 651.56 Tons LANDFILL PAD059087072
2015 Drill Cuttings (in Tons) 313.20 Tons RESIDUAL WASTE TRANSFER FACILITY 301071
2015 Drilling Fluid Waste (in Barrels) 458.00 Bbl REUSE OTHER THAN ROAD SPREADING
2016 VANTAGE ENERGY APPALACHIA II LLC Servicing Fluid (in Barrels) RWC 808 23.00 Bbl REUSE OTHER THAN ROAD SPREADING
2016 VANTAGE ENERGY APPALACHIA II LLC Other Oil & Gas Wastes (in Barrels) RWC 899 17.00 Bbl REUSE OTHER THAN ROAD SPREADING

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2431473 Primary Facility 2015-11-24 Drilling/Alteration No Violations Noted
2442362 Primary Facility 2015-12-10 Drilling/Alteration No Violations Noted Decker Rig #8. Tripping into the hole. Surface casing (18 5/8”) set and cemented to surface on 12/8/2015. Coal protective casing (13 3/8”) set and cemented to surface on 12/10/15. Review casing/cementing information. Conduct site inspection. Operator performing containment maintenance/repair.
2442373 Primary Facility 2015-12-28 Drilling/Alteration No Violations Noted Decker Rig #8. Operator unable to drill intermediate section of borehole (sidetrack) due to formation conditions and stuck tools. Unable remove fish. Operator set a cement plug in the intermediate section of the borehole. Top of cement plug 1,427’ (est).
2442384 Primary Facility 2015-12-17 Drilling/Alteration No Violations Noted Decker Rig #8. Operator was unable to retrieve stuck BHA due to formation conditions. A cement kick plug was set from 2,100’ to 1,600’ on 12/15/2015. Operator sidetracked and is re-drilling the intermediate portion of the borehole. Operator currently stuck in hole.
2480006 Primary Facility 2016-03-30 Routine/Complete Inspection No Violations Noted Operator did not complete drilling of the well. Operator plans to abandoned well and plug the well.
2508543 Primary Facility 2016-08-02 Routine/Complete Inspection No Violations Noted Well drilled. Well for hydrualic fracturing operations to begin.
2513501 Primary Facility 2016-08-24 Routine/Complete Inspection No Violations Noted Operator encountered difficulties during drilling. Well scheduled to be plugged.
2518393 Primary Facility 2016-09-06 Routine/Complete Inspection No Violations Noted Operator encountered problems during drilling. Well to be plugged.

For data sources see[6]

References