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Difference between revisions of "37-085-23750"

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Revision as of 23:55, 19 August 2019

Well Details

Well ID: 37-085-23750
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Country: United States
State: Pennsylvania
County: Mercer
Municipality: South Pymatuning Township
Operator Name: STRYKER ENERGY LLC
Well Pad ID:
Farm/Lease Name: T WOODS 3
License Status: Active
Spud Date: 2005-03-29
Permit Date: 2005-03-04
Unconventional Well: N
Configuration: Vertical Well
Latitude: 41.349165
Longitude: -80.471525

For data sources see[1][2][3]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2005 COBRA RESOURCES LLC 6,856.00 365 0.00 0 0.00 0
2006 COBRA RESOURCES LLC 7,885.00 365 0.00 0 0.00 0
2007 COBRA RESOURCES LLC 885.00 365 41.00 365 0.00 0
2008 COBRA RESOURCES LLC 0.00 0 0.00 0 0.00 0
2009 COBRA RESOURCES LLC 0.00 0 0.00 0 0.00 0
2012 STRYKER ENERGY LLC 0.00 0 0.00 0 0.00 0
2013 STRYKER ENERGY LLC 0.00 0 0.00 0 0.00 0
2014 STRYKER ENERGY LLC 0.00 0 0.00 0 0.00 0
2015 STRYKER ENERGY LLC 0.00 0 0.00 0 0.00 0
2016 STRYKER ENERGY LLC 100.00 274 0.00 0 0.00 0
2017 STRYKER ENERGY LLC 0.00 0 0.00 0 0.00 0
2018 STRYKER ENERGY LLC 0.00 0 0.00 0 0.00 0

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1441189 Primary Facility 2005-04-13 Drilling/Alteration No Violations Noted
1994664 Primary Facility 2011-08-09 Routine/Complete Inspection Violation(s) Noted
2011274 Primary Facility 2011-10-17 Compliance Evaluation No Violations Noted
2372859 Primary Facility 2015-05-26 Routine/Partial Inspection Violation(s) Noted
2454884 Primary Facility 2016-03-01 Complaint Inspection Violation(s) Noted
2494249 Primary Facility 2016-06-17 Complaint Inspection Outstanding Violations - No Viols Req'd
2533349 Primary Facility 2016-11-01 Follow-up Inspection Outstanding Violations - No Viols Req'd
2601100 Primary Facility 2017-05-17 Follow-up Inspection Outstanding Violations - Viols Req'd
2755283 Primary Facility 2018-07-24 Follow-up Inspection Violation(s) & Outstanding Violations Domestic gas meter attached to well but production casing valves are shut. Tubing valve is open but goes to shut sales line valve. Surface casing is vented to atmosphere.
2829799 Primary Facility 2019-01-22 Follow-up Inspection Violation(s) Noted Follow up from inspection dated 7/24/18. Operator is in non compliance with the Departments order dated March 21, 2018 to plug the well within 120 days of the date of the Order. The Department filed a petition to enforce with the Commonwealth Court and the Court issued an Order on August 6, 2018. Inspection shows no well label attached to the well head. Photo 2 shows valves closed to the domestic house gas meter and was previously mentioned in the 7/24/18 inspection report. Photo 3 shows the GPU with no meter. Operator reported on the required 2017 production report that well was temporarily not producing and well would be back up in 2018. A review of the Departments records revealed the operator failed to report the required 2017 MIA report. Well remains abandoned and no Notice of Intent to Plug has been filed with the Department.

NOTE: Operator remains in non compliance with the Departments Order dated March 21, 2018.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
1994664 617460 08/09/2011 2011-08-09 210UNPLUG - Failure to plug a well upon abandonment Administrative
2372859 724017 05/26/2015 2015-05-26 OGA 3220(A) - Failure to plug the well upon abandoning it. Environmental Health & Safety
2454884 747784 2016-03-01 OGA3220(A) Environmental Health & Safety
2454884 747785 2016-03-01 2016-06-17 OGA 3222(A) Administrative
2454884 747786 2016-03-01 OGA3211(H) Administrative
2601100 787313 2017-05-17 OGA3220(A) Environmental Health & Safety
2601100 787316 2017-05-17 OGA3211(H) Administrative
2755283 822979 2018-07-24 OGA3211(H) Administrative No API posted on well.
2755283 822980 2018-07-24 OGA3220(A) Environmental Health & Safety Continued failure to plug well upon abandonment.
2755283 822981 2018-07-24 OGA3259(1) Environmental Health & Safety Styker is in non-compliance with the Department order dated March 21, 2018 to plug well by 7/23/2018.
2829799 839544 2019-01-15 OGA3211(H) Administrative
2829799 839545 2019-01-15 78.88(a) Administrative
2829799 839546 2019-01-15 OGA3220(A) Environmental Health & Safety
2829799 839547 2019-01-15 OGA3259(1) Environmental Health & Safety Styker is in non-compliance with the Department order dated March 21, 2018 to plug well by 7/23/2018.

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
617460 273748 NOV - Notice of Violation Comply/Closed 2011-10-28
724017 323941 NOV - Notice of Violation
747784 340647 NOV - Notice of Violation
747784 362529 ADORD - Administrative Order
747785 340647 NOV - Notice of Violation
747785 362529 ADORD - Administrative Order
747786 340647 NOV - Notice of Violation
747786 362529 ADORD - Administrative Order
787313 340647 NOV - Notice of Violation
787313 362529 ADORD - Administrative Order
787316 340647 NOV - Notice of Violation
787316 362529 ADORD - Administrative Order
839544 372714 NOV - Notice of Violation
839545 372714 NOV - Notice of Violation
839546 372714 NOV - Notice of Violation
839547 372714 NOV - Notice of Violation

For data sources see[5]

References