If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
m |
m |
||
Line 113: | Line 113: | ||
|- | |- | ||
| 2000 | | 2000 | ||
− | | | + | | [[CHARLEMAGNE INVESTMENT CORP]] |
| style="text-align: right;" | 0.00 | | style="text-align: right;" | 0.00 | ||
| style="text-align: right;" | 0 | | style="text-align: right;" | 0 | ||
Line 158: | Line 158: | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
!scope="col" | Period | !scope="col" | Period | ||
+ | !scope="col" | Operator | ||
!scope="col" | Waste Type | !scope="col" | Waste Type | ||
!scope="col" | Quantity | !scope="col" | Quantity |
Well ID: 37-129-21614 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.119806,"lon":-79.646361,"icon":""}]} |
Country: United States | |
State: Pennsylvania | |
County: Westmoreland | |
Municipality: East Huntingdon Township | |
Operator Name: CHARLEMAGNE INVESTMENT CORP | |
Well Pad ID: | |
Farm/Lease Name: NANCY THRELFALL 11 | |
License Status: Active | |
Spud Date: 1800-01-01 | |
Permit Date: 1980-01-08 | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Latitude: 40.119806 | |
Longitude: -79.646361 |
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1997 | CHARLEMAGNE INVESTMENT CORP | 2,822.94 | 365 | 0.00 | 0 | 0.00 | 0 |
1998 | CHARLEMAGNE INVESTMENT CORP | 2,887.86 | 365 | 0.00 | 0 | 0.00 | 0 |
1999 | CHARLEMAGNE INVESTMENT CORP | 3,109.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2000 | CHARLEMAGNE INVESTMENT CORP | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2002 | CHARLEMAGNE INVESTMENT CORP | 533.00 | 150 | 0.00 | 0 | 0.00 | 0 |
2005 | CHARLEMAGNE INVESTMENT CORP | 1,343.83 | 210 | 0.00 | 0 | 0.00 | 0 |
2007 | CHARLEMAGNE INVESTMENT CORP | 874.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[4]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2569959 | Primary Facility | 2017-03-09 | Routine/Complete Inspection | No Violations Noted | Inspection conducted at request of main office with additional action pending. Well not tagged-turned into line-annulus shut. 4 1/2" casing corroded badly with compromised mechanical integrity but not leaking yet. 2 3/8" upset production tubing rusted badly but still ok. 2" production line pitted badly but not leaking yet. |
For data sources see[5]