If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
m |
m |
||
Line 11: | Line 11: | ||
| County: [[Muskingum_County,_Ohio|Muskingum]] | | County: [[Muskingum_County,_Ohio|Muskingum]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Harrison_Township,_Muskingum_County,_Ohio|Harrison Township]] |
|- | |- | ||
| Operator Name: [[VICTOR MCKENZIE DRILLING CO I]] | | Operator Name: [[VICTOR MCKENZIE DRILLING CO I]] |
Well ID: 34-119-27116 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":39.813351901,"lon":-81.932578,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Muskingum | |
Municipality: Harrison Township | |
Operator Name: VICTOR MCKENZIE DRILLING CO I | |
Well Pad ID: | |
Farm/Lease Name: ELSON CARL | |
License Status: Producing | |
License Date: 1984-07-20 | |
Spud Date: 1984-08-15 | |
Spud Drilling Contractor: VICTOR MCKENZIE | |
Final Drill Date: 1984-10-10 | |
Well Total Depth: 4370 ft | |
Configuration: Vertical | |
Latitude: 39.813351901 | |
Longitude: -81.93257800 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1984-07-20 | 281 McKENZIE VICTOR DRILL INC GeoDate 7/20/84 |
Oil and Gas | 1984-07-20 | Issued Date 7/20/84 Expired Date 1/16/85 Acres 0040000 Tool Type CT Proposed Formation CLINTON Proposed Depth 04370 Proposed Drill Depth 04370 |
Original Spud | 1984-08-15 | CHG. Y COORD. 10-26-85 |
Completed | 1984-10-10 | CHG. Y COORD. 10-26-85 |
Reached Total Depth | 1984-10-10 | CHG. Y COORD. 10-26-85 |
Completion Report Received | 1984-10-17 | CHG. Y COORD. 10-26-85 |
Construction Permit Expires | 1985-01-16 | CHG. Y COORD. 10-26-85 |
Record Last Modified | 2015-09-24 | CHG. Y COORD. 10-26-85 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 4216 | 4250 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 | FRAC: H2O,SAND |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0000PL8139 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0020920236 | 2008-01-03 | Production Wells | No Violations | On line but unsure if actually producing. |
0063666284 | 2016-01-29 | Production Wells | No Violations | I performed a follow-up inspection on Compliance Notice number 664017752. Mark Hughes the brother of Complainant accompanied me on the inspection. There has been nothing done at the well or the tank batteries. There is a power pole leaning with a transformer on the end. There is a possibility for spillage of the oil from the transformer. I will call Elmer and meet him on the site. |
0223557382 | 2016-12-07 | Production Wells | No Violations | The purpose of the inspection is a Follow-- |
0267592093 | 2015-04-13 | Production Wells | No Violations | This is Compliance Follow-up to # 664017752. There has been no change at the tanks. There is still a brine scald and the tanks need to be moved and the ground needs to be reclaimed and diked up. Remove all debris at the tank site. This well is closest to the tank batteries. Well is required to be plugged but no plug permit in hand yet. Remove the 1black plastic line from the tank to the well head. |
0341204898 | 2016-02-04 | Production Wells | No Violations | I met Elmer Gibson at site of the 119-27119 and 119-27116 and stressed that the site has not been touched since it was in violation on 11-2014. I have to have a plan to have all site cleaned up at the tanks with fixing the tanks and all pertinent plumbing for both wells. The scald at the tanks needs remediated. Then seed and mulch the affected area. Pick up all trash and debris from both well sites and haul away. Remove the power pole with the transformer that is leaning to prevent oil from escaping and ending on the site in the woods. Elmer stated he would have a plan sent to me by e-mail. I stated that if I do not have a plan than I will construct a Chiefs order. |
0500555066 | 2015-04-15 | Administrative Inspection | No Violations | I met with Elmer Gibson on the previous Compliance Action. Due to inclement weather The company wishes to be granted a 60 day extension on the said well. He will fix the problems at the tank site. He will have to get a rig in on well and pull the rods and down hole pump. |
0664017752 | 2014-11-07 | Production Wells | Violations Noted | I inspected well based on compliant #4858. Mark and Mike Hughes are the landowners. Mark and son in law met out on location. The Pumping unit has not moved for a while due to the polished rod has oxidized. The two shared tanks have leaked over the dike with brine creating a scald area of 6x130. Area needs soil removed and replaced and seeded and mulched as per Best Management Practices. The production records are current with the State. Failure to comply within 30 days of receipt of Compliance Notice may result in further Enforcement Action. |
0859601688 | 2016-11-07 | Administrative Inspection | No Violations | The Administrative inspection is due to a Compliance Notice follow-up on number 664017752. I called Elmer Gibson on the tank farm and stated that he needs to move the tanks and to extract the dirt out and replace the soil. The gypsum is not working. He wanted to try turning the soil. I stated that should have been done in the place. |
1173994853 | 2016-05-02 | Production Wells | No Violations | The purpose of the inspection is a follow-up to Compliance Notice # 664017752 and a verbal plan that was sent by e-mail from the company to the Division of Oil and Gas. The well has no means of mechanical movement. The gas line is cut to the prime mover and the electric line has been cut and unhooked. The polished rod has oxidized due to non- movement. There is no identification at the well. There are 2-100 barrel steel tanks that are shared with the 2 wells. The gas is leaking out of the back of the rotary meter. The meter is not in operation due non -- |
1464268296 | 2016-05-26 | Production Wells | No Violations | The purpose of the inspection is a follow-up to the Compliance Notice 664017752. I met Elmer Gibson on site and took some field samples of soil and tested with quantabs on Chlorides after he removed the contaminated soil. The samples were below 100 parts per million. They will place new top soil on the areas that were removed and hauled away. They are placing pelletized lime and gypsum down on the soil. They will seed and mulch in with all the material on site. |
1466090596 | 2016-05-06 | Production Wells | No Violations | The purpose of the inspection is a Compliance Notice Follow-up on number 664017752. Brent Bear and I met Elmer Gibson the operator of Victor McKenzie Drill Co. Inc. with owner #281. Elmer was showing us the work that has been performed and the work that will be completed. I asked Elmer where was the gas going and he stated that it is sold through Cameron out the road into a master meter. |
1627517338 | 2016-09-06 | Production Wells | No Violations | The inspection is due to a follow--100 barrel tank between the tank and the 2 vertical separators. The high Quantab strips measured 6200 parts per million of chlorides. |
1964371051 | 2004-04-20 | Production Wells | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0664017752 | US-OH-127522 | 2018-11-05 | 9-1-07 | Well operation causing pollution and contamination |
0664017752 | US-OH-127523 | 2018-11-05 | 9-9-05(A)9 | No SPCC dike/or failure to keep dike free of water or oil |
For data sources see[9]