If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
m |
m |
||
Line 11: | Line 11: | ||
| County: [[Washington_County,_Ohio|Washington]] | | County: [[Washington_County,_Ohio|Washington]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Decatur_Township,_Washington_County,_Ohio|Decatur Township]] |
|- | |- | ||
| Operator Name: [[BLAUSER ENERGY CORPORATION]] | | Operator Name: [[BLAUSER ENERGY CORPORATION]] |
Well ID: 34-167-26684 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":39.29234015,"lon":-81.80393685,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Decatur Township | |
Operator Name: BLAUSER ENERGY CORPORATION | |
Well Pad ID: | |
Farm/Lease Name: W T JAMES | |
License Status: Final Restoration | |
License Date: 2015-10-09 | |
Spud Date: 2009-02-03 | |
Spud Drilling Contractor: FMS DRILLING | |
Final Drill Date: 2009-02-08 | |
Well Total Depth: 4101 ft | |
Configuration: Vertical | |
Latitude: 39.292340150 | |
Longitude: -81.80393685 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1981-06-25 | 2 BLAUSER WELL SERVICE INC GeoDate 6/25/81 |
Original Spud | 1981-08-19 | OTD = 1961' IN OHIO SHALE |
Completed | 1981-08-22 | OTD = 1961' IN OHIO SHALE |
Change of Owner | 2008-08-22 | Operator changed from 2, BLAUSER WELL SERVICE INC to 7077, D T ATHA INC |
APP | 2008-09-18 | Proposed Formations:ORISKANY/OHIO SHALE, Issued Date:9/18/2008, Expired Date:9/18/2009 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL |
APP | 2008-09-30 | Proposed Formations:OHIO SHALE/ORISKANY, Issued Date:9/30/2008, Expired Date:9/30/2009 6:00:00 AM, Drilling unit acres:88, Proposed Well Type:OG, Proposed Well Class:EDPW |
Reached Total Depth | 2009-02-08 | OTD = 1961' IN OHIO SHALE |
Completion Report Received | 2009-04-24 | OTD = 1961' IN OHIO SHALE |
Change of Owner | 2010-03-18 | Operator changed from 7077, D T ATHA INC to 2, BLAUSER WELL SERVICE INC |
APP | 2015-10-09 | Proposed Formations:ORISKANY, Issued Date:10/9/2015, Expired Date:10/8/2017 12:00:00 PM, Drilling unit acres:88, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2015-11-13 | OTD = 1961' IN OHIO SHALE |
Record Last Modified | 2017-02-15 | OTD = 1961' IN OHIO SHALE |
Construction Permit Expires | 2017-10-08 | OTD = 1961' IN OHIO SHALE |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2009-07-20 | 1885 | 1893 | 8 |
2009-07-20 | 3987 | 3995 | 9 |
2009-07-20 | 3948 | 3970 | 5 |
2009-07-20 | 3238 | 3856 | 20 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 600 Bbl | 46000 | FRAC TREATMENT FOR ORIGINALLY DRILLED WELL | ||
H2O | 0 | 2964 Bbl | 75000 | FRAC INCLUDES BIG CINNAMON AND UPPER BIG LIME (UNDIFFERENTIATED). |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0830127337 | 2009-02-02 | Drill / Deepen / Reopen | No Violations | Tool pusher called to say moving on well to deepen. Went out to location - checked to see if have BOP and they do. Should start drilling late today or tomorrow. |
1051253551 | 2016-06-07 | Final Restoration | No Violations | The purpose of my inspection today is a status check on a final restoration. During my inspection I witnessed no evidence of an oil and gas well and the site has been restored. Location has met 1509.072 B requirements. |
1448896034 | 2015-11-13 | Plug / Plug Back | No Violations | On location to witness plugging activities for this well. Berry Well Service (Knox Energy) was able to rip the 7 intermediate casing at 326 and pull it OOH. Fluid level was gauged and observed to be 350 down. It was approved for a pre-cast concrete plug to be placed on top of the ripped 7 casing and sealed off with prepared clay to serve as a base for the bottom of surface casing and surface plug. Cemenco set a combination bottom of surface casing/surface plug from 326-0 using 150 sks class A cement, 5 sks of gel in the first half of the plug, and 60 lbs cottonseed hulls as LCM. Cement was poured in from surface did not drop once it reached surface. |
1603687139 | 2009-07-14 | Preliminary Restoration | No Violations | Inspection this day found location has been reclaimed, grass starting to grow, still has one frac tank there that they are putting brine into. Oil tank has good IDs, dike is breached, well producing with jack, gas bubbling around the wellhead. This was a Berea cable tool hole that was deepened. |
1851477640 | 2015-11-12 | Plug / Plug Back | No Violations | On location to check status of plugging operations for this well. Knox Energy/Berry Well Service is rigged up over the well and is ripping the 4.5 casing for the second time. A two part bottom perforation plug and rip isolation/Berea Sandstone plug was set on 11/11/15. During the displacement of the rip/Berea plug, open perforations in the 7 intermediate casing created vaccum and pulled the 4.5 casing against it, causing it to be lodged and subsequently cemented in the well. The remaining 4.5 casing will be pulled OOH and the uncemented portion of 7 intermediate casing will be ripped and pulled OOH. A bottom-of-surface casing and surface plug will be set on 11/13/15. |
1987510685 | 2006-01-26 | Production Wells | No Violations | Inspection this day found well producing thru the casing, tank has good IDs, current chart in meter, good dike. |
For data sources see[9]