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| County: [[Stark_County,_Ohio|Stark]] | | County: [[Stark_County,_Ohio|Stark]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Lexington_Township,_Stark_County,_Ohio|Lexington Township]] |
|- | |- | ||
| Operator Name: [[HALL & HORNING SERV INC]] | | Operator Name: [[HALL & HORNING SERV INC]] |
Well ID: 34-151-24011 | Loading map...
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Country: United States | |
State: Ohio | |
County: Stark | |
Municipality: Lexington Township | |
Operator Name: HALL & HORNING SERV INC | |
Well Pad ID: | |
Farm/Lease Name: MYERS L | |
License Status: Producing | |
License Date: 1984-05-21 | |
Spud Date: 1984-06-19 | |
Spud Drilling Contractor: SCOTT WELL DRLG | |
Final Drill Date: 1984-07-10 | |
Well Total Depth: 451 ft | |
Configuration: Vertical | |
Latitude: 40.987758558 | |
Longitude: -81.14535220 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1984-05-21 | 260 TWINOAKS OIL & GAS CO GeoDate 5/21/84 |
Oil and Gas | 1984-05-21 | Issued Date 5/21/84 Expired Date 5/21/85 Acres 0005000 Tool Type CT Proposed Formation BEREA Proposed Depth 00451 Proposed Drill Depth 00451 |
Original Spud | 1984-06-19 | |
Completed | 1984-07-10 | |
Reached Total Depth | 1984-07-10 | |
Completion Report Received | 1984-09-20 | |
Construction Permit Expires | 1985-05-21 | |
Change of Owner | 2002-11-12 | Operator changed from 260, TWINOAKS OIL & GAS CO to 3847, HALL & HORNING SERV INC |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 | NONE |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | ACTION PETROLEUM INC | 272 | 0 | 0 |
1986 | ACTION PETROLEUM INC | 432 | 0 | 365 |
2002 | HALL & HORNING SERV INC | 0 | 0 | 92 |
2003 | HALL & HORNING SERV INC | 11 | 0 | 365 |
2004 | HALL & HORNING SERV INC | 0 | 0 | 365 |
2005 | HALL & HORNING SERV INC | 0 | 0 | 365 |
2006 | HALL & HORNING SERV INC | 0 | 0 | 365 |
2007 | HALL & HORNING SERV INC | 0 | 0 | 365 |
2008 | HALL & HORNING SERV INC | 0 | 0 | 0 |
2009 | HALL & HORNING SERV INC | 0 | 0 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | ACTION PETROLEUM INC | Brine | 0 | 0 |
1986 | ACTION PETROLEUM INC | Brine | 0 | 365 |
2002 | HALL & HORNING SERV INC | Brine | 0 | 92 |
2003 | HALL & HORNING SERV INC | Brine | 0 | 365 |
2004 | HALL & HORNING SERV INC | Brine | 0 | 365 |
2005 | HALL & HORNING SERV INC | Brine | 0 | 365 |
2006 | HALL & HORNING SERV INC | Brine | 0 | 365 |
2007 | HALL & HORNING SERV INC | Brine | 0 | 365 |
2008 | HALL & HORNING SERV INC | Brine | 0 | 0 |
2009 | HALL & HORNING SERV INC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0000PL5349 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0152171004 | 2016-05-17 | UrbanProduction Wells | No Violations | I conducted a compliance notice follow up inspection on this well. A compliance notice was issued to plug the well on 1/28/2014. Plugging was required by 4/22/2014. The well has 7 casing with 4.5 production casing with a swage and non-functional pressure gauge on it. There is a sales line from the well. There is no associated tank battery and no other production equipment on the wellsite. The access to the well has been removed and the wellhead is located within a farm field. Production records for this well have reported zero since 2003. There is no identification on or around the well head. This well is currently incapable of production and needs to be plugged. |
0296036564 | 2017-10-26 | Production Wells | No Violations | I conducted a Chiefs Order Follow-up inspection on this well for Chiefs Order 2017-79 issued 03-07-2017. The well is not plugged as ordered. The master valve and the sales line valve are open. The well consists of a 7 casing with 4.5 production casing with a swage with a broken gauge on top. There is a sales line attached to the well above the master valve. No tank battery has been located at this time and no other flow lines or sale line have been found. The well is not legibly identified. I called 330-472-1389 and spoke with gentleman who claimed he doesnt own any more wells and Hall & Horning are out of business. |
0370209160 | 2018-01-10 | Production Wells | No Violations | I conducted a Chiefs Order Follow-up inspection on this well for Chiefs Order 2017-79 issued 03-07-2017. The well is not plugged as ordered. The master valve and the sales line valve are open. The well consists of a 7 casing with 4.5 production casing with a swage with a broken gauge on top. There is a sales line attached to the well above the master valve. No tank battery has been located at this time and no other flow lines or sale line have been found. The well is not legibly identified. I called 330-472-1389 and spoke with Randy Hall (owner). |
0436000731 | 2017-01-17 | Production Wells | No Violations | I conducted a compliance notice follow-up inspection on this well. The compliance notice was issued to on 1/28/2014 and plugging was required by 4/22/2014. The well has not been plugged. The master valve is open. The well consists of a 7 casing with 4.5 production casing with a swage with a broken gauge on top. There is a sales line valve is open and it is attached to the well above the master valve. No tank battery has been located at this time and no other flow lines or sale line have been found. The well is not legibly identified. No annual production reports have been submitted since 2009. This well is currently incapable of production. |
1101879929 | 2016-11-29 | Production Wells | No Violations | A compliance notice follow-up inspection was done on 11-26-2016. None of the noted compliance issues have been remedied by the operator at the time of this inspection. The initial Compliance Notice was issued on 01-28-2014 for the following non-compliance issue with a remedy required date of 04-22-2014:
Ohio Revised Code (ORC):
Ohio Administrative Code (OAC): 1501: 9-9- The record shows no new Plug and Abandon permit being issued. The Annual Statement of Production has not been updated and the well is not legibly identified. |
1104873354 | 2016-04-06 | UrbanProduction Wells | No Violations | I conducted a compliance notice follow-up inspection on this well. The well has 7 casing with 4.5 production casing with a swage and non functional pressure gauge on it. There is a sales line from the well but no production has been shown on this well since 2003. There is no associated tank battery with this well. There is no identification of any kind on or around the wellhead. There have been no changes since the last inspection report on 10/13/15. |
1472060937 | 2017-04-19 | Production Wells | No Violations | I conducted a Chiefs Order Follow-up inspection on this well for Chiefs Order 2017-79 issued 03-07-2017. The well has not been plugged as ordered. The master valve and the sales line valve are open. The well consists of a 7 casing with 4.5 production casing with a swage with a broken gauge on top. There is a sales line attached to the well above the master valve. No tank battery has been located at this time and no other flow lines or sale line have been found. The well is not legibly identified. No Annual Production Reports have been submitted since 2009. This well is currently incapable of production. |
1691130336 | 2018-11-23 | Production Wells | No Violations | My inspection found Chiefs Order #2017-79 for Plugging Required has not been complied with. The well is not plugged. No tank battery has been located for this well. I called 330-472-1389 and requested a return call. |
1801851805 | 2016-12-27 | Production Wells | No Violations | I conducted a compliance notice follow up inspection on this well. Th well has not been plugged. A compliance notice was issued to plug the well on 1/28/2014 by Inspector Fred Romeo. Plugging of the well was required by 4/22/2014. The well has 7 casing with 4.5 production casing with a swage. The swage has a closed valve on it followed by a broken pressure gauge. There is a sales line from the well. No tank battery or other production equipment has been located. The record shows zero production from 2003-2009 and no annual production reports submitted since 2009. The well is not legibly identified. |
1862204131 | 2019-05-02 | Production Wells | No Violations | My inspection found Chiefs Order #2017-79 for Plugging Required has not been complied with. The well is not plugged. No tank battery has been located for this well. I spoke with Randy Hall (330-472-1389), he advised me the State of Ohio has taken his bond. |
1917409981 | 2017-07-12 | Production Wells | No Violations | I conducted a Chiefs Order Follow-up inspection on this well for Chiefs Order 2017-79 issued 03-07-2017. The well is not plugged as ordered. The master valve and the sales line valve are open. The well consists of a 7 casing with 4.5 production casing with a swage with a broken gauge on top. There is a sales line attached to the well above the master valve. No tank battery has been located at this time and no other flow lines or sale line have been found. The well is not legibly identified. |
1986769764 | 2014-01-28 | Production Wells | Violations Noted | I was on location to perform a status check of this well. There is no associated tank battery with this well. The well has 7 casing with 4.5 production casing with a swage and non functional pressure gauge on it. There is a sales line from the well but no production has been shown on this well since 2003. There is no identification of any kind on or around the well head. Production for this well needs to be submitted and identification put on the well head. This well must either be plugged or put into production. |
2021223456 | 2015-10-13 | Production Wells | No Violations | I was on location to perform compliance notice follow up inspection on this well. A compliance notice was issued to plug the well on 1/28/2014. Plugging was required by 4/22/2014. There is no associated tank battery with this well. The well has 7 casing with 4.5 production casing with a swage and non-functional pressure gauge on it. There is a sales line from the well but no production has been shown on this well since 2003. There is no identification of any kind on or around the well head. This well is currently incapable of production. At this time there has been no change since the previous inspection and no attempt to plug the well. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1986769764 | US-OH-120120 | 2014-02-05 | Failure to legibly identify well | |
1986769764 | US-OH-120121 | 2014-02-05 | Well shall be plugged | |
1986769764 | US-OH-120122 | 2014-02-05 | Statement of annual production not filed |
For data sources see[8]