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Difference between revisions of "34-111-24737"

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| County: [[Monroe_County,_Ohio|Monroe]]
 
| County: [[Monroe_County,_Ohio|Monroe]]
 
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| Municipality: [[Center Township,_Monroe_County,_Ohio|Center Township]]
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| Municipality: [[Center_Township,_Monroe_County,_Ohio|Center Township]]
 
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| Operator Name: [[GULFPORT ENERGY CORPORATION]]
 
| Operator Name: [[GULFPORT ENERGY CORPORATION]]

Revision as of 12:10, 29 August 2019

Well Details

Well ID: 34-111-24737
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Country: United States
State: Ohio
County: Monroe
Municipality: Center Township
Operator Name: GULFPORT ENERGY CORPORATION
Well Pad ID: US-OH-001471
Farm/Lease Name: SCHUMACHER 210617
License Status: Well Drilled
License Date: 2017-06-07
Spud Date: 2017-05-17
Spud Drilling Contractor: PI0NEER DRLG
Final Drill Date: 2017-08-27
Well Total Depth: 17000 ft
Configuration: Horizontal
Latitude: 39.781288261
Longitude: -81.09086688

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2017-04-27 Proposed Formations:TRENTON, Issued Date:4/27/2017, Expired Date:4/27/2019 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT
APP 2017-06-07 Proposed Formations:UTICA/POINT PLEASANT, Issued Date:6/7/2017, Expired Date:6/7/2019 12:00:00 PM, Drilling unit acres:511.134, Proposed Well Type:OG, Proposed Well Class:EOUT
Reached Total Depth 2017-08-27 STATUS PER OPERATOR TELEPHONE CONVERSATION ALE 03/12/2018
Correction to Well 2018-08-24 TAKE TARGET AS-DRILLED
Record Last Modified 2019-04-15 STATUS PER OPERATOR TELEPHONE CONVERSATION ALE 03/12/2018
Construction Permit Expires 2019-06-07 STATUS PER OPERATOR TELEPHONE CONVERSATION ALE 03/12/2018

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0239882308 2019-03-07 Drill / Deepen / Reopen No Violations On this day, I am accompanied by ODNR Southeast Supervisor Brent Bear to conduct a follow-up inspection in regard to annular pressures. The current pressure reading on the 9.625 inch diameter casing is 1,400 pounds per square inch, and the pressure on the 13.375 inch diameter surface casing is 0 psi.
0330007150 2019-03-06 Drill / Deepen / Reopen No Violations On this day, I found the pad gated with signage at the entrance. There are (6) wells on the pad that have been drilled, but not completed. Steel fencing surrounds the perimeter of the wellheads. Each well has annular pressure monitoring devices equipped. Also noted, each well has signage stating that a back pressure valve (BPV) is installed. The 9.625 inch diameter intermediate casing has a pressure of 1,400 pounds per square inch (psi), and the 13.375 inch diameter surface casing has a pressure of 0 psi. I contacted Gulfport Energy Production Superintendent Justin Hoague to inform him of the pressures. Gulfport Representative Josh Starcher arrived onsite, and he made contact with additional Gulfport personnel. Pro-flow will be onsite within the next 48 hours to bleed the pressure down into a gas-buster tank. I informed Mr. Starcher to inform me of any updates. He also noted that the wells were recently equipped with pressure gauges. It was indicated that the wells may be completed in 2020.
0439559514 2019-03-08 Drill / Deepen / Reopen No Violations I am onsite to witness Pro-Flow bleed down the pressure of the 9.625 inch diameter intermediate casing. They are currently connecting the iron to the gas buster and will pressure test the lines prior to flowing into the tank. I spoke with Gulfport Representative Josh Starcher onsite and informed him to monitor the pressures, and update ODNR with the new pressures after 24 hours.
0460951866 2017-05-18 Casing String Witnessed No Violations On site inspection to witness the conductor casing cement job with Rocky Mountain Drillings top hole rig and Stingray Cement Service. Rock Mountain has drilled a 32 diameter borehole to 110 from ground level and ran 26 diameter .375 wall weld connection casing. Stingray cemented the casing using a 61 barrel cement mix consisting of 280 sacks of class A cement with 40% open hole cement excess ran. The cement weight was verified by weight of scale and displaced to 100 with 62 barrels of fresh water. 15 barrels of 6% gel spacer was pumped ahead of the cement.42 barrels of cement returns were witnessed to surface.
1900082606 2017-11-01 Preliminary Restoration No Violations Preliminary Restoration status check inspection found the area affected by the well pad construction has vegetation established and erosion control in place. The lease road and well pad is of stone construction with the well pad entrance gated. Signage is present at the lease road entrance off of State Route 26. There are 6 wells on the pad that has been drilled but not completed. No production equipment has been placed on the well pad at the time of my inspection.
1902522118 2019-03-11 Drill / Deepen / Reopen No Violations On this day, I am conducting a follow-up inspection to report the annular pressures. The 9.625 inch diameter intermediate casing is currently at 0 pounds per square inch, and 13.375 inch diameter surface casing is at 0 psi. I spoke with Gulfport Representative Josh Starcher on 3/9/19 and 3/10/19. Pro-Flow was onsite for those days and had flowlines connected from the wellhead to a gas buster tank. The 9.625 inch diameter intermediate casing was blown down to 0 psi from 1,500 psi on 3/08/19, returning 4 barrels of fluid. The pressure recovered to 300 psi on 3/9/19, and blown down to 0 psi, returning 2 barrels of fluid. The pressure stabilized at 0 psi on 3/10/19.

For data sources see[3]

References