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| County: [[Monroe_County,_Ohio|Monroe]] | | County: [[Monroe_County,_Ohio|Monroe]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Adams_Township,_Monroe_County,_Ohio|Adams Township]] |
|- | |- | ||
| Operator Name: [[ECLIPSE RESOURCES I LP]] | | Operator Name: [[ECLIPSE RESOURCES I LP]] | ||
Line 235: | Line 235: | ||
| style="text-align: right;" | 836 | | style="text-align: right;" | 836 | ||
|- | |- | ||
− | | Poly(oxy-1,2-ethanediyl), alpha-(4-nonylphenyl)-omega-hydroxy-, branched | + | | Poly(oxy-1,2-ethanediyl), alpha-(4-nonylphenyl)-omega-hydroxy-, |
+ | branched | ||
| 127087-87-0 | | 127087-87-0 | ||
| style="text-align: right;" | 5 | | style="text-align: right;" | 5 |
Well ID: 34-111-24797 | Loading map...
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Country: United States | |
State: Ohio | |
County: Monroe | |
Municipality: Adams Township | |
Operator Name: ECLIPSE RESOURCES I LP | |
Well Pad ID: US-OH-001512 | |
Farm/Lease Name: WILEY D | |
License Status: Producing | |
License Date: 2017-10-24 | |
Spud Date: 2018-02-26 | |
Spud Drilling Contractor: H&P DRILLING | |
Final Drill Date: 2018-04-02 | |
Well Total Depth: 30130 ft | |
Configuration: Horizontal | |
Latitude: 39.745557995 | |
Longitude: -80.98963951 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2017-10-24 | Proposed Formations:UTICA/POINT PLEASANT, Issued Date:10/24/2017, Expired Date:10/24/2019 12:00:00 PM, Drilling unit acres:327.64, Proposed Well Type:OG, Proposed Well Class:EOUT |
Correction to Well | 2018-03-09 | CHANGE TO UNIT SIZE, TAKE-POINT AND TARGET INFORMATION. |
Reached Total Depth | 2018-04-02 | |
Correction to Well | 2018-05-11 | updated take point and target on as drilled plat. TE |
Completion Report Received | 2018-10-31 | |
Record Last Modified | 2018-11-02 | |
Construction Permit Expires | 2019-10-24 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2018-11-01 | 10626 | 10792 | 0 |
2018-11-01 | 29860 | 29958 | 0 |
For data sources see[3]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 05/25/2018 | 07/07/2018 | 10452 | 37,849,500.0 | 0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | SAND-PREMIUM WHITE-40/70, BULK | Halliburton | Proppant | Listed Below | Listed Below | 0 | 0 | 0 |
HYDROCHLORIC ACID | Halliburton | Solvent | Listed Below | Listed Below | 0 | 0 | 0 | |
Crystalline silica, quartz | 14808-60-7 | 100 | 11.2184 | 40,109,600.0 | ||||
Hydrochloric acid | 7647-01-0 | 15 | 0.032272 | 115383 | ||||
Sodium Hydroxide | 1310-73-2 | 4 | 0.000960882 | 3436 | ||||
Crystalline silica, cristobalite | 14464-46-1 | 30 | 0.0759202 | 271440 | ||||
Ammonium Persulfate | 7727-54-0 | 95 | 0.00138382 | 4948 | ||||
Propargyl alcohol | 107-19-7 | 10 | 0.00003896 | 140 | ||||
Heavy aromatic petroleum naphtha | 64742-94-5 | 30 | 0.000118784 | 425 | ||||
Silica, amorphous - fumed | 7631-86-9 | 30 | 0.0759202 | 271440 | ||||
Oxyalkylated phenolic resin | Proprietary | 30 | 0.000158379 | 567 | ||||
Distillates (petroleum, hydrotreated light) | 64742-47-8 | 18 | 0.012655 | 45246 | ||||
Ammonium Chloride | 12125-02-9 | 1.5 | 0.000958299 | 3427 | ||||
Methanol | 67-56-1 | 60 | 0.000233782 | 836 | ||||
Poly(oxy-1,2-ethanediyl), alpha-(4-nonylphenyl)-omega-hydroxy-,
branched |
127087-87-0 | 5 | 0.00001980 | 71 | ||||
Citric acid | 77-92-9 | 60 | 0.00162953 | 5827 | ||||
Fatty acids, tall oil | Proprietary | 30 | 0.000116891 | 418 | ||||
Naphthalene | 91-20-3 | 5 | 0.00001980 | 71 | ||||
Mullite | 1302-93-8 | 100 | 0.253067 | 904800 | ||||
Ethoxylated alcohols | Proprietary | 30 | 0.000116891 | 418 | ||||
Aluminum Silicate | 1302-76-7 | 100 | 0.253067 | 904800 | ||||
1,2,4 Trimethylbenzene | 95-63-6 | 1 | 0.00000396 | 15 | ||||
Modified thiourea polymer | Proprietary | 30 | 0.000116891 | 418 | ||||
Organic phosphate copolymer | 71050-62-9 | 25 | 0.00345448 | 12351 | ||||
Ethanol | 64-17-5 | 60 | 0.000237568 | 850 | ||||
Olefins | Proprietary | 5 | 0.00004676 | 168 | ||||
Poly(oxy-1, 2-ethanediyl), a-tridecyl-w-hydroxy,branched | 69011-36-5 | 20 | 0.00462151 | 16524 | ||||
Dazomet | 533-74-4 | 24 | 0.00576529 | 20613 | ||||
HP-2816 | OneAqua | Friction Reducer | Listed Below | Listed Below | 0 | 0 | 0 | |
SAND-COMMON WHITE-100 MESH, SSA-2, BULK (100003676) | Halliburton | Proppant | Listed Below | Listed Below | 0 | 0 | 0 | |
HP-2220 | OneAqua | Scale Inhibitor | Listed Below | Listed Below | 0 | 0 | 0 | |
HP-9601 | OneAqua | Additive | Listed Below | Listed Below | 0 | 0 | 0 | |
HAI-OS ACID INHIBITOR | Halliburton | Corrosion Inhibitor | Listed Below | Listed Below | 0 | 0 | 0 | |
Ingredients | Listed Above | Listed Above | Water | 7732-18-5 | 100 | 0.216776 | 775048 | |
MB-7530 | OneAqua | Biocide | Listed Below | Listed Below | 0 | 0 | 0 | |
Fresh Water | Operator | Base Fluid | Water | 7732-18-5 | 100 | 88.1836 | 315,285,000.0 | |
FE-2A | Halliburton | Additive | Listed Below | Listed Below | 0 | 0 | 0 | |
HP-2814 | OneAqua | Friction Reducer | Listed Below | Listed Below | 0 | 0 | 0 | |
PROP-CERAMIC-30/50, BULK (101297495) | Halliburton | Proppant | Listed Below | Listed Below | 0 | 0 | 0 | |
OILPERM A | Halliburton | Non-ionic Surfactant | Listed Below | Listed Below | 0 | 0 | 0 |
For data sources see[4]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2018-07-07 | H2O | 15 | 373048 Gal | 444245 | Halliburton | STAGE 93/93
STAGES 2-92 SEE IMAGES |
2018-05-25 | H2O | 15 | 424659 Gal | 445530 | Halliburton | STAGE 1/93
STAGES 2-92 SEE IMAGES |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2018 | ECLIPSE RESOURCES I LP | 4766729 | 0 | 122 |
2019 | ECLIPSE RESOURCES I LP | 2184620 | 0 | 90 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2018 | ECLIPSE RESOURCES I LP | Brine | 117941 | 122 |
2019 | ECLIPSE RESOURCES I LP | Brine | 34798 | 90 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0255281240 | 2018-11-28 | Production Wells | No Violations | Status check inspection found 4 wells are present on the pad and all 4 wells are now in production. The said well is equipped with a lower A and upper B section with annular pressure monitoring in place on both well head sections. No annular pressure was found on this day on the A or B well head section. The well is producing off the 5.5 diameter production casing through (2) 3.5 diameter flow lines with both flow line valves open. The 5.5 casing pressure is 2,343 pounds per square inch (psi) and the flow line pressures are 1,400 psi and 1,200 psi. There is one manual master 7.0625 completion valve still on the well head B section that the well is being produced through. Each of the (2) flow lines has a separate glycol heater and downstream from the Glycol heater is a contact tower and B-Tex Condenser followed by third party mid stream Eureka Hunter pipeline station point. Also on location is a production fluid facility that consists of (6) 400 barrel production tanks situated inside a polymer lined steel containment dike area. Proper well identification is posted and hazard warning labeling is present at the production facility. Signage is posted at the well pad entry point and the well pad perimeter is protected by an earthen berm. |
0620822084 | 2018-07-30 | Completion Testing | No Violations | On this day, I accompanied ODNR Inspector William Stolarik. Please reference his comments for a detailed report. We are onsite witnessing Halliburton, 9 Energy, and S3 Pump Service conducting hydraulic fracturing operations. This particular well was completed with 93 total stages. |
1520353073 | 2018-03-06 | Drill / Deepen / Reopen | No Violations | |
1532967827 | 2018-07-30 | Completion Testing | No Violations | Status check inspection found the well drilling and completion process complete. Halliburton Pressure pumping service is on location and has stimulated 93 stages total with an initial shut in pressure of 6,400 pounds per square inch pressure. The 9.625 x 5.5 annular pressure is being monitored and is currently 22 psi. |
1534436267 | 2018-08-16 | Completion Testing | No Violations | Status check inspection on the well completion process found the well drilling and stimulation process complete. The well was stimulated in 95 stages with the last plug # 94 set at 29,000. The 5.5 diameter production casing was set to a depth of 30,098. The well head assembly consists of a lower A and upper B section with a production flow cross present followed by two 7.0625 diameter FMC manually operated master valves. The annular pressures are being monitored daily. A completion rig owned by Deep Well Service and identified as Snub unit # 10 is rigged up on Yellow Rose A 2 H drilling out the completion plugs maintaining well control using 10 pound per gallon brine. There are a total of 4 wells on the pad and the snubbing unit is drilling out the 1st one. No production tubing is scheduled to be set in the well. |
1751423329 | 2018-05-17 | Completion Testing | No Violations | On this day, I accompanied ODNR Inspector William Stolarik. Please refer to his comments for a detailed report. |
1762551719 | 2018-05-17 | Completion Testing | No Violations | Status check inspection found the well drilling process is complete and the well has the completion well head installed and has also had the 5.5 production string toe prep procedure and final pressure test conducted. The well is awaiting the start of the stimulation process in the next 10 days, Halliburton completion service will mobilize and begin. All completion equipment will be placed on polymer containment. All surface water created on the well pad due to the recent rain events is being removed by the means a vacuum truck. The perimeter drain valves are closed. |
For data sources see[10]