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| County: [[Medina_County,_Ohio|Medina]] | | County: [[Medina_County,_Ohio|Medina]] | ||
|- | |- | ||
− | | Municipality: [[Westfield Center | + | | Municipality: [[Westfield Center,_Medina_County,_Ohio|Westfield Center]] |
|- | |- | ||
| Operator Name: [[MFC DRILLING INC]] | | Operator Name: [[MFC DRILLING INC]] |
Well ID: 34-103-21507 | Loading map...
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Country: United States | |
State: Ohio | |
County: Medina | |
Municipality: Westfield Center | |
Operator Name: MFC DRILLING INC | |
Well Pad ID: | |
Farm/Lease Name: BOBIER JACK | |
License Status: Final Restoration | |
License Date: 2002-10-18 | |
Spud Date: 1965-03-18 | |
Spud Drilling Contractor: CO TOOLS | |
Final Drill Date: 1965-04-15 | |
Well Total Depth: 3343 ft | |
Configuration: Vertical | |
Latitude: 41.023638356 | |
Longitude: -81.91976684 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1965-03-18 | QUADRANGLE=( LEROY ) NOT IN DROP DOWN BOX |
Completed | 1965-04-15 | QUADRANGLE=( LEROY ) NOT IN DROP DOWN BOX |
Reached Total Depth | 1965-04-15 | QUADRANGLE=( LEROY ) NOT IN DROP DOWN BOX |
CO | 1984-05-21 | 255 KING DRILLING CO GeoDate 5/21/84 |
Unknown | 1984-05-21 | Issued Date 5/21/84 Expired Date 11/17/84 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Change of Owner | 2002-09-06 | Operator changed from 255, KING DRILLING CO to 3059, MFC DRILLING INC |
APP | 2002-10-18 | Proposed Formations:CLINTON, Issued Date:10/18/2002, Expired Date:10/18/2003 6:00:00 AM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2003-02-03 | QUADRANGLE=( LEROY ) NOT IN DROP DOWN BOX |
Construction Permit Expires | 2003-10-18 | QUADRANGLE=( LEROY ) NOT IN DROP DOWN BOX |
Record Last Modified | 2017-02-15 | QUADRANGLE=( LEROY ) NOT IN DROP DOWN BOX |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2002-04-04 | 3213 | 3275 | 16 |
2006-09-11 | 3254 | 3275 | 1 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1200 Bbl | 34000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | KING DRILLING CO | 155 | 17 | 0 |
1985 | KING DRILLING CO | 0 | 0 | 0 |
1986 | KING DRILLING CO | 3 | 19 | 365 |
1995 | KING DRILLING CO | 0 | 8 | 365 |
1996 | KING DRILLING CO | 0 | 16 | 365 |
1997 | KING DRILLING CO | 0 | 0 | 365 |
1998 | KING DRILLING CO | 0 | 15 | 365 |
1999 | KING DRILLING CO | 0 | 9 | 365 |
2000 | KING DRILLING CO | 0 | 7 | 365 |
2001 | KING DRILLING CO | 0 | 13 | 365 |
2002 | KING DRILLING CO | 0 | 9 | 365 |
2003 | KING DRILLING CO | 0 | 0 | 365 |
2004 | KING DRILLING CO | 0 | 0 | 365 |
2005 | KING DRILLING CO | 0 | 0 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | KING DRILLING CO | Brine | 0 | 0 |
1985 | KING DRILLING CO | Brine | 0 | 0 |
1986 | KING DRILLING CO | Brine | 0 | 365 |
1995 | KING DRILLING CO | Brine | 0 | 365 |
1996 | KING DRILLING CO | Brine | 0 | 365 |
1997 | KING DRILLING CO | Brine | 0 | 365 |
1998 | KING DRILLING CO | Brine | 0 | 365 |
1999 | KING DRILLING CO | Brine | 0 | 365 |
2000 | KING DRILLING CO | Brine | 0 | 365 |
2001 | KING DRILLING CO | Brine | 0 | 365 |
2002 | KING DRILLING CO | Brine | 0 | 365 |
2003 | KING DRILLING CO | Brine | 0 | 365 |
2004 | KING DRILLING CO | Brine | 0 | 365 |
2005 | KING DRILLING CO | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0010979085 | 2002-04-04 | Production Wells | No Violations | 4-3-2002 - Received complaint call from Mark Steigerwald; 40 Oakwood Dr., P.O. Box 139, Westfield Center, Ohio 44251; Phone # 330-887-5136; regarding a well located aprox. 10 feet from his condo. On 4-4-2002, ODNR/MRM Inspectors Dave Claus and Bob Worstall inspected the site. The well was shut-in and consisted of 4-1/2 dia. Casing swedged down to a 1/4 dia. Gauge. A single stock tank was located east of Ironwood drive. Inspector Claus called Andrew King of King Drilling and requested the status of the well. King stated that the Bobier #4 has been shut-in along with 3 other wells located on Westfield Golf Course. The single common stock tank for all 4 wells has been emptied along with the brine tank. A permit to plug the Bobier # 4 was issued in 1984, but was never used. RBDMS shows production thru the year 2000. King Drilling submitted a proposal for Westfield Golf Course and Westfield Condo Assoc. to purchase and plug all 4 wells over a year ago and has received no response. King Drilling is still responsible for these 4 wells. NO VIOLATIONS. ODNR/MRM will follow-up in 2 months with King Drilling to check on the status of these wells. King Drilling has been told to place I.D. signs on the 4 wells and on the common tank battery. |
0589602975 | 2003-01-27 | Plug / Plug Back | No Violations | Locate well in development. Well is 10 from home foundation. Working with Pluggers Inc. on plugging procedure. 10 degrees 8 of snow. |
1373559712 | 2003-09-02 | Final Restoration | No Violations | Final restoration approved. Yard of Condo. 70 degrees, Rain. |
For data sources see[9]