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| County: [[Ashland_County,_Ohio|Ashland]] | | County: [[Ashland_County,_Ohio|Ashland]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Mifflin_Township,_Ashland_County,_Ohio|Mifflin Township]] |
|- | |- | ||
| Operator Name: [[COLUMBIA GAS TRANSMISSION LLC]] | | Operator Name: [[COLUMBIA GAS TRANSMISSION LLC]] |
Well ID: 34-139-20434 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashland | |
Municipality: Mifflin Township | |
Operator Name: COLUMBIA GAS TRANSMISSION LLC | |
Well Pad ID: | |
Farm/Lease Name: L A MILLER #2 | |
License Status: Final Restoration | |
License Date: 2017-10-11 | |
Spud Date: 1966-09-05 | |
Spud Drilling Contractor: | |
Final Drill Date: 1966-10-14 | |
Well Total Depth: 2397 ft | |
Configuration: Vertical | |
Latitude: 40.739166401 | |
Longitude: -82.35744122 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1966-09-05 | STORAGE-2, GL=981.75 UPDATE LOCATION PER DOGRM SURVEYOR ALE 12-11-17. |
Completed | 1966-10-14 | STORAGE-2, GL=981.75 UPDATE LOCATION PER DOGRM SURVEYOR ALE 12-11-17. |
Reached Total Depth | 1966-10-14 | STORAGE-2, GL=981.75 UPDATE LOCATION PER DOGRM SURVEYOR ALE 12-11-17. |
Change of Owner | 2011-10-18 | Operator changed from 9998, HISTORIC OWNER to 22, COLUMBIA GAS TRANSMISSION |
APP | 2017-10-11 | Proposed Formations:CLINTON SANDSTONE, Issued Date:10/11/2017, Expired Date:10/11/2019 12:00:00 PM, Drilling unit acres:54, Proposed Well Type:SO, Proposed Well Class: |
Plugged/Abandoned | 2017-11-15 | STORAGE-2, GL=981.75 UPDATE LOCATION PER DOGRM SURVEYOR ALE 12-11-17. |
Record Last Modified | 2018-06-05 | STORAGE-2, GL=981.75 UPDATE LOCATION PER DOGRM SURVEYOR ALE 12-11-17. |
Construction Permit Expires | 2019-10-11 | STORAGE-2, GL=981.75 UPDATE LOCATION PER DOGRM SURVEYOR ALE 12-11-17. |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0094403984 | 2017-12-04 | Plug / Plug Back | No Violations | The operator has not completed restoration of the location yet. The well was plugged 11/15/17. The well is cut off with a plate on it and is exposed. No leakage observed. The road and sediment controls remain at the location. Grading also needs to be completed. The rig and associated equipment are off location. No pits were used during the workover. All fluid was contained to portable tanks and roll off containers. |
0130979276 | 2015-08-27 | Work Over Reconditioning | No Violations | The operator requested an inspection to witness production casing cement. See the casing ticket for details. |
0412573197 | 2014-04-11 | Storage Well | No Violations | There is no API number on the ID. The lease name and operator well number are written on the sign. The well is located in a swamp. |
0537379684 | 2015-10-14 | Storage Well | No Violations | The well is shut in. The rig is off location. There is a swage on the production casing with a 2.5 inch valve and pressure gauge on it. The valve is closed and the gauge is reading 0. The annulus is filled solid with cement. |
0785135556 | 2016-02-26 | Work Over Reconditioning | No Violations | The operator is replacing the production casing. The previous replacement was found to have defective threads. The new casing was connected to the previously installed cemented casing above the cement top at 1900 feet. New casing was used because the previously installed pipe had defective threads. The defects were not evident at the time the casing was installed. The replacement casing was installed with a cementing tool (DV tool). The rig crew was having difficulty with the ports on the tool operating properly and had to run a slick line to the tool to activate it. |
0788535947 | 2016-02-26 | Work Over Reconditioning | No Violations | Columbia Gas requested an inspection to witness cementing of the new pipe. The cementing tool was successfully activated yesterday evening. The cement crew was delayed an hour from the scheduled time. See the casing ticket for details. |
0923534960 | 2018-03-06 | Plug / Plug Back | No Violations | The operator still has to remove silt fencing to complete final restoration. The well location is flooded. |
0999063580 | 2018-01-17 | Plug / Plug Back | No Violations | The well was plugged on 11/15/17. The operator has started restoration work on the location. The lease road has been partially removed and the well is cut off and buried. No personnel were working during inspection. The ground is snow covered. |
1116807711 | 2015-09-08 | Work Over Reconditioning | No Violations | The operator requested an inspection to witness topping up cement on the backside of the 5.5 inch casing to surface. The casing was originally cemented to surface and the cement top was located 30 feet down during the workover. The operator is going to use the 5.5 inch casing for the wellhead base. |
1134246027 | 2016-05-12 | Work Over Reconditioning | No Violations | The operator moved the service rig back on to the well to attempt to fish out drill collars and the drill bit. They are using a custom washover fishing tool and hydraulic jars. The tool became stuck on the drill collars. The operator is unable to release the fishing tool and they are unable to move the fish up or down the hole. The DV tool is at 1868 feet with cement on top of the tool. The 3.5 inch casing is cemented to surface. There is 120 feet of cement on top of the DV tool inside the production casing. The bit is stuck at 1749 feet and there are 3 drill collars above the bit. The operator may be plugging the well from the top of the jars and fishing equipment if they are unable to retrieve the tools in the well. |
1201579183 | 2017-11-02 | Storage Well | No Violations | The well is equipped with tubing on a casing head. The tubing is shut in. There is no pipeline equipment at the location. The operator has a plugging permit on the well. |
1456406268 | 2016-02-24 | Work Over Reconditioning | No Violations | The operator moved the rig back on to the well. They are milling inside the 5.5 inch casing. There is a tight spot at 262 feet. They are going to run new 3.5 inch casing down to the previous 3.5 inch casing top and cement back to surface. |
1510761945 | 2017-11-15 | Plug / Plug Back | No Violations | The operator requested inspection to witness plugging the well. See the plug report for details. |
1514756259 | 2017-11-16 | Plug / Plug Back | No Violations | Columbia Gas cut the casing off at 3 feet below grade and installed a steel plate with the permit number on the well. Cement was just below the cut off casing. |
1525719729 | 2018-05-07 | Final Restoration | No Violations | The location has been finish graded. Sediment controls have been removed. The road is reclaimed up to the lawn of the house. Seed has been planted on the disturbed area. No other equipment or debris is at the location. A landowner waiver is required for the portion of road to be left for the landowners driveway. |
1847459046 | 2016-03-10 | Work Over Reconditioning | No Violations | The operator attempted to fish drill collars and the bit with a specialty fishing tool. The rig was able to grab the fish but the tool broke at approximately 50% of its rated load when the rig attempted to pull the collars from the well. The operator is deciding whether to have washover pipe made and make another attempt at salvaging the well. |
2013521809 | 2016-03-14 | Work Over Reconditioning | No Violations | The rig is off the well and off location. The support equipment for the rig is off location. The company is moving to another well. The company representative on location stated that they were having washover pipe made and would make another attempt to fish the collars and bit from the well. The custom pipe is going to take approximately 2 weeks to manufacture and deliver to the location. The operator has decided to continue their workover schedule and come back to this well at a later date. The well is shut in with an API wellhead on it. |
2137952426 | 2016-03-07 | Work Over Reconditioning | No Violations | The operator is attempting to recover the drill string from the well. The drill collars sheared off three joints up from the bit. The operator milled the top of the string and they are trying to fish it out with an overshot tool. |
For data sources see[4]