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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 37-059-01966 | | Well ID: 37-059-01966 | ||
| − | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 39.974881, -80.043272 | width=100% | height=100% }} |
|- | |- | ||
| Country: United States | | Country: United States | ||
| Line 19: | Line 19: | ||
| Farm/Lease Name: FREDERICKTOWN REAL ESTATE 102 | | Farm/Lease Name: FREDERICKTOWN REAL ESTATE 102 | ||
|- | |- | ||
| − | | License Status: | + | | License Status: |
|- | |- | ||
| − | | Spud Date: | + | | Spud Date: |
|- | |- | ||
| Permit Date: | | Permit Date: | ||
| + | |- | ||
| + | | Well Type: GAS | ||
|- | |- | ||
| Unconventional Well: N | | Unconventional Well: N | ||
|- | |- | ||
| Configuration: Vertical Well | | Configuration: Vertical Well | ||
| + | |- | ||
| + | | Conservation: No | ||
|- | |- | ||
| Latitude: 39.974881 | | Latitude: 39.974881 | ||
| Line 49: | Line 53: | ||
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
| accessdate = 2019-05-21 }}</ref> | | accessdate = 2019-05-21 }}</ref> | ||
| + | == Well History == | ||
| + | {| class="wikitable sortable" width="95%" | ||
| + | !scope="col" | Date | ||
| + | !scope="col" | Event | ||
| + | |- | ||
| + | | 1901-01-01 | ||
| + | | Drilling Completion | ||
| + | |- | ||
| + | | 1996-11-22 | ||
| + | | OLD WELL | ||
| + | |- | ||
| + | |} | ||
| + | For data sources see<ref>{{cite web | ||
| + | | title = Compiled from multiple data sources - see Pennsylvania Oil and Gas Data Sources | ||
| + | | date = 2020-02-27 | ||
| + | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
| + | | accessdate = 2020-02-27 }}</ref> | ||
<!--== Fracking Activities == | <!--== Fracking Activities == | ||
==== Fracking Jobs ==== | ==== Fracking Jobs ==== | ||
| Line 71: | Line 92: | ||
!scope="col" | Job Percentage by Mass | !scope="col" | Job Percentage by Mass | ||
!scope="col" | Mass Used (lb) | !scope="col" | Mass Used (lb) | ||
| + | |- | ||
| + | |}--> | ||
| + | |||
| + | <!--== Stimulation Data == | ||
| + | {| class="wikitable sortable" width="95%" | ||
| + | !scope="col" | Stimulation Date | ||
| + | !scope="col" | Phase Number | ||
| + | !scope="col" | Chemical Agent | ||
| + | !scope="col" | Volume (gal) | ||
| + | !scope="col" | Treating Pressure (psi) | ||
| + | !scope="col" | Breakdown Pressure (psi) | ||
|- | |- | ||
|}--> | |}--> | ||
| Line 90: | Line 122: | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
!scope="col" | Period | !scope="col" | Period | ||
| + | !scope="col" | Operator | ||
!scope="col" | Waste Type | !scope="col" | Waste Type | ||
!scope="col" | Quantity | !scope="col" | Quantity | ||
| Well ID: 37-059-01966 | Loading map...
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| Country: United States | |
| State: Pennsylvania | |
| County: Greene | |
| Municipality: Morgan Township | |
| Operator Name: OIL & GAS SVC INC | |
| Well Pad ID: | |
| Farm/Lease Name: FREDERICKTOWN REAL ESTATE 102 | |
| License Status: | |
| Spud Date: | |
| Permit Date: | |
| Well Type: GAS | |
| Unconventional Well: N | |
| Configuration: Vertical Well | |
| Conservation: No | |
| Latitude: 39.974881 | |
| Longitude: -80.043272 |
| Date | Event |
|---|---|
| 1901-01-01 | Drilling Completion |
| 1996-11-22 | OLD WELL |
For data sources see[4]
| Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|---|
| 2107569 | Primary Facility | 2012-10-02 | Routine/Complete Inspection | No Violations Noted | ROUTINE INSPECTION DONE ON WELL. CHECKED FOR GAS WITH GAS MONITOR. COULD NOT GET A READING. |
| 2467551 | Primary Facility | 2016-03-15 | Complaint Inspection | No Violations Noted | GPS coordinate: 39*-58'-31"N & - 80*-02'-37"W.The well shows gas readings between tree roots and casing. Level are 100+% LEL and 3%-6% gas.Observation shows tree roots causing wellhead to leak? Picture concludes the problem is tree planted to close to well. Follow- Up Inspection of prior complaint. It has a API# assigned already (059-01966).Well name is Fredericktown Real Estate 102 OG Well. |
| 2472335 | Primary Facility | 2016-04-07 | Routine/Complete Inspection | No Adverse Event or Action Reported | Went to site after inspection by Rick Lewis on 3/15/16. Wellhead is intact w/ 7" casing topped by casinghead w/ port plumbed w/ 2 1/4" tubing to drip, 4 1/2" casing topped by tee plumbed to drip & swaged to 2 1/4" tubing topped w/ plugged valve. Plug on casinghead is under stress by adjacent cherry tree root growing against it, and gas is leaking @ plug. |
| 2795661 | Primary Facility | 2018-10-29 | Routine/Partial Inspection | No Viols - Permanently Shut Down | Visited site to check the status of this abandoned well. Well is still leaking gas from around a plug on the casinghead that is under stress from growth of adjacent tree. Breezy day makes it difficult to determine how large the leak is, but it doesn't appear worse than 4/7/16 inspection. |
For data sources see[5]