X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

Difference between revisions of "37-059-25267"

m
m
 
(2 intermediate revisions by the same user not shown)
Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-059-25267
 
| Well ID: 37-059-25267
| style="height=100%; align=center" rowspan="14" | {{#display_map: 40.004867, -80.287747 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.004867, -80.287747 | width=100% | height=100% }}
 
|-
 
|-
 
| Country: United States
 
| Country: United States
Line 17: Line 17:
 
| Well Pad ID: [[147993]]
 
| Well Pad ID: [[147993]]
 
|-
 
|-
| Farm/Lease Name: CONRHEIN NV17CCV
+
| Farm/Lease Name: CONRHEIN
 
|-
 
|-
| License Status: Plugged OG Well
+
| License Status: Plugged and Abandoned
 
|-
 
|-
| Spud Date: 02/18/2010
+
| Spud Date:  
 
|-
 
|-
| Permit Date: 8/13/2009
+
| Permit Date: 2009-08-13
 +
|-
 +
| Well Type: GAS
 
|-
 
|-
 
| Unconventional Well: Y
 
| Unconventional Well: Y
 
|-
 
|-
 
| Configuration: Horizontal Well
 
| Configuration: Horizontal Well
 +
|-
 +
| Conservation: Yes
 
|-
 
|-
 
| Latitude: 40.004867
 
| Latitude: 40.004867
Line 49: Line 53:
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | accessdate = 2019-05-21 }}</ref>
 
  | accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Date
 +
!scope="col" | Event
 +
|-
 +
| 2009-08-13
 +
| New Permit Application
 +
|-
 +
| 2010-02-18
 +
| Performed Spud Operation
 +
|-
 +
| 2014-11-10
 +
| Begin Plugging
 +
|-
 +
| 2015-05-21
 +
| Finished Plugging
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Compiled from multiple data sources - see Pennsylvania Oil and Gas Data Sources
 +
| date = 2020-02-27
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-02-27 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Job Number
 +
!scope="col" | Job Start Date
 +
!scope="col" | Job End Date
 +
!scope="col" | True Vertical Depth (ft)
 +
!scope="col" | Total Water Volume (gal)
 +
!scope="col" | Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Job Number
 +
!scope="col" | Trade Name
 +
!scope="col" | Supplier
 +
!scope="col" | Purpose
 +
!scope="col" | Ingredient Name
 +
!scope="col" | CAS Number
 +
!scope="col" | Additive Percentage by Mass
 +
!scope="col" | Job Percentage by Mass
 +
!scope="col" | Mass Used (lb)
 +
|-
 +
|}-->
 +
 +
<!--== Stimulation Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Stimulation Date
 +
!scope="col" | Phase Number
 +
!scope="col" | Chemical Agent
 +
!scope="col" | Volume (gal)
 +
!scope="col" | Treating Pressure (psi)
 +
!scope="col" | Breakdown Pressure (psi)
 +
|-
 +
|}-->
 +
 
== Production Data ==
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 61: Line 124:
 
|-
 
|-
 
| 2009
 
| 2009
| style="text-align: right;" |
+
| [[CNX GAS CO LLC]]
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
| style="text-align: right;" |  
+
| style="text-align: right;" | 0
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
| style="text-align: right;" |  
+
| style="text-align: right;" | 0
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
| style="text-align: right;" |  
+
| style="text-align: right;" | 0
 
|-
 
|-
 
| 2010
 
| 2010
Line 142: Line 205:
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | Period
 
!scope="col" | Period
 +
!scope="col" | Operator
 
!scope="col" | Waste Type
 
!scope="col" | Waste Type
 
!scope="col" | Quantity
 
!scope="col" | Quantity
Line 147: Line 211:
 
!scope="col" | Waste Facility ID
 
!scope="col" | Waste Facility ID
 
|-
 
|-
| 16JANU
+
| 2013
| Produced Fluid (in Barrels) RWC 802
+
| [[CNX GAS CO LLC]]
| style="text-align: right;" | 82.50 Bbl
+
| Produced Fluid
 +
| style="text-align: right;" | 39.59 Bbl
 +
| INJECTION DISPOSAL WELL
 +
| 34-105-23619
 +
|-
 +
| 2013
 +
| [[CNX GAS CO LLC]]
 +
| Produced Fluid
 +
| style="text-align: right;" | 494.44 Bbl
 
| REUSE OTHER THAN ROAD SPREADING
 
| REUSE OTHER THAN ROAD SPREADING
 
|  
 
|  
 
|-
 
|-
| 2013-2
+
| 2013
| Produced Fluid (in Barrels)
+
| [[CNX GAS CO LLC]]
 +
| Produced Fluid
 +
| style="text-align: right;" | 10.11 Bbl
 +
| INJECTION DISPOSAL WELL
 +
| 34-031-27177
 +
|-
 +
| 2013
 +
| [[CNX GAS CO LLC]]
 +
| Produced Fluid
 
| style="text-align: right;" | 14.22 Bbl
 
| style="text-align: right;" | 14.22 Bbl
 
| INJECTION DISPOSAL WELL
 
| INJECTION DISPOSAL WELL
 
| 34-013-20609
 
| 34-013-20609
 
|-
 
|-
| 2013-2
+
| 2013
| Produced Fluid (in Barrels)
+
| [[CNX GAS CO LLC]]
| style="text-align: right;" | 10.11 Bbl
+
| Produced Fluid
| INJECTION DISPOSAL WELL
 
| 34-031-27177
 
|-
 
| 2013-2
 
| Produced Fluid (in Barrels)
 
 
| style="text-align: right;" | 5.54 Bbl
 
| style="text-align: right;" | 5.54 Bbl
 
| INJECTION DISPOSAL WELL
 
| INJECTION DISPOSAL WELL
 
| 34-059-24202
 
| 34-059-24202
 
|-
 
|-
| 2013-2
+
| 2013
| Produced Fluid (in Barrels)
+
| [[CNX GAS CO LLC]]
| style="text-align: right;" | 39.59 Bbl
+
| Produced Fluid
| INJECTION DISPOSAL WELL
 
| 34-105-23619
 
|-
 
| 2013-2
 
| Produced Fluid (in Barrels)
 
 
| style="text-align: right;" | 0.53 Bbl
 
| style="text-align: right;" | 0.53 Bbl
 
| INJECTION DISPOSAL WELL
 
| INJECTION DISPOSAL WELL
 
| 34-119-28776
 
| 34-119-28776
 
|-
 
|-
| 2013-2
+
| 2015
| Produced Fluid (in Barrels)
+
| [[CNX GAS CO LLC]]
| style="text-align: right;" | 494.44 Bbl
+
| Drilling Fluid Waste
| REUSE OTHER THAN ROAD SPREADING
 
|
 
|-
 
| 2015-1
 
| Drilling Fluid Waste (in Barrels)
 
 
| style="text-align: right;" | 1,269.33 Bbl
 
| style="text-align: right;" | 1,269.33 Bbl
 
| REUSE OTHER THAN ROAD SPREADING
 
| REUSE OTHER THAN ROAD SPREADING
 
|  
 
|  
 
|-
 
|-
| 2016-01
+
| 2016
| Produced Fluid (in Barrels) RWC 802
+
| [[CNX GAS CO LLC]]
 +
| Produced Fluid
 
| style="text-align: right;" | 82.50 Bbl
 
| style="text-align: right;" | 82.50 Bbl
 
| REUSE OTHER THAN ROAD SPREADING
 
| REUSE OTHER THAN ROAD SPREADING
Line 220: Line 286:
 
| 1867568
 
| 1867568
 
| Primary Facility
 
| Primary Facility
| 02/24/2010
+
| 2010-02-24
 
| Routine/Complete Inspection
 
| Routine/Complete Inspection
 
| No Violations Noted
 
| No Violations Noted
Line 227: Line 293:
 
| 1880487
 
| 1880487
 
| Primary Facility
 
| Primary Facility
| 03/24/2010
+
| 2010-03-24
 
| Routine/Complete Inspection
 
| Routine/Complete Inspection
 
| No Violations Noted
 
| No Violations Noted
Line 234: Line 300:
 
| 1881423
 
| 1881423
 
| Primary Facility
 
| Primary Facility
| 04/27/2010
+
| 2010-04-27
 
| Drilling/Alteration
 
| Drilling/Alteration
 
| No Violations Noted
 
| No Violations Noted
Line 241: Line 307:
 
| 1889660
 
| 1889660
 
| Primary Facility
 
| Primary Facility
| 05/18/2010
+
| 2010-05-18
 
| Routine/Complete Inspection
 
| Routine/Complete Inspection
 
| No Violations Noted
 
| No Violations Noted
Line 248: Line 314:
 
| 1895051
 
| 1895051
 
| Primary Facility
 
| Primary Facility
| 06/24/2010
+
| 2010-06-24
 
| Drilling/Alteration
 
| Drilling/Alteration
 
| No Violations Noted
 
| No Violations Noted
Line 255: Line 321:
 
| 1898832
 
| 1898832
 
| Primary Facility
 
| Primary Facility
| 06/21/2010
+
| 2010-06-21
 
| Routine/Complete Inspection
 
| Routine/Complete Inspection
 
| No Violations Noted
 
| No Violations Noted
Line 262: Line 328:
 
| 2362794
 
| 2362794
 
| Primary Facility
 
| Primary Facility
| 03/24/2015
+
| 2015-03-24
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
Line 269: Line 335:
 
| 2362871
 
| 2362871
 
| Primary Facility
 
| Primary Facility
| 04/10/2015
+
| 2015-04-10
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
Line 315: Line 381:
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | accessdate = 2019-05-21 }}</ref>
 
  | accessdate = 2019-05-21 }}</ref>
<!--== Fracking Activities ==
 
==== Fracking Jobs ====
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | Job Number
 
!scope="col" | Job Start Date
 
!scope="col" | Job End Date
 
!scope="col" | True Vertical Depth (ft)
 
!scope="col" | Total Water Volume (gal)
 
!scope="col" | Total Non-Water Volume (gal)
 
|-
 
|}-->
 
<!--==== Fluid Composition Data ====
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | Job Number
 
!scope="col" | Trade Name
 
!scope="col" | Supplier
 
!scope="col" | Purpose
 
!scope="col" | Ingredient Name
 
!scope="col" | CAS Number
 
!scope="col" | Additive Percentage by Mass
 
!scope="col" | Job Percentage by Mass
 
!scope="col" | Mass Used (lb)
 
|-
 
|}-->
 
 
 
==References==
 
==References==
 
<references/>
 
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Pennsylvania Wells]]
 
[[Category:Pennsylvania Wells]]

Latest revision as of 19:18, 14 May 2020

Well Details

Well ID: 37-059-25267
Loading map...
Country: United States
State: Pennsylvania
County: Greene
Municipality: Morris Township
Operator Name: CNX GAS CO LLC
Well Pad ID: 147993
Farm/Lease Name: CONRHEIN
License Status: Plugged and Abandoned
Spud Date:
Permit Date: 2009-08-13
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: Yes
Latitude: 40.004867
Longitude: -80.287747

For data sources see[1][2][3]

Well History

Date Event
2009-08-13 New Permit Application
2010-02-18 Performed Spud Operation
2014-11-10 Begin Plugging
2015-05-21 Finished Plugging

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2009 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2010 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2011 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2012 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2013 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2014 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2015 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2016 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2013 CNX GAS CO LLC Produced Fluid 39.59 Bbl INJECTION DISPOSAL WELL 34-105-23619
2013 CNX GAS CO LLC Produced Fluid 494.44 Bbl REUSE OTHER THAN ROAD SPREADING
2013 CNX GAS CO LLC Produced Fluid 10.11 Bbl INJECTION DISPOSAL WELL 34-031-27177
2013 CNX GAS CO LLC Produced Fluid 14.22 Bbl INJECTION DISPOSAL WELL 34-013-20609
2013 CNX GAS CO LLC Produced Fluid 5.54 Bbl INJECTION DISPOSAL WELL 34-059-24202
2013 CNX GAS CO LLC Produced Fluid 0.53 Bbl INJECTION DISPOSAL WELL 34-119-28776
2015 CNX GAS CO LLC Drilling Fluid Waste 1,269.33 Bbl REUSE OTHER THAN ROAD SPREADING
2016 CNX GAS CO LLC Produced Fluid 82.50 Bbl REUSE OTHER THAN ROAD SPREADING

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1867568 Primary Facility 2010-02-24 Routine/Complete Inspection No Violations Noted
1880487 Primary Facility 2010-03-24 Routine/Complete Inspection No Violations Noted Minor Modification to the ESCGP-1
1881423 Primary Facility 2010-04-27 Drilling/Alteration No Violations Noted WHIPSTOCK 23 MOVING, BUTCH'S ANCHOR SERVICE SETTING CONDUCTORS. PITS GOOD
1889660 Primary Facility 2010-05-18 Routine/Complete Inspection No Violations Noted The Department was at the above reference site to conduct a Waiver Inspection. The Operator has already built the site and is currently drilling Multiple Marcellus Wells on this pad. The Department approves the waiver for the 100 ft distance restriction to Bates Fork. Bates Fork is a tributary to Brown's Creek which is a High Quality Stream. The Department has reviewed the E/S plan and inspected the E/S Controls. All BMP's appear to be in good working order and the Operator should continue to inspect the site as needed..
1895051 Primary Facility 2010-06-24 Drilling/Alteration No Violations Noted HORIZONTAL MARCELLUS
1898832 Primary Facility 2010-06-21 Routine/Complete Inspection No Violations Noted Site and E/S Control in good condition.
2362794 Primary Facility 2015-03-24 Plugging(Includes Plugged/Mined Through) No Violations Noted Conserv rig on location in December, 2014 to plug CNX Marcellus lateral. Perf gun and wireline lost down hole.; left gun downhole; retrieved a lot of wirline. Set cast iron bridge plug @ 8000' and cemented from 8000' to 7525'; gel plug to 6500'; 2nd cement plug from 6500' to 6300'; get plug to 5300'; third cement plug from 5300 to 4750' over area where hole in 51/2' casing was found @ 5198'; TOC in 5 1/2" is 4370'; Bond log in 5 1/2' indicated no cement from 2750 to surface; Going to make cut @ 2740 to pull 5 1/2" casing out; Then a bond log will be run on 9 5/8" to confirm good cement bond or TOC as cement flash set and only 3 bbls was run down annulus.
2362871 Primary Facility 2015-04-10 Plugging(Includes Plugged/Mined Through) No Violations Noted Ran bond log behind the 9 5/8 from app 476 to surface; TOC is shown app.93' indicating a basket was placed on the casing; no cement bond from 93 feet down.;; will review with operator;
2787646 Primary Facility 2018-10-10 Routine/Complete Inspection No Violations Noted On Wednesday October 10, 2018 I conducted a routine-complete inspection at the NV17 Well Site located in Morris Township, Greene County.

Gas well NV17CCV (059-25267) was plugged in 2015 and a monument identifies the location and permit number.

No violations were identified during the inspection.

For data sources see[7]

References