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Difference between revisions of "37-059-26625"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-059-26625
 
| Well ID: 37-059-26625
| style="height=100%; align=center" rowspan="14" | {{#display_map: 39.847556, -80.405139 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.847556, -80.405139 | width=100% | height=100% }}
 
|-
 
|-
 
| Country: United States
 
| Country: United States
Line 17: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name: PARRY POWER LINE 1
+
| Farm/Lease Name: PARRY POWER LINE
 
|-
 
|-
| License Status: Plugged OG Well
+
| License Status: Plugged and Abandoned
 
|-
 
|-
| Spud Date: 1/1/1800
+
| Spud Date:  
 
|-
 
|-
 
| Permit Date:  
 
| Permit Date:  
 +
|-
 +
| Well Type: GAS
 
|-
 
|-
 
| Unconventional Well: N
 
| Unconventional Well: N
 
|-
 
|-
 
| Configuration: Undetermined
 
| Configuration: Undetermined
 +
|-
 +
| Conservation: No
 
|-
 
|-
 
| Latitude: 39.847556
 
| Latitude: 39.847556
Line 49: Line 53:
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | accessdate = 2019-05-21 }}</ref>
 
  | accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Date
 +
!scope="col" | Event
 +
|-
 +
| 2014-08-28
 +
| Begin Plugging
 +
|-
 +
| 2014-08-28
 +
| Finished Plugging
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Compiled from multiple data sources - see Pennsylvania Oil and Gas Data Sources
 +
| date = 2020-02-27
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-02-27 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Job Number
 +
!scope="col" | Job Start Date
 +
!scope="col" | Job End Date
 +
!scope="col" | True Vertical Depth (ft)
 +
!scope="col" | Total Water Volume (gal)
 +
!scope="col" | Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Job Number
 +
!scope="col" | Trade Name
 +
!scope="col" | Supplier
 +
!scope="col" | Purpose
 +
!scope="col" | Ingredient Name
 +
!scope="col" | CAS Number
 +
!scope="col" | Additive Percentage by Mass
 +
!scope="col" | Job Percentage by Mass
 +
!scope="col" | Mass Used (lb)
 +
|-
 +
|}-->
 +
 +
<!--== Stimulation Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Stimulation Date
 +
!scope="col" | Phase Number
 +
!scope="col" | Chemical Agent
 +
!scope="col" | Volume (gal)
 +
!scope="col" | Treating Pressure (psi)
 +
!scope="col" | Breakdown Pressure (psi)
 +
|-
 +
|}-->
 +
 
<!--== Production Data ==
 
<!--== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
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{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | Period
 
!scope="col" | Period
 +
!scope="col" | Operator
 
!scope="col" | Waste Type
 
!scope="col" | Waste Type
 
!scope="col" | Quantity
 
!scope="col" | Quantity
Line 84: Line 142:
 
| 2308625
 
| 2308625
 
| Primary Facility
 
| Primary Facility
| 08/27/2014
+
| 2014-08-27
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
Line 91: Line 149:
 
| 2320282
 
| 2320282
 
| Primary Facility
 
| Primary Facility
| 10/28/2014
+
| 2014-10-28
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
Line 98: Line 156:
 
| 2347701
 
| 2347701
 
| Primary Facility
 
| Primary Facility
| 10/28/2014
+
| 2014-10-28
 
| Compliance Evaluation
 
| Compliance Evaluation
 
| No Violations Noted
 
| No Violations Noted
Line 133: Line 191:
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | accessdate = 2019-05-21 }}</ref>
 
  | accessdate = 2019-05-21 }}</ref>
<!--== Fracking Activities ==
 
==== Fracking Jobs ====
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | Job Number
 
!scope="col" | Job Start Date
 
!scope="col" | Job End Date
 
!scope="col" | True Vertical Depth (ft)
 
!scope="col" | Total Water Volume (gal)
 
!scope="col" | Total Non-Water Volume (gal)
 
|-
 
|}-->
 
<!--==== Fluid Composition Data ====
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | Job Number
 
!scope="col" | Trade Name
 
!scope="col" | Supplier
 
!scope="col" | Purpose
 
!scope="col" | Ingredient Name
 
!scope="col" | CAS Number
 
!scope="col" | Additive Percentage by Mass
 
!scope="col" | Job Percentage by Mass
 
!scope="col" | Mass Used (lb)
 
|-
 
|}-->
 
 
 
==References==
 
==References==
 
<references/>
 
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Pennsylvania Wells]]
 
[[Category:Pennsylvania Wells]]

Latest revision as of 21:56, 14 May 2020

Well Details

Well ID: 37-059-26625
Loading map...
Country: United States
State: Pennsylvania
County: Greene
Municipality: Aleppo Township
Operator Name: PENNECO OIL CO INC
Well Pad ID:
Farm/Lease Name: PARRY POWER LINE
License Status: Plugged and Abandoned
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Undetermined
Conservation: No
Latitude: 39.847556
Longitude: -80.405139

For data sources see[1][2][3]

Well History

Date Event
2014-08-28 Begin Plugging
2014-08-28 Finished Plugging

For data sources see[4]



Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2308625 Primary Facility 2014-08-27 Plugging(Includes Plugged/Mined Through) No Violations Noted HYDROCARBON WELL SERVICES PLUGGING WELL FOR PENNECO. HAD CLEANED WELL OUT TO 1185' WITH 8-5/8 BIT. ENCOUNTERED HARD SPOT IN OPEN HOLE AT 1185'. ATTEMPTED TO DRILL AHEAD WITH NO SUCCESS. ATTAINABLE BOTTOM 1185' PUMPED CEMENT JOB WITH 20BBL RETURN TO SURFACE
2320282 Primary Facility 2014-10-28 Plugging(Includes Plugged/Mined Through) No Violations Noted PLUGGING OF WELL IS COMPLETE. OPERATOR IS WAITING TO HEAR FROM LAND OWNER TO COMPLETE MONUMENT AT SURFACE.
2347701 Primary Facility 2014-10-28 Compliance Evaluation No Violations Noted On 10/28/2014, I performed an inspection of Penneco Parry Powerline well plugging site. The site is located Aleppo Twp., Greene County. The inspection was performed as a compliance evaluation inspection related to frac out and discharge to a stream on 7/14/2014.

For data sources see[5]

References