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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 37-047-24135 | | Well ID: 37-047-24135 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 41.578450, -78.471072 | width=100% | height=100% }} |
|- | |- | ||
| Country: United States | | Country: United States | ||
Line 17: | Line 17: | ||
| Well Pad ID: [[146796]] | | Well Pad ID: [[146796]] | ||
|- | |- | ||
− | | Farm/Lease Name: COP 4V | + | | Farm/Lease Name: COP 4V |
|- | |- | ||
− | | License Status: | + | | License Status: PLUGGED & ABANDONED |
|- | |- | ||
− | | Spud Date: | + | | Spud Date: |
|- | |- | ||
| Permit Date: 2008-06-12 | | Permit Date: 2008-06-12 | ||
+ | |- | ||
+ | | Well Type: GAS | ||
|- | |- | ||
| Unconventional Well: Y | | Unconventional Well: Y | ||
|- | |- | ||
| Configuration: Vertical Well | | Configuration: Vertical Well | ||
+ | |- | ||
+ | | Conservation: Yes | ||
|- | |- | ||
| Latitude: 41.578450 | | Latitude: 41.578450 | ||
Line 49: | Line 53: | ||
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
| accessdate = 2019-05-21 }}</ref> | | accessdate = 2019-05-21 }}</ref> | ||
+ | == Well History == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Date | ||
+ | !scope="col" | Event | ||
+ | |- | ||
+ | | 2008-06-12 | ||
+ | | New Permit Application | ||
+ | |- | ||
+ | | 2008-08-21 | ||
+ | | Performed Spud Operation | ||
+ | |- | ||
+ | | 2008-08-26 | ||
+ | | Drilling Completion | ||
+ | |- | ||
+ | | 2009-05-22 | ||
+ | | Newly Drilled | ||
+ | |- | ||
+ | | 2013-08-08 | ||
+ | | Begin Plugging | ||
+ | |- | ||
+ | | 2013-08-09 | ||
+ | | Finished Plugging | ||
+ | |- | ||
+ | | 2014-05-20 | ||
+ | | Fully Plugged | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Compiled from multiple data sources - see Pennsylvania Oil and Gas Data Sources | ||
+ | | date = 2020-02-27 | ||
+ | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-02-27 }}</ref> | ||
<!--== Fracking Activities == | <!--== Fracking Activities == | ||
==== Fracking Jobs ==== | ==== Fracking Jobs ==== | ||
Line 71: | Line 107: | ||
!scope="col" | Job Percentage by Mass | !scope="col" | Job Percentage by Mass | ||
!scope="col" | Mass Used (lb) | !scope="col" | Mass Used (lb) | ||
+ | |- | ||
+ | |}--> | ||
+ | |||
+ | <!--== Stimulation Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Stimulation Date | ||
+ | !scope="col" | Phase Number | ||
+ | !scope="col" | Chemical Agent | ||
+ | !scope="col" | Volume (gal) | ||
+ | !scope="col" | Treating Pressure (psi) | ||
+ | !scope="col" | Breakdown Pressure (psi) | ||
|- | |- | ||
|}--> | |}--> | ||
Line 86: | Line 133: | ||
|- | |- | ||
| 2008 | | 2008 | ||
− | | | + | | [[EOG RESOURCES INC]] |
| style="text-align: right;" | 0.00 | | style="text-align: right;" | 0.00 | ||
| style="text-align: right;" | 0 | | style="text-align: right;" | 0 | ||
Line 95: | Line 142: | ||
|- | |- | ||
| 2009 | | 2009 | ||
− | | | + | | [[EOG RESOURCES INC]] |
| style="text-align: right;" | 0.00 | | style="text-align: right;" | 0.00 | ||
| style="text-align: right;" | 0 | | style="text-align: right;" | 0 | ||
Line 149: | Line 196: | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
!scope="col" | Period | !scope="col" | Period | ||
+ | !scope="col" | Operator | ||
!scope="col" | Waste Type | !scope="col" | Waste Type | ||
!scope="col" | Quantity | !scope="col" | Quantity | ||
Line 154: | Line 202: | ||
!scope="col" | Waste Facility ID | !scope="col" | Waste Facility ID | ||
|- | |- | ||
− | | 2013 | + | | 2013 |
− | | Drilling Fluid Waste | + | | [[EOG RESOURCES INC]] |
+ | | Drilling Fluid Waste | ||
| style="text-align: right;" | 66.65 Bbl | | style="text-align: right;" | 66.65 Bbl | ||
| LANDFILL | | LANDFILL | ||
| 301358 | | 301358 | ||
|- | |- | ||
− | | 2018 | + | | 2018 |
− | | Drilling Fluid Waste | + | | [[EOG RESOURCES INC]] |
+ | | Drilling Fluid Waste | ||
| style="text-align: right;" | 335.00 Bbl | | style="text-align: right;" | 335.00 Bbl | ||
| RESIDUAL WASTE PROCESSING FACILITY | | RESIDUAL WASTE PROCESSING FACILITY | ||
| WMGR123NW005 | | WMGR123NW005 | ||
|- | |- | ||
− | | 2018 | + | | 2018 |
− | | Drilling Fluid Waste | + | | [[EOG RESOURCES INC]] |
+ | | Drilling Fluid Waste | ||
| style="text-align: right;" | 6.77 Tons | | style="text-align: right;" | 6.77 Tons | ||
| LANDFILL | | LANDFILL |
Well ID: 37-047-24135 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Elk | |
Municipality: Jones Township | |
Operator Name: EOG RESOURCES INC | |
Well Pad ID: 146796 | |
Farm/Lease Name: COP 4V | |
License Status: PLUGGED & ABANDONED | |
Spud Date: | |
Permit Date: 2008-06-12 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Vertical Well | |
Conservation: Yes | |
Latitude: 41.578450 | |
Longitude: -78.471072 |
Date | Event |
---|---|
2008-06-12 | New Permit Application |
2008-08-21 | Performed Spud Operation |
2008-08-26 | Drilling Completion |
2009-05-22 | Newly Drilled |
2013-08-08 | Begin Plugging |
2013-08-09 | Finished Plugging |
2014-05-20 | Fully Plugged |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2008 | EOG RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2009 | EOG RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | EOG RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | EOG RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | EOG RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | EOG RESOURCES INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2013 | EOG RESOURCES INC | Drilling Fluid Waste | 66.65 Bbl | LANDFILL | 301358 |
2018 | EOG RESOURCES INC | Drilling Fluid Waste | 335.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW005 |
2018 | EOG RESOURCES INC | Drilling Fluid Waste | 6.77 Tons | LANDFILL | 101397 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1813730 | Primary Facility | 2009-07-15 | Routine/Complete Inspection | No Violations Noted | |
1902556 | Primary Facility | 2010-07-28 | Routine/Complete Inspection | No Violations Noted | |
2195982 | Primary Facility | 2013-08-09 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | |
2219513 | Primary Facility | 2013-11-07 | Administrative/File Review | No Violations Noted | |
2719747 | Primary Facility | 2018-04-18 | Routine/Complete Inspection | Violation(s) Noted | This well is plugged and leaking gas. I could see the vapors when I drove by the well. I put my gas meter in the vent and got 100% methane. |
2743433 | Primary Facility | 2018-06-20 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | This well was plugged and is being replugged due to it leaking gas. They are currently washing the pea gravel out of the well bore so they can run a camera and see if the plug is leaking. They are at 150' deep at this time. Everything is being contained in above ground pits/ tanks. |
2749666 | Primary Facility | 2018-07-09 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | This well was plugged and is being replugged due to it leaking gas. They found first plug was leaking so they drilled out that plug and gel spacer to the top of the second plug @1556'. They let the well set for 3 days and reran the camera and could not see any bubbles at that plug. They are going to cement with 125 sacks of cement up into the surface casing 50'. |
2753762 | Primary Facility | 2018-07-19 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | This well is not leaking any gas at this time. The well was replugged. I am waiting for the new plugging certificate to arrive. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2719747 | 814078 | 2018-04-18 | 2018-08-15 | 78.91(a) | Environmental Health & Safety |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
814078 | 363503 | NOV - Notice of Violation | 2018-08-15 |
For data sources see[7]