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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 37-123-25292 | | Well ID: 37-123-25292 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 41.652190, -79.001660 | width=100% | height=100% }} |
|- | |- | ||
| Country: United States | | Country: United States | ||
Line 19: | Line 19: | ||
| Farm/Lease Name: CURTIN 13 | | Farm/Lease Name: CURTIN 13 | ||
|- | |- | ||
− | | License Status: Plugged | + | | License Status: Plugged and Abandoned |
|- | |- | ||
− | | Spud Date: | + | | Spud Date: 1975-08-05 |
|- | |- | ||
| Permit Date: 1975-08-01 | | Permit Date: 1975-08-01 | ||
+ | |- | ||
+ | | Well Type: OIL | ||
|- | |- | ||
| Unconventional Well: N | | Unconventional Well: N | ||
|- | |- | ||
| Configuration: Vertical Well | | Configuration: Vertical Well | ||
+ | |- | ||
+ | | Conservation: No | ||
|- | |- | ||
| Latitude: 41.652190 | | Latitude: 41.652190 | ||
Line 49: | Line 53: | ||
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
| accessdate = 2019-05-21 }}</ref> | | accessdate = 2019-05-21 }}</ref> | ||
+ | == Well History == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Date | ||
+ | !scope="col" | Event | ||
+ | |- | ||
+ | | 1975-08-01 | ||
+ | | New Permit Application | ||
+ | |- | ||
+ | | 1975-08-09 | ||
+ | | Drilling Completion | ||
+ | |- | ||
+ | | 2013-05-06 | ||
+ | | Newly Drilled | ||
+ | |- | ||
+ | | 2018-07-25 | ||
+ | | Begin Plugging | ||
+ | |- | ||
+ | | 2018-07-30 | ||
+ | | Finished Plugging | ||
+ | |- | ||
+ | | 2018-10-25 | ||
+ | | Fully Plugged | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Compiled from multiple data sources - see Pennsylvania Oil and Gas Data Sources | ||
+ | | date = 2020-02-27 | ||
+ | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-02-27 }}</ref> | ||
<!--== Fracking Activities == | <!--== Fracking Activities == | ||
==== Fracking Jobs ==== | ==== Fracking Jobs ==== | ||
Line 71: | Line 104: | ||
!scope="col" | Job Percentage by Mass | !scope="col" | Job Percentage by Mass | ||
!scope="col" | Mass Used (lb) | !scope="col" | Mass Used (lb) | ||
+ | |- | ||
+ | |}--> | ||
+ | |||
+ | <!--== Stimulation Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Stimulation Date | ||
+ | !scope="col" | Phase Number | ||
+ | !scope="col" | Chemical Agent | ||
+ | !scope="col" | Volume (gal) | ||
+ | !scope="col" | Treating Pressure (psi) | ||
+ | !scope="col" | Breakdown Pressure (psi) | ||
|- | |- | ||
|}--> | |}--> | ||
Line 90: | Line 134: | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
!scope="col" | Period | !scope="col" | Period | ||
+ | !scope="col" | Operator | ||
!scope="col" | Waste Type | !scope="col" | Waste Type | ||
!scope="col" | Quantity | !scope="col" | Quantity |
Well ID: 37-123-25292 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Warren | |
Municipality: Sheffield Township | |
Operator Name: FE PETRO INC | |
Well Pad ID: | |
Farm/Lease Name: CURTIN 13 | |
License Status: Plugged and Abandoned | |
Spud Date: 1975-08-05 | |
Permit Date: 1975-08-01 | |
Well Type: OIL | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.652190 | |
Longitude: -79.001660 |
Date | Event |
---|---|
1975-08-01 | New Permit Application |
1975-08-09 | Drilling Completion |
2013-05-06 | Newly Drilled |
2018-07-25 | Begin Plugging |
2018-07-30 | Finished Plugging |
2018-10-25 | Fully Plugged |
For data sources see[4]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2697441 | Primary Facility | 2018-02-23 | Routine/Partial Inspection | No Violations Noted | Located well site. No well visible on location. Possibly plugged. Well record on file in DEP database. Well has become inundated with vegetation.Well is Registered to FE Petroleum in DEP database. FE is no longer in business, as described in client database. Unable to determine ownership beyond FE Petroleum. Due to the condition of well, it has been determined that abandoned status would be appropriate. |
2758597 | Primary Facility | 2018-08-01 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Drilling out bridge at 1575' at this time. Bridge was encountered at the top of the Clarendon sand. Circulated water and drill cuttings are being diverted into a lined pit. Cameron Energy is performing plugging procedures. |
2761080 | Primary Facility | 2018-08-07 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Currently drilling out shale at 1550'. As noted on well record, total depth of well bore is 1847'. Drilling has not made progress since last inspection. Drill pipe and bit are 2 7/8". Prior attempts were made using 1 1/2" pipe and bit. Smaller diameter pipe would not drill enough to lift the cuttings to surface. Well bore may have collapsed. Rig operator noted that drill bit hangs at the casing seat when entering the well. |
For data sources see[5]