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+ | __TOC__ | ||
== Well Details == | == Well Details == | ||
− | {| class="wikitable" width="95%" | + | {| class="wikitable welldetails" width="95%" |
| Well ID: 37-131-20037 | | Well ID: 37-131-20037 | ||
− | | style=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 41.639314, -75.973297 | width=100% | height=100% }} |
+ | |- | ||
+ | | Country: United States | ||
+ | |- | ||
+ | | State: Pennsylvania | ||
|- | |- | ||
− | | County: [[ | + | | County: [[Wyoming_County,_Pennsylvania|Wyoming]] |
|- | |- | ||
− | | Municipality: [[Washington Township, | + | | Municipality: [[Washington Township,_Wyoming_County,_Pennsylvania|Washington Township]] |
|- | |- | ||
− | | Operator Name: [[ | + | | Operator Name: [[CHESAPEAKE APPALACHIA LLC]] |
|- | |- | ||
| Well Pad ID: [[148860]] | | Well Pad ID: [[148860]] | ||
Line 14: | Line 19: | ||
| Farm/Lease Name: MCGRAW 2H | | Farm/Lease Name: MCGRAW 2H | ||
|- | |- | ||
− | | | + | | License Status: |
|- | |- | ||
− | | | + | | Spud Date: 2010-09-22 |
|- | |- | ||
− | | | + | | Permit Date: 2010-05-12 |
|- | |- | ||
− | | | + | | Well Type: GAS |
|- | |- | ||
− | | | + | | Unconventional Well: Y |
|- | |- | ||
− | | | + | | Configuration: Horizontal Well |
|- | |- | ||
− | | | + | | Conservation: No |
|- | |- | ||
− | | Latitude: 41. | + | | Latitude: 41.639314 |
|- | |- | ||
| Longitude: -75.973297 | | Longitude: -75.973297 | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Permits Issued Detail Report | ||
+ | |publisher = [[Pennsylvania Department of Environmental Protection]] | ||
+ | | date = 2019-05-20 | ||
+ | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref><ref>{{cite web | ||
+ | | title = Spud Data Report | ||
+ | |publisher = [[Pennsylvania Department of Environmental Protection]] | ||
+ | | date = 2019-04-30 | ||
+ | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-16 }}</ref><ref>{{cite web | ||
+ | | title = Oil and Gas Well Pad Report | ||
+ | |publisher = [[Pennsylvania Department of Environmental Protection]] | ||
+ | | date = 2019-05-20 | ||
+ | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | == Well History == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Date | ||
+ | !scope="col" | Event | ||
+ | |- | ||
+ | | 2010-05-12 | ||
+ | | New Permit Application | ||
+ | |- | ||
+ | | 2010-08-24 | ||
+ | | Performed Spud Operation | ||
+ | |- | ||
+ | | 2010-10-20 | ||
+ | | Drilling Completion | ||
+ | |- | ||
+ | | 2010-12-17 | ||
+ | | Perforation | ||
+ | |- | ||
+ | | 2010-12-17 | ||
+ | | Performed Stimulation | ||
+ | |- | ||
+ | | 2013-01-16 | ||
+ | | DEVIATED | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Compiled from multiple data sources - see Pennsylvania Oil and Gas Data Sources | ||
+ | | date = 2020-02-27 | ||
+ | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-02-27 }}</ref> | ||
+ | <!--== Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Job Number | ||
+ | !scope="col" | Job Start Date | ||
+ | !scope="col" | Job End Date | ||
+ | !scope="col" | True Vertical Depth (ft) | ||
+ | !scope="col" | Total Water Volume (gal) | ||
+ | !scope="col" | Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Job Number | ||
+ | !scope="col" | Trade Name | ||
+ | !scope="col" | Supplier | ||
+ | !scope="col" | Purpose | ||
+ | !scope="col" | Ingredient Name | ||
+ | !scope="col" | CAS Number | ||
+ | !scope="col" | Additive Percentage by Mass | ||
+ | !scope="col" | Job Percentage by Mass | ||
+ | !scope="col" | Mass Used (lb) | ||
+ | |- | ||
+ | |}--> | ||
+ | |||
+ | == Stimulation Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Stimulation Date | ||
+ | !scope="col" | Phase Number | ||
+ | !scope="col" | Chemical Agent | ||
+ | !scope="col" | Volume (gal) | ||
+ | !scope="col" | Treating Pressure (psi) | ||
+ | !scope="col" | Breakdown Pressure (psi) | ||
+ | |- | ||
+ | | 2010-12-17 | ||
+ | | style="text-align: right;" | | ||
+ | |||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Completion Reports - Stimulations | ||
+ | | publisher = Pennsylvania Department of Conservation and Natural Resources | ||
+ | | date = 2020-03-02 | ||
+ | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-03-02 }}</ref> | ||
+ | == Production Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Period | ||
+ | !scope="col" | Operator Name | ||
+ | !scope="col" | Gas Quantity (mcf) | ||
+ | !scope="col" | Gas Production Days | ||
+ | !scope="col" | Oil Quantity (bbl) | ||
+ | !scope="col" | Oil Production Days | ||
+ | !scope="col" | Water Quantity (bbl) | ||
+ | !scope="col" | Water Production Days | ||
+ | |- | ||
+ | | 2010 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2011 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2012 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | style="text-align: right;" | 827,205.00 | ||
+ | | style="text-align: right;" | 93 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2013 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | style="text-align: right;" | 3,642,592.00 | ||
+ | | style="text-align: right;" | 365 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2014 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | style="text-align: right;" | 1,738,481.00 | ||
+ | | style="text-align: right;" | 251 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2015 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | style="text-align: right;" | 1,972,310.00 | ||
+ | | style="text-align: right;" | 278 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | style="text-align: right;" | 1,256,774.00 | ||
+ | | style="text-align: right;" | 262 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2017 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | style="text-align: right;" | 1,074,208.00 | ||
+ | | style="text-align: right;" | 351 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2018 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | style="text-align: right;" | 760,584.00 | ||
+ | | style="text-align: right;" | 322 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2019 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | style="text-align: right;" | 594,375.00 | ||
+ | | style="text-align: right;" | 357 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.00 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title =Oil and Gas Production Reports | ||
+ | |publisher = [[Pennsylvania Department of Environmental Protection]] | ||
+ | | date = 2019-03-31 | ||
+ | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | == Waste Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Period | ||
+ | !scope="col" | Operator | ||
+ | !scope="col" | Waste Type | ||
+ | !scope="col" | Quantity | ||
+ | !scope="col" | Disposal Method | ||
+ | !scope="col" | Waste Facility ID | ||
+ | |- | ||
+ | | 2012 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 55.00 Bbl | ||
+ | | CENTRALIZED TREATMENT PLANT FOR RECYCLE | ||
+ | | WMGR119 | ||
+ | |- | ||
+ | | 2012 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 1,040.50 Bbl | ||
+ | | REUSE OTHER THAN ROAD SPREADING | ||
+ | | | ||
+ | |- | ||
+ | | 2013 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 782.83 Bbl | ||
+ | | REUSE OTHER THAN ROAD SPREADING | ||
+ | | | ||
+ | |- | ||
+ | | 2014 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 20.00 Bbl | ||
+ | | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | ||
+ | | WMGR123NC008 | ||
+ | |- | ||
+ | | 2014 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Drilling Fluid Waste | ||
+ | | style="text-align: right;" | 100.00 Bbl | ||
+ | | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | ||
+ | | WMGR123NC008 | ||
+ | |- | ||
+ | | 2014 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 353.04 Bbl | ||
+ | | REUSE OTHER THAN ROAD SPREADING | ||
+ | | | ||
+ | |- | ||
+ | | 2014 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Fracing Fluid Waste | ||
+ | | style="text-align: right;" | 30.00 Bbl | ||
+ | | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | ||
+ | | WMGR123NC008 | ||
+ | |- | ||
+ | | 2015 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 738.50 Bbl | ||
+ | | REUSE OTHER THAN ROAD SPREADING | ||
+ | | | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 347.50 Bbl | ||
+ | | REUSE OTHER THAN ROAD SPREADING | ||
+ | | | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Other Oil & Gas Wastes | ||
+ | | style="text-align: right;" | 25.00 Bbl | ||
+ | | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | ||
+ | | WMGR123NC010 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Other Oil & Gas Wastes | ||
+ | | style="text-align: right;" | 173.00 Bbl | ||
+ | | CENTRALIZED TREATMENT PLANT FOR RECYCLE | ||
+ | | WMGR123NW011 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Soil Contaminated by Oil | ||
+ | | style="text-align: right;" | 3.17 Tons | ||
+ | | LANDFILL | ||
+ | | 301626 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 115.00 Bbl | ||
+ | | RESIDUAL WASTE PROCESSING FACILITY | ||
+ | | WMGR123NC018 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 11.50 Bbl | ||
+ | | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | ||
+ | | WMGR123 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 159.00 Bbl | ||
+ | | RESIDUAL WASTE PROCESSING FACILITY | ||
+ | | WMGR123NW011 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 110.00 Bbl | ||
+ | | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | ||
+ | | WMGR123NC018 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 34.00 Bbl | ||
+ | | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | ||
+ | | WMGR123NC010 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 110.00 Bbl | ||
+ | | RESIDUAL WASTE PROCESSING FACILITY | ||
+ | | WMGR123NC008 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 175.00 Bbl | ||
+ | | RESIDUAL WASTE PROCESSING FACILITY | ||
+ | | WMGR123NC010 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Soil Contaminated by Oil & Gas Related Spills | ||
+ | | style="text-align: right;" | 3.17 Tons | ||
+ | | LANDFILL | ||
+ | | 301626 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Synthetic Liner Materials | ||
+ | | style="text-align: right;" | 0.45 Tons | ||
+ | | LANDFILL | ||
+ | | 8-0728-0004/013 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Other Oil & Gas Wastes | ||
+ | | style="text-align: right;" | 45.00 Bbl | ||
+ | | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | ||
+ | | WMGR123NC008 | ||
+ | |- | ||
+ | | 2017 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Synthetic Liner Materials | ||
+ | | style="text-align: right;" | 5.00 Tons | ||
+ | | CENT WASTE TRT FAC NPDES | ||
+ | | PAG034815 | ||
+ | |- | ||
+ | | 2017 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 28.00 Bbl | ||
+ | | RESIDUAL WASTE PROCESSING FACILITY | ||
+ | | WMGR123NC010 | ||
+ | |- | ||
+ | | 2017 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Other Oil & Gas Wastes | ||
+ | | style="text-align: right;" | 22.00 Bbl | ||
+ | | REUSE (AT WELL PAD) | ||
+ | | | ||
+ | |- | ||
+ | | 2017 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 115.55 Bbl | ||
+ | | RESIDUAL WASTE PROCESSING FACILITY | ||
+ | | WMGR123NW011 | ||
+ | |- | ||
+ | | 2017 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 28.00 Bbl | ||
+ | | RESIDUAL WASTE PROCESSING FACILITY | ||
+ | | WMGR123NC018 | ||
+ | |- | ||
+ | | 2017 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 66.30 Bbl | ||
+ | | REUSE (AT WELL PAD) | ||
+ | | | ||
+ | |- | ||
+ | | 2017 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 47.50 Bbl | ||
+ | | RESIDUAL WASTE PROCESSING FACILITY | ||
+ | | WMGR123NC008 | ||
+ | |- | ||
+ | | 2017 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Synthetic Liner Materials | ||
+ | | style="text-align: right;" | 5.00 Tons | ||
+ | | CENT WASTE TRT FAC NPDES DISCHARGE | ||
+ | | PAG034815 | ||
+ | |- | ||
+ | | 2018 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Synthetic Liner Materials | ||
+ | | style="text-align: right;" | 0.70 Tons | ||
+ | | LANDFILL | ||
+ | | 8-0728-0004/013 | ||
+ | |- | ||
+ | | 2018 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Other Oil & Gas Wastes | ||
+ | | style="text-align: right;" | 29.00 Bbl | ||
+ | | REUSE (AT WELL PAD) | ||
+ | | | ||
+ | |- | ||
+ | | 2018 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Synthetic Liner Materials | ||
+ | | style="text-align: right;" | 1.30 Tons | ||
+ | | CENT WASTE TRT FAC NPDES DISCHARGE | ||
+ | | PAG034815 | ||
+ | |- | ||
+ | | 2018 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 324.80 Bbl | ||
+ | | REUSE (AT WELL PAD) | ||
+ | | | ||
+ | |- | ||
+ | | 2018 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 207.60 Bbl | ||
+ | | RESIDUAL WASTE PROCESSING FACILITY | ||
+ | | WMGR123NC008 | ||
+ | |- | ||
+ | | 2018 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Waste Water Treatment Sludge | ||
+ | | style="text-align: right;" | 8.19 Tons | ||
+ | | LANDFILL | ||
+ | | 301626 | ||
+ | |- | ||
+ | | 2018 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Synthetic Liner Materials | ||
+ | | style="text-align: right;" | 1.30 Tons | ||
+ | | CENT WASTE TRT FAC NPDES | ||
+ | | PAG034815 | ||
+ | |- | ||
+ | | 2018 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Other Oil & Gas Wastes | ||
+ | | style="text-align: right;" | 48.40 Bbl | ||
+ | | RESIDUAL WASTE PROCESSING FACILITY | ||
+ | | WMGR123NC008 | ||
+ | |- | ||
+ | | 2018 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 35.40 Bbl | ||
+ | | RESIDUAL WASTE PROCESSING FACILITY | ||
+ | | WMGR123NC018 | ||
+ | |- | ||
+ | | 2019 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Other Oil & Gas Wastes | ||
+ | | style="text-align: right;" | 82.87 Bbl | ||
+ | | RESIDUAL WASTE PROCESSING FACILITY | ||
+ | | WMGR123NC008 | ||
+ | |- | ||
+ | | 2019 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Waste Water Treatment Sludge | ||
+ | | style="text-align: right;" | 2.40 Tons | ||
+ | | LANDFILL | ||
+ | | 301626 | ||
+ | |- | ||
+ | | 2019 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 540.75 Bbl | ||
+ | | RESIDUAL WASTE PROCESSING FACILITY | ||
+ | | WMGR123NC008 | ||
+ | |- | ||
+ | | 2019 | ||
+ | | [[CHESAPEAKE APPALACHIA LLC]] | ||
+ | | Produced Fluid | ||
+ | | style="text-align: right;" | 95.85 Bbl | ||
+ | | REUSE (AT WELL PAD) | ||
+ | | | ||
|- | |- | ||
|} | |} | ||
− | + | For data sources see<ref>{{cite web | |
+ | | title =Oil and Gas Waste Reports | ||
+ | |publisher = [[Pennsylvania Department of Environmental Protection]] | ||
+ | | date = 2019-03-31 | ||
+ | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
== Inspection Data == | == Inspection Data == | ||
+ | ==== Inspections Performed ==== | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" | Inspection ID |
− | !scope="col" | | + | !scope="col" | Inspection Category |
− | !scope="col" | | + | !scope="col" | Inspection Date |
− | !scope="col" | | + | !scope="col" | Inspection Type |
− | !scope="col" | | + | !scope="col" | Inspection Result |
+ | !scope="col" | Inspection Comments | ||
|- | |- | ||
| 1922616 | | 1922616 | ||
+ | | Primary Facility | ||
| 2010-10-25 | | 2010-10-25 | ||
+ | | Drilling/Alteration | ||
| No Violations Noted | | No Violations Noted | ||
| Rigging down to move to McGraw 5H | | Rigging down to move to McGraw 5H | ||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1930322 | | 1930322 | ||
+ | | Primary Facility | ||
| 2010-11-23 | | 2010-11-23 | ||
+ | | Follow-up Inspection | ||
| Violation(s) Noted | | Violation(s) Noted | ||
| Onsite visit with DEP Geologist (Eric Rooney) and DEP WQS (Ryan Klemish). Followup inpsection of possible stray gas in cellar. Lower elbow on the 2" vent line of the 13 3/8" annulus had bubbles migrating out of joint. Small intermitent bubbles seen every 10 sec. Approx 6" of water in cellar at time of inspection. Asked DEP rep to use flir camera to detect any gas that may be present as I wasn't sure if bubbling from elbow was gas migration or plumbing problem. Also, Gauge on 13 3/8 showing 0 psi, however vavle closed during time of inspection and possible loose elbow. Talked with completions supervisor Nick Pottmeyer stating they would go out and tighten up fittings, open the vavle and monitor for any pressure buildup. Also asked Mr. Pottmeyer to replace the guage on the string with one with smaller graduations to detect any gas that may be present. | | Onsite visit with DEP Geologist (Eric Rooney) and DEP WQS (Ryan Klemish). Followup inpsection of possible stray gas in cellar. Lower elbow on the 2" vent line of the 13 3/8" annulus had bubbles migrating out of joint. Small intermitent bubbles seen every 10 sec. Approx 6" of water in cellar at time of inspection. Asked DEP rep to use flir camera to detect any gas that may be present as I wasn't sure if bubbling from elbow was gas migration or plumbing problem. Also, Gauge on 13 3/8 showing 0 psi, however vavle closed during time of inspection and possible loose elbow. Talked with completions supervisor Nick Pottmeyer stating they would go out and tighten up fittings, open the vavle and monitor for any pressure buildup. Also asked Mr. Pottmeyer to replace the guage on the string with one with smaller graduations to detect any gas that may be present. | ||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1931929 | | 1931929 | ||
+ | | Primary Facility | ||
| 2010-11-30 | | 2010-11-30 | ||
+ | | Follow-up Inspection | ||
| Violation(s) Noted | | Violation(s) Noted | ||
| Follow-up of loose elbow on 2" vent line of 13 3/8". Water drained from cellar. Gauges were replaced with those of smaller graduations on casing strings. 300PSI on production string. | | Follow-up of loose elbow on 2" vent line of 13 3/8". Water drained from cellar. Gauges were replaced with those of smaller graduations on casing strings. 300PSI on production string. | ||
− | |||
− | |||
|- | |- | ||
| 1931939 | | 1931939 | ||
+ | | Primary Facility | ||
| 2010-12-03 | | 2010-12-03 | ||
+ | | Follow-up Inspection | ||
| Violation(s) Noted | | Violation(s) Noted | ||
| All valves were open and that there was no pressure on any of the gauges (including the production string). I also noted that there was a brass vented nipple installed on the 2" vent line that appeared to be on the outside of the 13 3/8" annulus. | | All valves were open and that there was no pressure on any of the gauges (including the production string). I also noted that there was a brass vented nipple installed on the 2" vent line that appeared to be on the outside of the 13 3/8" annulus. | ||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1939058 | | 1939058 | ||
+ | | Primary Facility | ||
| 2010-12-22 | | 2010-12-22 | ||
+ | | Routine/Complete Inspection | ||
| No Violations Noted | | No Violations Noted | ||
| Reading at wellhead measured 50% methane on vent of 13 3/8". During time of inspection noted that pressure guages were removed from the wellhead. | | Reading at wellhead measured 50% methane on vent of 13 3/8". During time of inspection noted that pressure guages were removed from the wellhead. | ||
− | |||
− | |||
|- | |- | ||
| 1944427 | | 1944427 | ||
+ | | Primary Facility | ||
| 2011-01-04 | | 2011-01-04 | ||
+ | | Drilling/Alteration | ||
| No Violations Noted | | No Violations Noted | ||
| Preparing location for fract ops | | Preparing location for fract ops | ||
− | |||
− | |||
|- | |- | ||
| 1950451 | | 1950451 | ||
+ | | Primary Facility | ||
| 2011-02-16 | | 2011-02-16 | ||
+ | | Drilling/Alteration | ||
| No Violations Noted | | No Violations Noted | ||
| | | | ||
− | |||
− | |||
|- | |- | ||
| 1955249 | | 1955249 | ||
+ | | Primary Facility | ||
| 2011-01-24 | | 2011-01-24 | ||
+ | | Follow-up Inspection | ||
| No Violations Noted | | No Violations Noted | ||
| Checked well. Head being heated. No activity. 13 3/8" being vented. | | Checked well. Head being heated. No activity. 13 3/8" being vented. | ||
− | |||
− | |||
|- | |- | ||
| 1966044 | | 1966044 | ||
+ | | Primary Facility | ||
| 2011-04-07 | | 2011-04-07 | ||
+ | | Routine/Complete Inspection | ||
| No Violations Noted | | No Violations Noted | ||
| Laying down mats and liner to prepare for spudding of 5H | | Laying down mats and liner to prepare for spudding of 5H | ||
− | |||
− | |||
|- | |- | ||
| 1985334 | | 1985334 | ||
+ | | Primary Facility | ||
| 2011-06-30 | | 2011-06-30 | ||
+ | | Routine/Complete Inspection | ||
| No Violations Noted | | No Violations Noted | ||
| 200# gauge on surface. 0 psi. Contacted Nick Pottmeyer requesting smaller gauge (50#) on surface casing string. | | 200# gauge on surface. 0 psi. Contacted Nick Pottmeyer requesting smaller gauge (50#) on surface casing string. | ||
− | |||
− | |||
|- | |- | ||
| 1987623 | | 1987623 | ||
+ | | Primary Facility | ||
| 2011-07-13 | | 2011-07-13 | ||
+ | | Routine/Complete Inspection | ||
| No Violations Noted | | No Violations Noted | ||
| 13 3/8 gauges replaced wth 50# as requested. All other gauges 100# | | 13 3/8 gauges replaced wth 50# as requested. All other gauges 100# | ||
− | |||
− | |||
|- | |- | ||
| 2004017 | | 2004017 | ||
+ | | Primary Facility | ||
| 2011-09-19 | | 2011-09-19 | ||
+ | | Routine/Complete Inspection | ||
| No Violations Noted | | No Violations Noted | ||
| | | | ||
− | |||
− | |||
|- | |- | ||
| 2062439 | | 2062439 | ||
+ | | Primary Facility | ||
| 2012-03-15 | | 2012-03-15 | ||
+ | | Routine/Complete Inspection | ||
| No Violations Noted | | No Violations Noted | ||
| cellar is dug out, no water. 9 5/8" X 13 3/8" annulus vented. Checked with gas meter, no gas. | | cellar is dug out, no water. 9 5/8" X 13 3/8" annulus vented. Checked with gas meter, no gas. | ||
− | |||
− | |||
|- | |- | ||
| 2120690 | | 2120690 | ||
+ | | Primary Facility | ||
| 2012-09-13 | | 2012-09-13 | ||
+ | | Routine/Complete Inspection | ||
| No Violations Noted | | No Violations Noted | ||
| Well fract. 2 seperators, 2 tanks. 8 Brine water tanks, 11 fresh water tanks on location | | Well fract. 2 seperators, 2 tanks. 8 Brine water tanks, 11 fresh water tanks on location | ||
− | |||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 2133552 | | 2133552 | ||
+ | | Primary Facility | ||
| 2013-01-15 | | 2013-01-15 | ||
+ | | Routine/Complete Inspection | ||
| No Violations Noted | | No Violations Noted | ||
| Producing well. No water in cellar. | | Producing well. No water in cellar. | ||
− | + | |- | |
− | + | | 2248241 | |
− | + | | Primary Facility | |
− | + | | 2014-02-25 | |
− | + | | Routine/Complete Inspection | |
+ | | No Violations Noted | ||
+ | | Producing well. Cellar empty w/ a little snow. | ||
+ | |- | ||
+ | | 2337920 | ||
+ | | Primary Facility | ||
+ | | 2015-01-20 | ||
+ | | Follow-up Inspection | ||
+ | | No Violations Noted | ||
| | | | ||
|- | |- | ||
− | | | + | | 2348623 |
− | + | | Primary Facility | |
− | + | | 2015-02-18 | |
− | + | | Follow-up Inspection | |
− | + | | No Violations Noted | |
− | + | | Chesapeake was in the process of breaking down secondary containment and washing rig mats. I recorded a conductivity reading of (3.59) milliSiemens/cm in water on containment on the western side of the pad near the cut slope. A vacuum truck operator was in the process of removing water on containment nearby area where the elevated conductivity was recorded. I pointed out to him the where the water with the elevated conductivity was. He claimed he would remove all of the water on containment. I recorded (3.62) milliSiemens/cm conductivity in water on the pad surface next to a heating unit and frac tank used to contain water to wash the rig mats. Mr. Wilkes informed that the water with the elevated conductivity readings off containment will be removed via and on-site vacuum truck. | |
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
− | | | + | | 2349427 |
− | | | + | | Primary Facility |
− | | | + | | 2015-02-26 |
− | | | + | | Follow-up Inspection |
− | | | + | | No Violations Noted |
− | + | | Chesapeake was in the process of breaking down secondary containment, washing rig mats and removing snow and ice on containment. Mr. Krut informed me of a crack in the poly urea encompassing the perimeter of the 1H wellhead. The wellheads are contained with a cement apron. The cement below the poly urea on the 1H well is not compromised according to Mr. Krut. Due to the crack in the poly urea, Leidos Engineering performed soil conductivity screening on the pad surface around the perimeter of the cement apron on 2/25/15. Mr. Krut indicated that Leidos collected a total of (6) EC screenings/. The highest reading was (628) microSiemens/cm. Background soil conductivity readings, which were collected in the Northeast corner of the Pad, were (301) microSiemens/cm according to Mr. Krut. The Department did not observe staining/visibly impacted soils on the pad surface near the cement apron; N 41°38’22”; W-75°58’24”. | |
− | |||
|- | |- | ||
+ | | 2349574 | ||
+ | | Primary Facility | ||
+ | | 2015-03-05 | ||
+ | | Administrative/File Review | ||
+ | | No Violations Noted | ||
+ | | This administrative inspection has been created to document Chesapeake’s discovery of soil conductivity screening readings above background levels on 2/26/15. On 3/2/15, Nick Krut, Environmental Representative of Chesapeake submitted an Electrical Conductivity Screening Summary Map for the McGraw Wyo Pad. Leidos Engineering performed soil conductivity screening at the site on 2/26/15. Due to soil conductivity readings elevated above background levels, the Department requested Chesapeake collect a sample in the area that exhibited the conductivity reading of (637) microSiemens/cm to verify the presence or absence of potentially impacted pad surface material. The Department requested the sample be analyzed for flowback/production fluid parameters. Chesapeake has agreed to collect a sample based on the Department’s request. | ||
|- | |- | ||
− | | | + | | 2349622 |
− | | | + | | Primary Facility |
− | | | + | | 2015-03-06 |
− | | | + | | Follow-up Inspection |
− | | | + | | No Violations Noted |
− | + | | Chesapeake was in the process of attempting to return the McGraw 2H and McGraw 5H wells into production. Mr. Krut contacted me on 3-5-15 regarding the removal of all of the secondary containment used for hydraulic fracturing operations. The containment was completely removed from the site on 3-4-15. It has taken several weeks to remove the containment from the site due to the weather, according to Mr. Krut. The department did not observe any signs of contamination of the pad surface where the containment was staged. The majority of the pad surface was snow covered from the most recent snowfall event. | |
− | |||
|- | |- | ||
+ | | 2359214 | ||
+ | | Primary Facility | ||
+ | | 2015-04-08 | ||
+ | | Administrative/File Review | ||
+ | | No Violations Noted | ||
+ | | This administrative inspection has been created to document Chesapeake’s submittal of a report to the Department on 4/2/15 containing a datatable and sample results of a sample collected by Chesapeake’s contractor, Leidos Engineering at the McGraw well Pad on 3/11/15 in response to the release of approximately (750) barrels of proppant laden fluid on containment on January 19, 2015, and elevated field electrical conductivity (EC) screenings, conducted by Leidos, on February 25, 2015 documented in the McGraw 3/5/15 inspection report. The Department has concluded that there are no technical deficiencies in the report containing the data table and sampling results and no further action is warranted at this time at the McGraw well pad in the area where the proppant laden fluid was released to containment and the field electrical conductivity screening readings were detected at levels slightly above background. | ||
|- | |- | ||
− | | | + | | 2472337 |
− | | | + | | Primary Facility |
− | | | + | | 2016-04-07 |
− | + | | Routine/Complete Inspection | |
− | | | + | | No Violations Noted |
− | | | + | | |
− | | | ||
|- | |- | ||
+ | | 2478660 | ||
+ | | Primary Facility | ||
+ | | 2016-04-25 | ||
+ | | Routine/Complete Inspection | ||
+ | | No Violations Noted | ||
+ | | | ||
|- | |- | ||
− | | | + | | 2692769 |
− | | | + | | Primary Facility |
− | | | + | | 2018-02-01 |
− | | | + | | Routine/Partial Inspection |
− | | | + | | No Violations Noted |
− | + | | Onsite in follow-up to citizens report of activity occurring on pad. Upon arrival: Weather: Clear, cold, ~20 degs. (5) wells are present on this pad. The 1H, 2H, 3H & 5H were Producing. The 4H well head was being prepped for Stimulation. Weir Energy hands were onsite replacing the production tree of 4H with a 10K master valve. I spoke with CALLC's Completions WSS, Brian Heffron onsite. Mr. Heffron mentioned that the (4) producing wells would remain in production until the the Completions equipment was being mobilized to pad, which he thought would be several weeks. Access was limited to well area due to work being performed on pad. No obvious concerns or violations were noted at time of inspection. | |
− | |||
|- | |- | ||
+ | | 2708814 | ||
+ | | Primary Facility | ||
+ | | 2018-03-22 | ||
+ | | Routine/Complete Inspection | ||
+ | | No Violations Noted | ||
+ | | Hydraulic fracturing operations have recently concluded CHK Personnel were prepping the well (4H) for production. No violations were noted. If you have any questions, please contact me. | ||
|- | |- | ||
− | | | + | |} |
− | | | + | ==== Violations Commited ==== |
− | | | + | {| class="wikitable sortable" width="95%" |
− | + | !scope="col" | Inspection ID | |
− | + | !scope="col" | Violation ID | |
− | + | !scope="col" | Violation Date | |
− | + | !scope="col" | Date Resolved | |
+ | !scope="col" | Violation Code | ||
+ | !scope="col" | Violation Type | ||
+ | !scope="col" | Violation Comments | ||
|- | |- | ||
+ | | 1930322 | ||
+ | | 601700 | ||
+ | | 11/23/2010 | ||
+ | | 2010-11-23 | ||
+ | | 207B - Failure to case and cement to prevent migrations into fresh groundwater | ||
+ | | Environmental Health & Safety | ||
+ | | 78.81(a)(2)&(3) | ||
|- | |- | ||
− | | | + | | 1930322 |
− | | | + | | 601701 |
− | | | + | | 11/23/2010 |
− | | | + | | 2010-11-23 |
− | + | | 78.86* - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days | |
− | | | + | | Administrative |
− | | | + | | |
|- | |- | ||
− | | | + | | 1931929 |
− | + | | 600760 | |
− | + | | 11/30/2010 | |
− | + | | 2010-11-30 | |
− | + | | 207B - Failure to case and cement to prevent migrations into fresh groundwater | |
− | + | | Environmental Health & Safety | |
− | + | | 78.81(a)(2)&(3) | |
− | |||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
− | | | + | | 1931929 |
− | | | + | | 600761 |
− | | | + | | 11/30/2010 |
− | | | + | | 2010-11-30 |
− | | | + | | 78.86* - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days |
− | + | | Administrative | |
− | + | | | |
− | | | ||
− | | | ||
|- | |- | ||
+ | | 1931939 | ||
+ | | 600762 | ||
+ | | 12/03/2010 | ||
+ | | 2010-12-03 | ||
+ | | 207B - Failure to case and cement to prevent migrations into fresh groundwater | ||
+ | | Environmental Health & Safety | ||
+ | | 78.81(a)(2)&(3) | ||
|- | |- | ||
− | | | + | | 1931939 |
− | | | + | | 600763 |
− | | | + | | 12/03/2010 |
− | + | | 2010-12-03 | |
− | | | + | | 78.86* - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days |
+ | | Administrative | ||
| | | | ||
− | | | + | |- |
+ | |} | ||
+ | ==== Penalties Applied ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" | Violation ID | ||
+ | !scope="col" | Penalty ID | ||
+ | !scope="col" | Penalty Code | ||
+ | !scope="col" | Penalty Status | ||
+ | !scope="col" | Penalty Date | ||
+ | !scope="col" | Enforcement Date | ||
+ | !scope="col" | Penalty Amount | ||
+ | !scope="col" | Amount Collected | ||
+ | |- | ||
+ | | 601700 | ||
+ | | 266243 | ||
+ | | NOV - Notice of Violation | ||
+ | | Comply/Closed | ||
| | | | ||
+ | | 2013-01-25 | ||
+ | | style="text-align: right;" | | ||
+ | | style="text-align: right;" | | ||
+ | |- | ||
+ | | 601701 | ||
+ | | 266243 | ||
+ | | NOV - Notice of Violation | ||
+ | | Comply/Closed | ||
| | | | ||
+ | | 2013-01-25 | ||
+ | | style="text-align: right;" | | ||
+ | | style="text-align: right;" | | ||
|- | |- | ||
+ | | 600760 | ||
+ | | 266243 | ||
+ | | NOV - Notice of Violation | ||
+ | | Comply/Closed | ||
+ | | | ||
+ | | 2013-01-25 | ||
+ | | style="text-align: right;" | | ||
+ | | style="text-align: right;" | | ||
|- | |- | ||
− | | | + | | 600761 |
− | | | + | | 266243 |
− | | | + | | NOV - Notice of Violation |
− | + | | Comply/Closed | |
− | | | ||
| | | | ||
− | | | + | | 2013-01-25 |
+ | | style="text-align: right;" | | ||
+ | | style="text-align: right;" | | ||
+ | |- | ||
+ | | 600762 | ||
+ | | 266243 | ||
+ | | NOV - Notice of Violation | ||
+ | | Comply/Closed | ||
| | | | ||
+ | | 2013-01-25 | ||
+ | | style="text-align: right;" | | ||
+ | | style="text-align: right;" | | ||
+ | |- | ||
+ | | 600763 | ||
+ | | 266243 | ||
+ | | NOV - Notice of Violation | ||
+ | | Comply/Closed | ||
| | | | ||
+ | | 2013-01-25 | ||
+ | | style="text-align: right;" | | ||
+ | | style="text-align: right;" | | ||
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title =Oil and Gas Compliance Report | ||
+ | |publisher = [[Pennsylvania Department of Environmental Protection]] | ||
+ | | date = 2019-05-20 | ||
+ | | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
==References== | ==References== | ||
− | + | <references/> | |
− | |||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
+ | [[Category:Pennsylvania Wells]] |
Well ID: 37-131-20037 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Wyoming | |
Municipality: Washington Township | |
Operator Name: CHESAPEAKE APPALACHIA LLC | |
Well Pad ID: 148860 | |
Farm/Lease Name: MCGRAW 2H | |
License Status: | |
Spud Date: 2010-09-22 | |
Permit Date: 2010-05-12 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Conservation: No | |
Latitude: 41.639314 | |
Longitude: -75.973297 |
Date | Event |
---|---|
2010-05-12 | New Permit Application |
2010-08-24 | Performed Spud Operation |
2010-10-20 | Drilling Completion |
2010-12-17 | Perforation |
2010-12-17 | Performed Stimulation |
2013-01-16 | DEVIATED |
For data sources see[4]
Stimulation Date | Phase Number | Chemical Agent | Volume (gal) | Treating Pressure (psi) | Breakdown Pressure (psi) |
---|---|---|---|---|---|
2010-12-17 | 0 | 0 | 0 |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2010 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | CHESAPEAKE APPALACHIA LLC | 827,205.00 | 93 | 0.00 | 0 | 0.00 | 0 |
2013 | CHESAPEAKE APPALACHIA LLC | 3,642,592.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | CHESAPEAKE APPALACHIA LLC | 1,738,481.00 | 251 | 0.00 | 0 | 0.00 | 0 |
2015 | CHESAPEAKE APPALACHIA LLC | 1,972,310.00 | 278 | 0.00 | 0 | 0.00 | 0 |
2016 | CHESAPEAKE APPALACHIA LLC | 1,256,774.00 | 262 | 0.00 | 0 | 0.00 | 0 |
2017 | CHESAPEAKE APPALACHIA LLC | 1,074,208.00 | 351 | 0.00 | 0 | 0.00 | 0 |
2018 | CHESAPEAKE APPALACHIA LLC | 760,584.00 | 322 | 0.00 | 0 | 0.00 | 0 |
2019 | CHESAPEAKE APPALACHIA LLC | 594,375.00 | 357 | 0.00 | 0 | 0.00 | 0 |
For data sources see[6]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2012 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 55.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR119 |
2012 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 1,040.50 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2013 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 782.83 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2014 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 20.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC008 |
2014 | CHESAPEAKE APPALACHIA LLC | Drilling Fluid Waste | 100.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC008 |
2014 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 353.04 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2014 | CHESAPEAKE APPALACHIA LLC | Fracing Fluid Waste | 30.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC008 |
2015 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 738.50 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2016 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 347.50 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2016 | CHESAPEAKE APPALACHIA LLC | Other Oil & Gas Wastes | 25.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC010 |
2016 | CHESAPEAKE APPALACHIA LLC | Other Oil & Gas Wastes | 173.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123NW011 |
2016 | CHESAPEAKE APPALACHIA LLC | Soil Contaminated by Oil | 3.17 Tons | LANDFILL | 301626 |
2016 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 115.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC018 |
2016 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 11.50 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123 |
2016 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 159.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW011 |
2016 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 110.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC018 |
2016 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 34.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC010 |
2016 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 110.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC008 |
2016 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 175.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2016 | CHESAPEAKE APPALACHIA LLC | Soil Contaminated by Oil & Gas Related Spills | 3.17 Tons | LANDFILL | 301626 |
2016 | CHESAPEAKE APPALACHIA LLC | Synthetic Liner Materials | 0.45 Tons | LANDFILL | 8-0728-0004/013 |
2016 | CHESAPEAKE APPALACHIA LLC | Other Oil & Gas Wastes | 45.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC008 |
2017 | CHESAPEAKE APPALACHIA LLC | Synthetic Liner Materials | 5.00 Tons | CENT WASTE TRT FAC NPDES | PAG034815 |
2017 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 28.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2017 | CHESAPEAKE APPALACHIA LLC | Other Oil & Gas Wastes | 22.00 Bbl | REUSE (AT WELL PAD) | |
2017 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 115.55 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW011 |
2017 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 28.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC018 |
2017 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 66.30 Bbl | REUSE (AT WELL PAD) | |
2017 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 47.50 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC008 |
2017 | CHESAPEAKE APPALACHIA LLC | Synthetic Liner Materials | 5.00 Tons | CENT WASTE TRT FAC NPDES DISCHARGE | PAG034815 |
2018 | CHESAPEAKE APPALACHIA LLC | Synthetic Liner Materials | 0.70 Tons | LANDFILL | 8-0728-0004/013 |
2018 | CHESAPEAKE APPALACHIA LLC | Other Oil & Gas Wastes | 29.00 Bbl | REUSE (AT WELL PAD) | |
2018 | CHESAPEAKE APPALACHIA LLC | Synthetic Liner Materials | 1.30 Tons | CENT WASTE TRT FAC NPDES DISCHARGE | PAG034815 |
2018 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 324.80 Bbl | REUSE (AT WELL PAD) | |
2018 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 207.60 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC008 |
2018 | CHESAPEAKE APPALACHIA LLC | Waste Water Treatment Sludge | 8.19 Tons | LANDFILL | 301626 |
2018 | CHESAPEAKE APPALACHIA LLC | Synthetic Liner Materials | 1.30 Tons | CENT WASTE TRT FAC NPDES | PAG034815 |
2018 | CHESAPEAKE APPALACHIA LLC | Other Oil & Gas Wastes | 48.40 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC008 |
2018 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 35.40 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC018 |
2019 | CHESAPEAKE APPALACHIA LLC | Other Oil & Gas Wastes | 82.87 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC008 |
2019 | CHESAPEAKE APPALACHIA LLC | Waste Water Treatment Sludge | 2.40 Tons | LANDFILL | 301626 |
2019 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 540.75 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC008 |
2019 | CHESAPEAKE APPALACHIA LLC | Produced Fluid | 95.85 Bbl | REUSE (AT WELL PAD) |
For data sources see[7]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1922616 | Primary Facility | 2010-10-25 | Drilling/Alteration | No Violations Noted | Rigging down to move to McGraw 5H |
1930322 | Primary Facility | 2010-11-23 | Follow-up Inspection | Violation(s) Noted | Onsite visit with DEP Geologist (Eric Rooney) and DEP WQS (Ryan Klemish). Followup inpsection of possible stray gas in cellar. Lower elbow on the 2" vent line of the 13 3/8" annulus had bubbles migrating out of joint. Small intermitent bubbles seen every 10 sec. Approx 6" of water in cellar at time of inspection. Asked DEP rep to use flir camera to detect any gas that may be present as I wasn't sure if bubbling from elbow was gas migration or plumbing problem. Also, Gauge on 13 3/8 showing 0 psi, however vavle closed during time of inspection and possible loose elbow. Talked with completions supervisor Nick Pottmeyer stating they would go out and tighten up fittings, open the vavle and monitor for any pressure buildup. Also asked Mr. Pottmeyer to replace the guage on the string with one with smaller graduations to detect any gas that may be present. |
1931929 | Primary Facility | 2010-11-30 | Follow-up Inspection | Violation(s) Noted | Follow-up of loose elbow on 2" vent line of 13 3/8". Water drained from cellar. Gauges were replaced with those of smaller graduations on casing strings. 300PSI on production string. |
1931939 | Primary Facility | 2010-12-03 | Follow-up Inspection | Violation(s) Noted | All valves were open and that there was no pressure on any of the gauges (including the production string). I also noted that there was a brass vented nipple installed on the 2" vent line that appeared to be on the outside of the 13 3/8" annulus. |
1939058 | Primary Facility | 2010-12-22 | Routine/Complete Inspection | No Violations Noted | Reading at wellhead measured 50% methane on vent of 13 3/8". During time of inspection noted that pressure guages were removed from the wellhead. |
1944427 | Primary Facility | 2011-01-04 | Drilling/Alteration | No Violations Noted | Preparing location for fract ops |
1950451 | Primary Facility | 2011-02-16 | Drilling/Alteration | No Violations Noted | |
1955249 | Primary Facility | 2011-01-24 | Follow-up Inspection | No Violations Noted | Checked well. Head being heated. No activity. 13 3/8" being vented. |
1966044 | Primary Facility | 2011-04-07 | Routine/Complete Inspection | No Violations Noted | Laying down mats and liner to prepare for spudding of 5H |
1985334 | Primary Facility | 2011-06-30 | Routine/Complete Inspection | No Violations Noted | 200# gauge on surface. 0 psi. Contacted Nick Pottmeyer requesting smaller gauge (50#) on surface casing string. |
1987623 | Primary Facility | 2011-07-13 | Routine/Complete Inspection | No Violations Noted | 13 3/8 gauges replaced wth 50# as requested. All other gauges 100# |
2004017 | Primary Facility | 2011-09-19 | Routine/Complete Inspection | No Violations Noted | |
2062439 | Primary Facility | 2012-03-15 | Routine/Complete Inspection | No Violations Noted | cellar is dug out, no water. 9 5/8" X 13 3/8" annulus vented. Checked with gas meter, no gas. |
2120690 | Primary Facility | 2012-09-13 | Routine/Complete Inspection | No Violations Noted | Well fract. 2 seperators, 2 tanks. 8 Brine water tanks, 11 fresh water tanks on location |
2133552 | Primary Facility | 2013-01-15 | Routine/Complete Inspection | No Violations Noted | Producing well. No water in cellar. |
2248241 | Primary Facility | 2014-02-25 | Routine/Complete Inspection | No Violations Noted | Producing well. Cellar empty w/ a little snow. |
2337920 | Primary Facility | 2015-01-20 | Follow-up Inspection | No Violations Noted | |
2348623 | Primary Facility | 2015-02-18 | Follow-up Inspection | No Violations Noted | Chesapeake was in the process of breaking down secondary containment and washing rig mats. I recorded a conductivity reading of (3.59) milliSiemens/cm in water on containment on the western side of the pad near the cut slope. A vacuum truck operator was in the process of removing water on containment nearby area where the elevated conductivity was recorded. I pointed out to him the where the water with the elevated conductivity was. He claimed he would remove all of the water on containment. I recorded (3.62) milliSiemens/cm conductivity in water on the pad surface next to a heating unit and frac tank used to contain water to wash the rig mats. Mr. Wilkes informed that the water with the elevated conductivity readings off containment will be removed via and on-site vacuum truck. |
2349427 | Primary Facility | 2015-02-26 | Follow-up Inspection | No Violations Noted | Chesapeake was in the process of breaking down secondary containment, washing rig mats and removing snow and ice on containment. Mr. Krut informed me of a crack in the poly urea encompassing the perimeter of the 1H wellhead. The wellheads are contained with a cement apron. The cement below the poly urea on the 1H well is not compromised according to Mr. Krut. Due to the crack in the poly urea, Leidos Engineering performed soil conductivity screening on the pad surface around the perimeter of the cement apron on 2/25/15. Mr. Krut indicated that Leidos collected a total of (6) EC screenings/. The highest reading was (628) microSiemens/cm. Background soil conductivity readings, which were collected in the Northeast corner of the Pad, were (301) microSiemens/cm according to Mr. Krut. The Department did not observe staining/visibly impacted soils on the pad surface near the cement apron; N 41°38’22”; W-75°58’24”. |
2349574 | Primary Facility | 2015-03-05 | Administrative/File Review | No Violations Noted | This administrative inspection has been created to document Chesapeake’s discovery of soil conductivity screening readings above background levels on 2/26/15. On 3/2/15, Nick Krut, Environmental Representative of Chesapeake submitted an Electrical Conductivity Screening Summary Map for the McGraw Wyo Pad. Leidos Engineering performed soil conductivity screening at the site on 2/26/15. Due to soil conductivity readings elevated above background levels, the Department requested Chesapeake collect a sample in the area that exhibited the conductivity reading of (637) microSiemens/cm to verify the presence or absence of potentially impacted pad surface material. The Department requested the sample be analyzed for flowback/production fluid parameters. Chesapeake has agreed to collect a sample based on the Department’s request. |
2349622 | Primary Facility | 2015-03-06 | Follow-up Inspection | No Violations Noted | Chesapeake was in the process of attempting to return the McGraw 2H and McGraw 5H wells into production. Mr. Krut contacted me on 3-5-15 regarding the removal of all of the secondary containment used for hydraulic fracturing operations. The containment was completely removed from the site on 3-4-15. It has taken several weeks to remove the containment from the site due to the weather, according to Mr. Krut. The department did not observe any signs of contamination of the pad surface where the containment was staged. The majority of the pad surface was snow covered from the most recent snowfall event. |
2359214 | Primary Facility | 2015-04-08 | Administrative/File Review | No Violations Noted | This administrative inspection has been created to document Chesapeake’s submittal of a report to the Department on 4/2/15 containing a datatable and sample results of a sample collected by Chesapeake’s contractor, Leidos Engineering at the McGraw well Pad on 3/11/15 in response to the release of approximately (750) barrels of proppant laden fluid on containment on January 19, 2015, and elevated field electrical conductivity (EC) screenings, conducted by Leidos, on February 25, 2015 documented in the McGraw 3/5/15 inspection report. The Department has concluded that there are no technical deficiencies in the report containing the data table and sampling results and no further action is warranted at this time at the McGraw well pad in the area where the proppant laden fluid was released to containment and the field electrical conductivity screening readings were detected at levels slightly above background. |
2472337 | Primary Facility | 2016-04-07 | Routine/Complete Inspection | No Violations Noted | |
2478660 | Primary Facility | 2016-04-25 | Routine/Complete Inspection | No Violations Noted | |
2692769 | Primary Facility | 2018-02-01 | Routine/Partial Inspection | No Violations Noted | Onsite in follow-up to citizens report of activity occurring on pad. Upon arrival: Weather: Clear, cold, ~20 degs. (5) wells are present on this pad. The 1H, 2H, 3H & 5H were Producing. The 4H well head was being prepped for Stimulation. Weir Energy hands were onsite replacing the production tree of 4H with a 10K master valve. I spoke with CALLC's Completions WSS, Brian Heffron onsite. Mr. Heffron mentioned that the (4) producing wells would remain in production until the the Completions equipment was being mobilized to pad, which he thought would be several weeks. Access was limited to well area due to work being performed on pad. No obvious concerns or violations were noted at time of inspection. |
2708814 | Primary Facility | 2018-03-22 | Routine/Complete Inspection | No Violations Noted | Hydraulic fracturing operations have recently concluded CHK Personnel were prepping the well (4H) for production. No violations were noted. If you have any questions, please contact me. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
1930322 | 601700 | 11/23/2010 | 2010-11-23 | 207B - Failure to case and cement to prevent migrations into fresh groundwater | Environmental Health & Safety | 78.81(a)(2)&(3) |
1930322 | 601701 | 11/23/2010 | 2010-11-23 | 78.86* - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days | Administrative | |
1931929 | 600760 | 11/30/2010 | 2010-11-30 | 207B - Failure to case and cement to prevent migrations into fresh groundwater | Environmental Health & Safety | 78.81(a)(2)&(3) |
1931929 | 600761 | 11/30/2010 | 2010-11-30 | 78.86* - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days | Administrative | |
1931939 | 600762 | 12/03/2010 | 2010-12-03 | 207B - Failure to case and cement to prevent migrations into fresh groundwater | Environmental Health & Safety | 78.81(a)(2)&(3) |
1931939 | 600763 | 12/03/2010 | 2010-12-03 | 78.86* - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days | Administrative |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
601700 | 266243 | NOV - Notice of Violation | Comply/Closed | 2013-01-25 | |||
601701 | 266243 | NOV - Notice of Violation | Comply/Closed | 2013-01-25 | |||
600760 | 266243 | NOV - Notice of Violation | Comply/Closed | 2013-01-25 | |||
600761 | 266243 | NOV - Notice of Violation | Comply/Closed | 2013-01-25 | |||
600762 | 266243 | NOV - Notice of Violation | Comply/Closed | 2013-01-25 | |||
600763 | 266243 | NOV - Notice of Violation | Comply/Closed | 2013-01-25 |
For data sources see[8]