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Difference between revisions of "37-049-24158"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-049-24158
 
| Well ID: 37-049-24158
| style="height=100%; align=center" rowspan="14" | {{#display_map: 42.01985, -79.949912 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 42.019851, -79.949912 | width=100% | height=100% }}
 
|-
 
|-
| Operator Name: [[MITCH WELL ENERGY INC]]
+
| Country: United States
 
|-
 
|-
| First Permit Date: 1984-09-13
+
| State: Pennsylvania
 
|-
 
|-
| Last Permit Date: 1984-09-13
+
| County: [[Erie_County,_Pennsylvania|Erie]]
 
|-
 
|-
| Spud Date: 1800-01-01
+
| Municipality: [[Greene Township,_Erie_County,_Pennsylvania|Greene Township]]
 
|-
 
|-
| Unconventional: No
+
| Operator Name:  
 
|-
 
|-
| Horizontal: No
+
| Well Pad ID:  
 
|-
 
|-
| Violations: 1
+
| Farm/Lease Name: WEISER 1
 
|-
 
|-
| Latitude: 42.01985
+
| License Status:
 +
|-
 +
| Spud Date:
 +
|-
 +
| Permit Date: 1984-09-13
 +
|-
 +
| Well Type: GAS
 +
|-
 +
| Unconventional Well: N
 +
|-
 +
| Configuration: Vertical Well
 +
|-
 +
| Conservation: Yes
 +
|-
 +
| Latitude: 42.019851
 
|-
 
|-
 
| Longitude: -79.949912
 
| Longitude: -79.949912
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Permits Issued Detail Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-05-20
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref><ref>{{cite web
 +
| title = Spud Data Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-04-30
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-16 }}</ref><ref>{{cite web
 +
| title = Oil and Gas Well Pad Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-05-20
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Date
 +
!scope="col" | Event
 +
|-
 +
| 1984-09-13
 +
| New Permit Application
 +
|-
 +
| 1984-12-12
 +
| Drilling Completion
 +
|-
 +
| 1984-12-23
 +
| Perforation
 +
|-
 +
| 1984-12-26
 +
| Performed Stimulation 
 +
|-
 +
| 1985-08-26
 +
| NEWLY DRILLED
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Compiled from multiple data sources - see Pennsylvania Oil and Gas Data Sources
 +
| date = 2020-02-27
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-02-27 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Job Number
 +
!scope="col" | Job Start Date
 +
!scope="col" | Job End Date
 +
!scope="col" | True Vertical Depth (ft)
 +
!scope="col" | Total Water Volume (gal)
 +
!scope="col" | Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Job Number
 +
!scope="col" | Trade Name
 +
!scope="col" | Supplier
 +
!scope="col" | Purpose
 +
!scope="col" | Ingredient Name
 +
!scope="col" | CAS Number
 +
!scope="col" | Additive Percentage by Mass
 +
!scope="col" | Job Percentage by Mass
 +
!scope="col" | Mass Used (lb)
 +
|-
 +
|}-->
 +
 +
== Stimulation Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Stimulation Date
 +
!scope="col" | Phase Number
 +
!scope="col" | Chemical Agent
 +
!scope="col" | Volume (gal)
 +
!scope="col" | Treating Pressure (psi)
 +
!scope="col" | Breakdown Pressure (psi)
 +
|-
 +
| 1984-12-26
 +
| style="text-align: right;" |
 +
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Completion Reports - Stimulations
 +
| publisher = Pennsylvania Department of Conservation and Natural Resources
 +
| date = 2020-03-02
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-03-02 }}</ref>
 
== Production Data ==
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" | Period
!scope="col" | GAS QUANTITY
+
!scope="col" | Operator Name
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" | Gas Quantity (mcf)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" | Gas Production Days
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" | Oil Quantity (bbl)
!scope="col" | OIL QUANTITY
+
!scope="col" | Oil Production Days
!scope="col" | OIL PRODUCTION DAYS
+
!scope="col" | Water Quantity (bbl)
 +
!scope="col" | Water Production Days
 +
|-
 +
| 1989
 +
| [[MITCH WELL ENERGY INC]]
 +
| style="text-align: right;" | 3,200.00
 +
| style="text-align: right;" | 300
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2012-0
+
| 2012
| style="text-align:right;" | 100.0
+
| [[MITCH WELL ENERGY INC]]
| style="text-align:right;" | 365.0
+
| style="text-align: right;" | 100.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
+
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title =Oil and Gas Production Reports
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-03-31
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 
== Waste Data ==
 
== Waste Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" | Period
!scope="col" | TYPE
+
!scope="col" | Operator
!scope="col" | QUANTITY
+
!scope="col" | Waste Type
!scope="col" | UNITS
+
!scope="col" | Quantity
!scope="col" | DISPOSAL METHOD
+
!scope="col" | Disposal Method
!scope="col" | WASTE FACILITY PERMIT ID
+
!scope="col" | Waste Facility ID
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|-
 
| 2012-0
 
| PRODUCED FLUID
 
| style="text-align:right;" | 1.0
 
| Bbl
 
| STORAGE PENDING DISPOSAL OR REUSE
 
|
 
| STORAGE PENDING DISPOSAL OR REUSE
 
|
 
| PA
 
 
|-
 
|-
|-
+
| 2012
| 2012-0
+
| [[MITCH WELL ENERGY INC]]
| PRODUCED FLUID
+
| Produced Fluid
| style="text-align:right;" | 1.0
+
| style="text-align: right;" | 1.00 Bbl
| Bbl
 
 
| STORAGE PENDING DISPOSAL OR REUSE
 
| STORAGE PENDING DISPOSAL OR REUSE
 
|  
 
|  
| STORAGE PENDING DISPOSAL OR REUSE
 
|
 
| PA
 
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title =Oil and Gas Waste Reports
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-03-31
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" | Inspection ID
!scope="col" | DATE
+
!scope="col" | Inspection Category
!scope="col" | DESCRIPTION
+
!scope="col" | Inspection Date
!scope="col" | COMMENT
+
!scope="col" | Inspection Type
!scope="col" | VIOLATION ID
+
!scope="col" | Inspection Result
 +
!scope="col" | Inspection Comments
 
|-
 
|-
 
| 1963683
 
| 1963683
 +
| Primary Facility
 
| 2011-04-04
 
| 2011-04-04
 +
| Routine/Complete Inspection
 
| Violation(s) Noted
 
| Violation(s) Noted
 
| I inspected this well to determine if it has been abandon. Upon inspection I found the well commerically shut-in and producing only house gas. I spoke to the land  owner, Mr Weiser and he indicated that Bill Mitchwell has not been on-site for years. The steel production tank is rusted out and discinnected. The heater/dryer on-site, but unaccessable due to heavy brush growth. The commerical sales line going out is valved off.  The equipment is in a state of disrepair. The landowner told me he would like an opportunity to buy the well, instead of it being plugged.
 
| I inspected this well to determine if it has been abandon. Upon inspection I found the well commerically shut-in and producing only house gas. I spoke to the land  owner, Mr Weiser and he indicated that Bill Mitchwell has not been on-site for years. The steel production tank is rusted out and discinnected. The heater/dryer on-site, but unaccessable due to heavy brush growth. The commerical sales line going out is valved off.  The equipment is in a state of disrepair. The landowner told me he would like an opportunity to buy the well, instead of it being plugged.
| 608238
 
 
|-
 
|-
 +
| 2110178
 +
| Primary Facility
 +
| 2012-10-12
 +
| Follow-up Inspection
 +
| Outstanding Violations - No Viols Req'd
 +
|
 +
|-
 +
| 2162572
 +
| Primary Facility
 +
| 2013-04-25
 +
| Follow-up Inspection
 +
| No Violations Noted
 +
|
 +
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Inspection ID
 +
!scope="col" | Violation ID
 +
!scope="col" | Violation Date
 +
!scope="col" | Date Resolved
 +
!scope="col" | Violation Code
 +
!scope="col" | Violation Type
 +
!scope="col" | Violation Comments
 
|-
 
|-
 
| 1963683
 
| 1963683
 +
| 608238
 +
| 04/04/2011
 
| 2011-04-04
 
| 2011-04-04
| Violation(s) Noted
+
| 509 - Failure to comply w/ order, CO&A, hindrance to personnel, misrepresentation under OGA
| I inspected this well to determine if it has been abandon. Upon inspection I found the well commerically shut-in and producing only house gas. I spoke to the land  owner, Mr Weiser and he indicated that Bill Mitchwell has not been on-site for years. The steel production tank is rusted out and discinnected. The heater/dryer on-site, but unaccessable due to heavy brush growth. The commerical sales line going out is valved off.  The equipment is in a state of disrepair. The landowner told me he would like an opportunity to buy the well, instead of it being plugged.
+
| Administrative
| 608238
+
|  
 
|-
 
|-
 +
|}
 +
==== Penalties Applied ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Violation ID
 +
!scope="col" | Penalty ID
 +
!scope="col" | Penalty Code
 +
!scope="col" | Penalty Status
 +
!scope="col" | Penalty Date
 +
!scope="col" | Enforcement Date
 +
!scope="col" | Penalty Amount
 +
!scope="col" | Amount Collected
 
|-
 
|-
| 1963683
 
| 2011-04-04
 
| Violation(s) Noted
 
| I inspected this well to determine if it has been abandon. Upon inspection I found the well commerically shut-in and producing only house gas. I spoke to the land  owner, Mr Weiser and he indicated that Bill Mitchwell has not been on-site for years. The steel production tank is rusted out and discinnected. The heater/dryer on-site, but unaccessable due to heavy brush growth. The commerical sales line going out is valved off.  The equipment is in a state of disrepair. The landowner told me he would like an opportunity to buy the well, instead of it being plugged.
 
 
| 608238
 
| 608238
 +
| 269756
 +
| NOV - Notice of Violation
 +
| Superseded
 +
|
 +
| 2013-01-29
 +
| style="text-align: right;" |
 +
| style="text-align: right;" |
 
|-
 
|-
 +
| 608238
 +
| 292029
 +
| ADORD - Administrative Order
 +
| Superseded
 +
|
 +
| 2013-01-29
 +
| style="text-align: right;" |
 +
| style="text-align: right;" |
 
|-
 
|-
| 2110178
+
| 608238
| 2012-10-12
+
| 294448
| Outstanding Violations - No Viols Req'd
+
| ADORD - Administrative Order
 +
|  
 
|  
 
|  
 
|  
 
|  
|-
+
| style="text-align: right;" |  
|-
+
| style="text-align: right;" |  
| 2162572
 
| 2013-04-25
 
| Erie
 
| Greene Twp
 
| No Violations Noted
 
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title =Oil and Gas Compliance Report
 +
|publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2019-05-20
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 
==References==
 
==References==
{{Reflist}}
+
<references/>
 
 
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Pennsylvania Wells]]

Latest revision as of 15:20, 2 June 2020

Well Details

Well ID: 37-049-24158
Loading map...
Country: United States
State: Pennsylvania
County: Erie
Municipality: Greene Township
Operator Name:
Well Pad ID:
Farm/Lease Name: WEISER 1
License Status:
Spud Date:
Permit Date: 1984-09-13
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: Yes
Latitude: 42.019851
Longitude: -79.949912

For data sources see[1][2][3]

Well History

Date Event
1984-09-13 New Permit Application
1984-12-12 Drilling Completion
1984-12-23 Perforation
1984-12-26 Performed Stimulation
1985-08-26 NEWLY DRILLED

For data sources see[4]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
1984-12-26 0 0 0

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1989 MITCH WELL ENERGY INC 3,200.00 300 0.00 0 0.00 0
2012 MITCH WELL ENERGY INC 100.00 365 0.00 0 0.00 0

For data sources see[6]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2012 MITCH WELL ENERGY INC Produced Fluid 1.00 Bbl STORAGE PENDING DISPOSAL OR REUSE

For data sources see[7]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1963683 Primary Facility 2011-04-04 Routine/Complete Inspection Violation(s) Noted I inspected this well to determine if it has been abandon. Upon inspection I found the well commerically shut-in and producing only house gas. I spoke to the land owner, Mr Weiser and he indicated that Bill Mitchwell has not been on-site for years. The steel production tank is rusted out and discinnected. The heater/dryer on-site, but unaccessable due to heavy brush growth. The commerical sales line going out is valved off. The equipment is in a state of disrepair. The landowner told me he would like an opportunity to buy the well, instead of it being plugged.
2110178 Primary Facility 2012-10-12 Follow-up Inspection Outstanding Violations - No Viols Req'd
2162572 Primary Facility 2013-04-25 Follow-up Inspection No Violations Noted

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
1963683 608238 04/04/2011 2011-04-04 509 - Failure to comply w/ order, CO&A, hindrance to personnel, misrepresentation under OGA Administrative

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
608238 269756 NOV - Notice of Violation Superseded 2013-01-29
608238 292029 ADORD - Administrative Order Superseded 2013-01-29
608238 294448 ADORD - Administrative Order

For data sources see[8]

References