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Difference between revisions of "34-045-20834"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-045-20834
 
| Well ID: 34-045-20834
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.6801831, -82.38305433 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.680253856, -82.38264692 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Fairfield County, Ohio|Fairfield]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Fairfield_County,_Ohio|Fairfield]]
 +
|-
 +
| Municipality: [[Rush_Creek_Township,_Fairfield_County,_Ohio|Rush creek Township]]
 
|-
 
|-
 
| Operator Name: [[ENGLE DAVID G SR]]
 
| Operator Name: [[ENGLE DAVID G SR]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: ENGLE D ETAL
 
|-
 
|-
| First Permit Date:  
+
| License Status: Domestic Well
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 1982-12-06
 
|-
 
|-
 
| Spud Date: 1982-12-16
 
| Spud Date: 1982-12-16
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor: [[SHOULTS DRLG]]
 +
|-
 +
| Final Drill Date: 1983-02-07
 +
|-
 +
| Well Total Depth: 2785 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Domestic Well
+
| Latitude: 39.680253856
 +
|-
 +
| Longitude: -82.38264692
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| Oil and Gas
 +
| 1982-12-06
 +
| Issued Date 12/6/82 Expired Date 6/4/83 Acres 0020000 Tool Type CT Proposed Formation CLINTON Proposed Depth 02785 Proposed Drill Depth 02785
 +
|-
 +
| Original Spud
 +
| 1982-12-16
 +
 +
|-
 +
| Completed
 +
| 1983-02-07
 +
 +
|-
 +
| Reached Total Depth
 +
| 1983-02-07
 +
 +
|-
 +
| Completion Report Received
 +
| 1983-03-17
 +
 +
|-
 +
| CO
 +
| 1983-03-20
 +
| 136  ALTEX INC  GeoDate  12/6/82
 +
|-
 +
| Change of Owner
 +
| 1998-10-21
 +
| Operator changed from 136, ALTEX INC to 1429, ALTIER BROTHERS INC
 +
|-
 +
| APP
 +
| 2002-01-03
 +
| Proposed Formations:CLINTON, Issued Date:1/3/2002, Expired Date:1/3/2003 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:HAD, Proposed Well Class:
 +
|-
 +
| Change of Owner
 +
| 2002-06-05
 +
| Operator changed from 1429, ALTIER BROTHERS INC to 7227, ENGLE DAVID G SR
 +
|-
 +
| Construction Permit Expires
 +
| 2003-01-03
 +
 +
|-
 +
| Record Last Modified
 +
| 2017-02-15
 +
 
|-
 
|-
| Violations: 0
+
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 
|-
 
|-
| Latitude: 39.6801831
+
| 1997-06-29
 +
| style="text-align: right;" | 2750
 +
| style="text-align: right;" | 2772
 +
| style="text-align: right;" | 0
 
|-
 
|-
| Longitude: -82.38305433
+
| 2006-09-11
 +
| style="text-align: right;" | 2752
 +
| style="text-align: right;" | 2772
 +
| style="text-align: right;" | 2
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
== Stimulations Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Stimulation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Chemical Agent
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Fracking Fluid Volume
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
!scope="col" | OIL QUANTITY
+
!scope="col" style="text-align: center"| Fracking Company
!scope="col" | OIL PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 1985-0
 
| style="text-align:right;" | 5906.0
 
 
|  
 
|  
 +
| H2O
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 50000
 
|  
 
|  
|  
+
| FRAC;H2O,50M# SAND
| style="text-align:right;" | 1789.0
+
|-
|  
+
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 1985
 +
| [[ALTEX INC]]
 +
| style="text-align: right;" | 5906
 +
| style="text-align: right;" | 1789
 +
| style="text-align: right;" | 6
 +
|-
 +
| 1999
 +
| [[ALTHEIRS OIL INC]]
 +
| style="text-align: right;" | 185
 +
| style="text-align: right;" | 367
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2000
 +
| [[ALTHEIRS OIL INC]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 145
 +
| style="text-align: right;" | 365
 
|-
 
|-
 +
| 2001
 +
| [[ALTHEIRS OIL INC]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1999-0
+
| 2002
| style="text-align:right;" | 185.0
+
| [[ALTHEIRS OIL INC]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 367.0
 
|
 
 
|-
 
|-
 +
| 2003
 +
| [[ALTHEIRS OIL INC]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2000-0
+
|}
| style="text-align:right;" | 0.0
+
For data sources see<ref>{{cite web
|  
+
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
|  
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date =  2019-05-07
| style="text-align:right;" | 145.0
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
|
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
| 1985
 +
| [[ALTEX INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 6
 
|-
 
|-
| 2001-0
+
| 1999
| style="text-align:right;" | 0.0
+
| [[ALTHEIRS OIL INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2000
 +
| [[ALTHEIRS OIL INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2002-0
+
| 2001
| style="text-align:right;" | 0.0
+
| [[ALTHEIRS OIL INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2002
 +
| [[ALTHEIRS OIL INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2003-0
+
| 2003
| style="text-align:right;" | 0.0
+
| [[ALTHEIRS OIL INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2019-05-07
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2019-05-21 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
| 1248i191
+
| 001248i191
 
| 2002-01-30
 
| 2002-01-30
|  
+
| Production Wells
 +
| No Violations
 
| WEATHER CONDITIONS: Rain and 45 degrees. Inspection revealed no violations noted this date. (Service rig was to be on location this week for service work or plugging operations.)
 
| WEATHER CONDITIONS: Rain and 45 degrees. Inspection revealed no violations noted this date. (Service rig was to be on location this week for service work or plugging operations.)
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 001248i274
| 1248i274
 
 
| 2002-03-01
 
| 2002-03-01
|  
+
| Work Over Reconditioning
 +
| No Violations
 
| WEATHER CONDITIONS: Sunny and 30 degrees. Inspection revealed Altiers service rig over the well pilling rods and tubing. Owner obtained plugging permit but the service rig was able to retrieve the down hole equipment so the owner is going to place the well back into production.
 
| WEATHER CONDITIONS: Sunny and 30 degrees. Inspection revealed Altiers service rig over the well pilling rods and tubing. Owner obtained plugging permit but the service rig was able to retrieve the down hole equipment so the owner is going to place the well back into production.
|  
+
|-
|  
+
| 0401126978
|  
+
| 2019-04-18
 +
| Production Wells
 +
| No Violations
 +
| My inspection for compliance revealed the well did not have legible identification. The phone number listed for the well was a non working number. I do not have another option to contact the owner of this well to obtain compliance.
 +
|-
 +
| 0429944094
 +
| 2019-03-15
 +
| Production Wells
 +
| No Violations
 +
| My inspection revealed this wells status remains unchanged since my last inspection on 1.18.19. The well lacks legible identification. The owner of this well is deceased. I will attempt to contact the widow of the deceased owner to bring the well into compliance.
 +
|-
 +
| 0937357720
 +
| 2018-11-30
 +
| Production Wells
 +
| No Violations
 +
| My follow up inspection revealed the wells status remains unchanged. The well lacks a legible identification. I have spoke with Mrs. Engel and she stated she is working on getting a sign made for the identification.
 +
|-
 +
| 1063796230
 +
| 2018-11-02
 +
| Production Wells
 +
| No Violations
 +
| My inspection revealed the well consists of 4.5 inch diameter casing with a 4.5 inch diameter to 2 inch diameter swage. There was a plastic line plumbed into the tee fitting on top of the swage. There was a valve that was plumbed into the 1 inch line that was in the open position. The tank battery consisted of 1-100 barrel tank. The well lacked a legible identification. The owner of the well shall place a legible identification at the wellhead or at the tank battery.
 +
|-
 +
| 1437096072
 +
| 2019-01-18
 +
| Production Wells
 +
| No Violations
 +
| My inspection revealed this well does not have a legible identification. I called the phone number listed for the owner of the well. This phone number is not a working number.
 +
|-
 +
| 1471347966
 +
| 2018-11-19
 +
| Production Wells
 +
| No Violations
 +
| At 12:42 PM I attempted to call well owner Mr. David Engel. The phone number listed in RBDMS is no longer a working number. The well remains in violation for no legible identification. I will ask the neighbors if they know if Mr. Engle is alive or deceased.
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 20:58, 24 July 2019

Well Details

Well ID: 34-045-20834
Loading map...
Country: United States
State: Ohio
County: Fairfield
Municipality: Rush creek Township
Operator Name: ENGLE DAVID G SR
Well Pad ID:
Farm/Lease Name: ENGLE D ETAL
License Status: Domestic Well
License Date: 1982-12-06
Spud Date: 1982-12-16
Spud Drilling Contractor: SHOULTS DRLG
Final Drill Date: 1983-02-07
Well Total Depth: 2785 ft
Configuration: Vertical
Latitude: 39.680253856
Longitude: -82.38264692

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1982-12-06 Issued Date 12/6/82 Expired Date 6/4/83 Acres 0020000 Tool Type CT Proposed Formation CLINTON Proposed Depth 02785 Proposed Drill Depth 02785
Original Spud 1982-12-16
Completed 1983-02-07
Reached Total Depth 1983-02-07
Completion Report Received 1983-03-17
CO 1983-03-20 136 ALTEX INC GeoDate 12/6/82
Change of Owner 1998-10-21 Operator changed from 136, ALTEX INC to 1429, ALTIER BROTHERS INC
APP 2002-01-03 Proposed Formations:CLINTON, Issued Date:1/3/2002, Expired Date:1/3/2003 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:HAD, Proposed Well Class:
Change of Owner 2002-06-05 Operator changed from 1429, ALTIER BROTHERS INC to 7227, ENGLE DAVID G SR
Construction Permit Expires 2003-01-03
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 2750 2772 0
2006-09-11 2752 2772 2

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 0 50000 FRAC;H2O,50M# SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 ALTEX INC 5906 1789 6
1999 ALTHEIRS OIL INC 185 367 365
2000 ALTHEIRS OIL INC 0 145 365
2001 ALTHEIRS OIL INC 0 0 365
2002 ALTHEIRS OIL INC 0 0 365
2003 ALTHEIRS OIL INC 0 0 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 ALTEX INC Brine 0 6
1999 ALTHEIRS OIL INC Brine 0 365
2000 ALTHEIRS OIL INC Brine 0 365
2001 ALTHEIRS OIL INC Brine 0 365
2002 ALTHEIRS OIL INC Brine 0 365
2003 ALTHEIRS OIL INC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
001248i191 2002-01-30 Production Wells No Violations WEATHER CONDITIONS: Rain and 45 degrees. Inspection revealed no violations noted this date. (Service rig was to be on location this week for service work or plugging operations.)
001248i274 2002-03-01 Work Over Reconditioning No Violations WEATHER CONDITIONS: Sunny and 30 degrees. Inspection revealed Altiers service rig over the well pilling rods and tubing. Owner obtained plugging permit but the service rig was able to retrieve the down hole equipment so the owner is going to place the well back into production.
0401126978 2019-04-18 Production Wells No Violations My inspection for compliance revealed the well did not have legible identification. The phone number listed for the well was a non working number. I do not have another option to contact the owner of this well to obtain compliance.
0429944094 2019-03-15 Production Wells No Violations My inspection revealed this wells status remains unchanged since my last inspection on 1.18.19. The well lacks legible identification. The owner of this well is deceased. I will attempt to contact the widow of the deceased owner to bring the well into compliance.
0937357720 2018-11-30 Production Wells No Violations My follow up inspection revealed the wells status remains unchanged. The well lacks a legible identification. I have spoke with Mrs. Engel and she stated she is working on getting a sign made for the identification.
1063796230 2018-11-02 Production Wells No Violations My inspection revealed the well consists of 4.5 inch diameter casing with a 4.5 inch diameter to 2 inch diameter swage. There was a plastic line plumbed into the tee fitting on top of the swage. There was a valve that was plumbed into the 1 inch line that was in the open position. The tank battery consisted of 1-100 barrel tank. The well lacked a legible identification. The owner of the well shall place a legible identification at the wellhead or at the tank battery.
1437096072 2019-01-18 Production Wells No Violations My inspection revealed this well does not have a legible identification. I called the phone number listed for the owner of the well. This phone number is not a working number.
1471347966 2018-11-19 Production Wells No Violations At 12:42 PM I attempted to call well owner Mr. David Engel. The phone number listed in RBDMS is no longer a working number. The well remains in violation for no legible identification. I will ask the neighbors if they know if Mr. Engle is alive or deceased.

For data sources see[9]

References