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Difference between revisions of "34-167-24603"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-167-24603
 
| Well ID: 34-167-24603
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.29706593, -81.6752944 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.296990919, -81.67544288 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Washington County, Ohio|Washington]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Washington_County,_Ohio|Washington]]
 +
|-
 +
| Municipality: [[Belpre,_Ohio|Belpre]]
 
|-
 
|-
 
| Operator Name: [[HUFFMAN-BOWERS INC]]
 
| Operator Name: [[HUFFMAN-BOWERS INC]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: RICHARDSON CALVIN & RUTH
 
|-
 
|-
| First Permit Date:  
+
| License Status: Producing
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 1979-04-13
 
|-
 
|-
 
| Spud Date:  
 
| Spud Date:  
 
|-
 
|-
| Unconventional:  
+
| Spud Drilling Contractor:  
 +
|-
 +
| Final Drill Date:
 +
|-
 +
| Well Total Depth:
 +
|-
 +
| Configuration: Vertical
 
|-
 
|-
| Configuration:  
+
| Latitude: 39.296990919
 
|-
 
|-
| Well Status: Producing
+
| Longitude: -81.67544288
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 
|-
 
|-
| Violations: 0
+
| CO
 +
| 1979-04-13
 +
| 187  L & S OIL AND GAS  GeoDate  4/13/79
 
|-
 
|-
| Latitude: 39.29706593
+
| Oil and Gas
 +
| 1979-04-13
 +
| Issued Date 4/13/79 Expired Date 4/12/80 Acres 0000000 Tool Type  Proposed Formation  Proposed Depth 00000 Proposed Drill Depth 00000
 
|-
 
|-
| Longitude: -81.6752944
+
| Construction Permit Expires
 +
| 1980-04-12
 +
| PERMIT EXPIRED.
 +
|-
 +
| CO
 +
| 1996-04-10
 +
| 5155  HUFFMAN-BOWERS INC  GeoDate  4/13/79
 +
|-
 +
| Record Last Modified
 +
| 2014-01-09
 +
| PERMIT EXPIRED.
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 
== Production Data ==
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Period
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Operator Name
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Gas Quantity (mcf)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Oil Quantity (bbl)
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Production Days
!scope="col" | OIL QUANTITY
+
|-
!scope="col" | OIL PRODUCTION DAYS
+
| 1993
 +
| [[L & S OIL AND GAS]]
 +
| style="text-align: right;" | 520
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 60
 +
|-
 +
| 1996
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 1518
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 265
 +
|-
 +
| 1997
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 1546
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1998
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 1729
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1999
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 2007
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2000
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 1826
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2001
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 1567
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2002
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 1566
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2003
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 1420
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2005
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 694
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2006
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 2201
 +
| style="text-align: right;" | 70
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2007
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 1184
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2008
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 1847
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2009
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 1161
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2010
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 1733
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2011
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 2253
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2012
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 826
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 366
 +
|-
 +
| 2013
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 1488
 +
| style="text-align: right;" | 60
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2014
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 1495
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1993-0
+
| 2015
| style="text-align:right;" | 520.0
+
| [[HUFFMAN-BOWERS INC]]
|  
+
| style="text-align: right;" | 1797
|  
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
+
|-
|  
+
| 2016
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 1964
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2017
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 1513
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
 +
| 2018
 +
| [[HUFFMAN-BOWERS INC]]
 +
| style="text-align: right;" | 1394
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1996-0
+
|}
| style="text-align:right;" | 1518.0
+
For data sources see<ref>{{cite web
|  
+
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
|  
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date =  2019-05-07
| style="text-align:right;" | 0.0
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
|
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
| 1993
 +
| [[L & S OIL AND GAS]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 60
 
|-
 
|-
| 1997-0
+
| 1996
| style="text-align:right;" | 1546.0
+
| [[HUFFMAN-BOWERS INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 265
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1997
 +
| [[HUFFMAN-BOWERS INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1998-0
+
| 1998
| style="text-align:right;" | 1729.0
+
| [[HUFFMAN-BOWERS INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1999
 +
| [[HUFFMAN-BOWERS INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1999-0
+
| 2000
| style="text-align:right;" | 2007.0
+
| [[HUFFMAN-BOWERS INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2001
 +
| [[HUFFMAN-BOWERS INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2000-0
+
| 2002
| style="text-align:right;" | 1826.0
+
| [[HUFFMAN-BOWERS INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2003
 +
| [[HUFFMAN-BOWERS INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2001-0
+
| 2005
| style="text-align:right;" | 1567.0
+
| [[HUFFMAN-BOWERS INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2006
 +
| [[HUFFMAN-BOWERS INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2002-0
+
| 2007
| style="text-align:right;" | 1566.0
+
| [[HUFFMAN-BOWERS INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2008
 +
| [[HUFFMAN-BOWERS INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2003-0
+
| 2009
| style="text-align:right;" | 1420.0
+
| [[HUFFMAN-BOWERS INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2010
 +
| [[HUFFMAN-BOWERS INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2005-0
+
| 2011
| style="text-align:right;" | 694.0
+
| [[HUFFMAN-BOWERS INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2012
 +
| [[HUFFMAN-BOWERS INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 366
 
|-
 
|-
| 2006-0
+
| 2013
| style="text-align:right;" | 2201.0
+
| [[HUFFMAN-BOWERS INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 70.0
 
|
 
 
|-
 
|-
 +
| 2014
 +
| [[HUFFMAN-BOWERS INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2007-0
+
| 2015
| style="text-align:right;" | 1184.0
+
| [[HUFFMAN-BOWERS INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2016
 +
| [[HUFFMAN-BOWERS INC]]
 +
| Brine
 +
| style="text-align: right;" | 50
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2008-0
+
| 2017
| style="text-align:right;" | 1847.0
+
| [[HUFFMAN-BOWERS INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2018
 +
| [[HUFFMAN-BOWERS INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2009-0
+
|}
| style="text-align:right;" | 1161.0
+
For data sources see<ref>{{cite web
|  
+
| title = Risk Based Data Management System - Production Table - Brine Data
|  
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date =  2019-05-07
| style="text-align:right;" | 0.0
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
|
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Inspection Data ==
 +
==== Inspections Performed ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Inspection Date
 +
!scope="col" style="text-align: center"| Inspection Type
 +
!scope="col" style="text-align: center"| Inspection Result
 +
!scope="col" style="text-align: center"| Inspection Comments
 
|-
 
|-
 +
| 0029102370
 +
| 2016-01-15
 +
| Production Wells
 +
| No Violations
 +
| Upon inspection, it was observed that no effort has been made to reach compliance since the last inspection on 12/30/15. Free oil is still puddled around the well head. I will contact Mr. Barry Bowers and instruct him to clean the mess up and pack off the well head immediately to prevent further soil contamination.
 
|-
 
|-
| 2010-0
+
| 0391266452
| style="text-align:right;" | 1733.0
+
| 2016-06-07
|  
+
| Production Wells
|  
+
| No Violations
|  
+
| Upon inspection, it was observed that the well has recently been serviced to address leaking surface casing. The well now has a 7x 3.5 casing head welded in place which sealed the previously leaking annular space. All free oil product has been cleaned up around the well head area. In addition, a containment dike has been constructed around the tank battery. The location will be seeded and mulched to revegetate disturbed areas. This satisfies the requirements of the compliance notice dated 9/9/2015. I was accompanied on this inspection by DOGRM ER Coordinator Nathan Lane.
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 0453621292
 +
| 2016-05-13
 +
| Production Wells
 +
| No Violations
 +
| Upon inspection, it was observed that there has been no resolution to pollution and contamination issues at this well. I contacted Mr. Barry Bowers and instructed him to have a 7 x 3.5 well head installed on the well next week to prevent further leakage of oil from the well. Mr. Bowers agreed to have the issues resolved as soon as possible.
 
|-
 
|-
| 2011-0
+
| 0521244328
| style="text-align:right;" | 2253.0
+
| 2016-03-14
|  
+
| Production Wells
|  
+
| No Violations
|  
+
| Upon inspection, it was observed that no effort has been made by the operator to gain compliance. There is still no well head/packoff on the 7-3.5 annulus and there is oil and water pooled up around the casing. New photos were taken of the location.
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 0918789624
 +
| 2015-12-02
 +
| Production Wells
 +
| No Violations
 +
| Upon inspection, it was observed that oily soil around the well head has not been removed and more contamination has built up at the surface since the last inspection. Quantab samples of puddled fluid around the well head read 6.6, which is equivalent to 2245 ppm chlorides. I contacted Mr. Barry Bowers and instructed him to service the well and repair it in a manner which prevents the escape of oil and brine from the surface casing. Mr. Bowers stated he would bring a crew down next week to repair the well and clean up the contaminated soil and properly dispose of it.
 
|-
 
|-
| 2012-0
+
| 1050563619
| style="text-align:right;" | 826.0
+
| 2016-01-22
|  
+
| Production Wells
|  
+
| No Violations
|  
+
| Upon inspection, it was observed that work has been done to try and pack off the 3.5-7 annulus with an epoxy cement mixture. The attempt was unsuccessful as there is still oil leaking around the cement and pooling up around the casing on the ground. I contacted Mr. Barry Bowers and stated he must pack the well off properly with a 7-3.5 well head in order to prevent further leakage. Mr. Bowers agreed and stated he would bring a rig in to perform the work on the well.
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1107486943
 +
| 2015-12-30
 +
| Production Wells
 +
| No Violations
 +
| Upon inspection, it was observed that no effort has been made by the operator to gain compliance at this well location. There is still oily soil and gravel surrounding the well head, and the well has not been packed off to prevent further leakage. I contacted Mr. Barry Bowers at 8:32 a.m. and inquired why no work had been done. Mr. Bowers stated that it had been too wet to work on the well. Mr. Bowers stated that he would have the well packed off and the location cleaned up by the end of next week.
 
|-
 
|-
| 2013-0
+
| 1711517183
| style="text-align:right;" | 1488.0
+
| 2015-09-08
|  
+
| Production Wells
|  
+
| Violations Noted
|  
+
| Upon inspection, it was observed that this well is currently in production. The well consists of a pumping unit standing over 8.625 surface casing, 3.5 production casing, and 1.5 tubing. There is no well head on the 8.625 surface casing, allowing surface water to infiltrate and flow oil and brine onto the ground surface around the well. There is a vegetation kill area approximately 4 wide x 15 long extending downhill away from the well. I contacted Mr. Barry Bowers and notified him of the situation. Mr. Bowers stated that he knows of the problem and that this is not the first time is has happened. I told him to have the mess cleaned up by the end of the week and he agreed. I stronly recommended that he put a service rig on the well and install an 8.625- 4.5 well head to prevent such leaks from re-occurring.
| style="text-align:right;" | 60.0
 
|
 
 
|-
 
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 
|-
 
|-
| 2014-0
+
| 1711517183
| style="text-align:right;" | 1495.0
+
| US-OH-116964
| style="text-align:right;" | 365.0
+
| 2016-06-14
|
 
 
|  
 
|  
| style="text-align:right;" | 0.0
+
| Well operation causing pollution and contamination
| style="text-align:right;" | 365.0
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 07:55, 30 July 2019

Well Details

Well ID: 34-167-24603
Loading map...
Country: United States
State: Ohio
County: Washington
Municipality: Belpre
Operator Name: HUFFMAN-BOWERS INC
Well Pad ID:
Farm/Lease Name: RICHARDSON CALVIN & RUTH
License Status: Producing
License Date: 1979-04-13
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 39.296990919
Longitude: -81.67544288

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1979-04-13 187 L & S OIL AND GAS GeoDate 4/13/79
Oil and Gas 1979-04-13 Issued Date 4/13/79 Expired Date 4/12/80 Acres 0000000 Tool Type Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000
Construction Permit Expires 1980-04-12 PERMIT EXPIRED.
CO 1996-04-10 5155 HUFFMAN-BOWERS INC GeoDate 4/13/79
Record Last Modified 2014-01-09 PERMIT EXPIRED.

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1993 L & S OIL AND GAS 520 0 60
1996 HUFFMAN-BOWERS INC 1518 0 265
1997 HUFFMAN-BOWERS INC 1546 0 365
1998 HUFFMAN-BOWERS INC 1729 0 365
1999 HUFFMAN-BOWERS INC 2007 0 365
2000 HUFFMAN-BOWERS INC 1826 0 365
2001 HUFFMAN-BOWERS INC 1567 0 365
2002 HUFFMAN-BOWERS INC 1566 0 365
2003 HUFFMAN-BOWERS INC 1420 0 365
2005 HUFFMAN-BOWERS INC 694 0 365
2006 HUFFMAN-BOWERS INC 2201 70 365
2007 HUFFMAN-BOWERS INC 1184 0 365
2008 HUFFMAN-BOWERS INC 1847 0 365
2009 HUFFMAN-BOWERS INC 1161 0 365
2010 HUFFMAN-BOWERS INC 1733 0 365
2011 HUFFMAN-BOWERS INC 2253 0 365
2012 HUFFMAN-BOWERS INC 826 0 366
2013 HUFFMAN-BOWERS INC 1488 60 365
2014 HUFFMAN-BOWERS INC 1495 0 365
2015 HUFFMAN-BOWERS INC 1797 0 365
2016 HUFFMAN-BOWERS INC 1964 0 365
2017 HUFFMAN-BOWERS INC 1513 0 365
2018 HUFFMAN-BOWERS INC 1394 0 365

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1993 L & S OIL AND GAS Brine 0 60
1996 HUFFMAN-BOWERS INC Brine 0 265
1997 HUFFMAN-BOWERS INC Brine 0 365
1998 HUFFMAN-BOWERS INC Brine 0 365
1999 HUFFMAN-BOWERS INC Brine 0 365
2000 HUFFMAN-BOWERS INC Brine 0 365
2001 HUFFMAN-BOWERS INC Brine 0 365
2002 HUFFMAN-BOWERS INC Brine 0 365
2003 HUFFMAN-BOWERS INC Brine 0 365
2005 HUFFMAN-BOWERS INC Brine 0 365
2006 HUFFMAN-BOWERS INC Brine 0 365
2007 HUFFMAN-BOWERS INC Brine 0 365
2008 HUFFMAN-BOWERS INC Brine 0 365
2009 HUFFMAN-BOWERS INC Brine 0 365
2010 HUFFMAN-BOWERS INC Brine 0 365
2011 HUFFMAN-BOWERS INC Brine 0 365
2012 HUFFMAN-BOWERS INC Brine 0 366
2013 HUFFMAN-BOWERS INC Brine 0 365
2014 HUFFMAN-BOWERS INC Brine 0 365
2015 HUFFMAN-BOWERS INC Brine 0 365
2016 HUFFMAN-BOWERS INC Brine 50 365
2017 HUFFMAN-BOWERS INC Brine 0 365
2018 HUFFMAN-BOWERS INC Brine 0 365

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0029102370 2016-01-15 Production Wells No Violations Upon inspection, it was observed that no effort has been made to reach compliance since the last inspection on 12/30/15. Free oil is still puddled around the well head. I will contact Mr. Barry Bowers and instruct him to clean the mess up and pack off the well head immediately to prevent further soil contamination.
0391266452 2016-06-07 Production Wells No Violations Upon inspection, it was observed that the well has recently been serviced to address leaking surface casing. The well now has a 7x 3.5 casing head welded in place which sealed the previously leaking annular space. All free oil product has been cleaned up around the well head area. In addition, a containment dike has been constructed around the tank battery. The location will be seeded and mulched to revegetate disturbed areas. This satisfies the requirements of the compliance notice dated 9/9/2015. I was accompanied on this inspection by DOGRM ER Coordinator Nathan Lane.
0453621292 2016-05-13 Production Wells No Violations Upon inspection, it was observed that there has been no resolution to pollution and contamination issues at this well. I contacted Mr. Barry Bowers and instructed him to have a 7 x 3.5 well head installed on the well next week to prevent further leakage of oil from the well. Mr. Bowers agreed to have the issues resolved as soon as possible.
0521244328 2016-03-14 Production Wells No Violations Upon inspection, it was observed that no effort has been made by the operator to gain compliance. There is still no well head/packoff on the 7-3.5 annulus and there is oil and water pooled up around the casing. New photos were taken of the location.
0918789624 2015-12-02 Production Wells No Violations Upon inspection, it was observed that oily soil around the well head has not been removed and more contamination has built up at the surface since the last inspection. Quantab samples of puddled fluid around the well head read 6.6, which is equivalent to 2245 ppm chlorides. I contacted Mr. Barry Bowers and instructed him to service the well and repair it in a manner which prevents the escape of oil and brine from the surface casing. Mr. Bowers stated he would bring a crew down next week to repair the well and clean up the contaminated soil and properly dispose of it.
1050563619 2016-01-22 Production Wells No Violations Upon inspection, it was observed that work has been done to try and pack off the 3.5-7 annulus with an epoxy cement mixture. The attempt was unsuccessful as there is still oil leaking around the cement and pooling up around the casing on the ground. I contacted Mr. Barry Bowers and stated he must pack the well off properly with a 7-3.5 well head in order to prevent further leakage. Mr. Bowers agreed and stated he would bring a rig in to perform the work on the well.
1107486943 2015-12-30 Production Wells No Violations Upon inspection, it was observed that no effort has been made by the operator to gain compliance at this well location. There is still oily soil and gravel surrounding the well head, and the well has not been packed off to prevent further leakage. I contacted Mr. Barry Bowers at 8:32 a.m. and inquired why no work had been done. Mr. Bowers stated that it had been too wet to work on the well. Mr. Bowers stated that he would have the well packed off and the location cleaned up by the end of next week.
1711517183 2015-09-08 Production Wells Violations Noted Upon inspection, it was observed that this well is currently in production. The well consists of a pumping unit standing over 8.625 surface casing, 3.5 production casing, and 1.5 tubing. There is no well head on the 8.625 surface casing, allowing surface water to infiltrate and flow oil and brine onto the ground surface around the well. There is a vegetation kill area approximately 4 wide x 15 long extending downhill away from the well. I contacted Mr. Barry Bowers and notified him of the situation. Mr. Bowers stated that he knows of the problem and that this is not the first time is has happened. I told him to have the mess cleaned up by the end of the week and he agreed. I stronly recommended that he put a service rig on the well and install an 8.625- 4.5 well head to prevent such leaks from re-occurring.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1711517183 US-OH-116964 2016-06-14 Well operation causing pollution and contamination

For data sources see[7]

References