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Difference between revisions of "34-059-24410"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-059-24410
 
| Well ID: 34-059-24410
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.08477235, -81.26478762 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.084703143, -81.26495495 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Guernsey County, Ohio|Guernsey]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Guernsey_County,_Ohio|Guernsey]]
 +
|-
 +
| Municipality: [[Londonderry_Township,_Guernsey_County,_Ohio|Londonderry Township]]
 
|-
 
|-
 
| Operator Name: [[ECLIPSE RESOURCES I LP]]
 
| Operator Name: [[ECLIPSE RESOURCES I LP]]
 
|-
 
|-
| Well Pad ID:  
+
| Well Pad ID: [[US-OH-001087]]
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: ABE TROYER
 
|-
 
|-
| First Permit Date:  
+
| License Status: Producing
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2014-08-08
 
|-
 
|-
 
| Spud Date: 2014-09-25
 
| Spud Date: 2014-09-25
 
|-
 
|-
| Unconventional:
+
| Spud Drilling Contractor: [[NOMAC DRILLING CORP]]
|-
 
| Configuration:  
 
 
|-
 
|-
| Well Status: Well Drilled
+
| Final Drill Date: 2014-12-27
 
|-
 
|-
| Violations: 0
+
| Well Total Depth: 14953 ft
 
|-
 
|-
| Latitude: 40.08477235
+
| Configuration: Horizontal
 
|-
 
|-
| Longitude: -81.26478762
+
| Latitude: 40.084703143
 
|-
 
|-
 +
| Longitude: -81.26495495
 
|}
 
|}
== Inspection Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Well Status
!scope="col" | DATE
+
!scope="col" style="width: 15%;text-align: center"| Well Status Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Comment
!scope="col" | COMMENT
+
|-
!scope="col" | VIOLATION ID
+
| APP
!scope="col" | VIOLATION CODE
+
| 2014-08-08
!scope="col" | VIOLATION COMMENT
+
| Proposed Formations:POINT PLEASANT, Issued Date:8/8/2014, Expired Date:8/7/2016 12:00:00 PM, Drilling unit acres:698.607, Proposed Well Type:OG, Proposed Well Class:EDPW
 
|-
 
|-
| 1418653519
+
| Reached Total Depth
| 2014-12-15
+
| 2014-12-27
 
|  
 
|  
| On the day of my inspection I witnessed that Nomac Drilling Rig #359 was drilling a 17.5 inch diameter vertical hole at a depth of 587 feet with a planned td of 1359 feet. 13.375 inch casing and cementing to follow early Tuesday morning. Site inspection revealed no violations.
+
|-
 +
| Construction Permit Expires
 +
| 2016-08-07
 
|  
 
|  
 +
|-
 +
| Completion Report Received
 +
| 2017-05-23
 
|  
 
|  
 +
|-
 +
| Record Last Modified
 +
| 2019-06-11
 
|  
 
|  
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
| 2017-05-30
 +
| style="text-align: right;" | 7993
 +
| style="text-align: right;" | 8149
 +
| style="text-align: right;" | 36
 +
|-
 +
| 2017-05-30
 +
| style="text-align: right;" | 14639
 +
| style="text-align: right;" | 14811
 +
| style="text-align: right;" | 48
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
| 1
 +
| 11/17/2016
 +
| 12/03/2016
 +
| style="text-align: right;" | 7929
 +
| style="text-align: right;" | 15,919,600.0
 +
| style="text-align: right;" | 0
 +
|-
 +
|}
 +
==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|- valign="top"
 +
| rowspan="22"| 1
 +
| rowspan="1"| FE-1A ACIDIZING COMPOSITION
 +
| rowspan="1"| Halliburton
 +
| rowspan="1"| Additive
 +
| Listed Below
 +
| Listed Below
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| FDP-S1225-15
 +
| rowspan="1"| Halliburton
 +
| rowspan="1"| Surfactant
 +
| Listed Below
 +
| Listed Below
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| SAND-PREMIUM WHITE-40/70
 +
| rowspan="1"| Halliburton
 +
| rowspan="1"| Proppant
 +
| Listed Below
 +
| Listed Below
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="14"|
 +
| rowspan="14"|
 +
| rowspan="14"|
 +
| Crystalline silica, quartz
 +
| 14808-60-7
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 11.5714
 +
| style="text-align: right;" | 17,401,300.0
 +
|-
 +
| Fatty acids, tall oil
 +
| Proprietary
 +
| style="text-align: right;" | 30
 +
| style="text-align: right;" | 0.000133659
 +
| style="text-align: right;" | 201
 +
|-
 +
| Hydrochloric acid
 +
| 7647-01-0
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 0.0367263
 +
| style="text-align: right;" | 55230
 +
|-
 +
| Olefins
 +
| Proprietary
 +
| style="text-align: right;" | 5
 +
| style="text-align: right;" | 0.00005453
 +
| style="text-align: right;" | 82
 +
|-
 +
| Propargyl alcohol
 +
| 107-19-7
 +
| style="text-align: right;" | 10
 +
| style="text-align: right;" | 0.00004455
 +
| style="text-align: right;" | 67
 +
|-
 +
| Alcohols, C12-16, ethoxylated
 +
| 68551-12-2
 +
| style="text-align: right;" | 5
 +
| style="text-align: right;" | 0.00002593
 +
| style="text-align: right;" | 39
 +
|-
 +
| Acetic anhydride
 +
| 108-24-7
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 0.0010726
 +
| style="text-align: right;" | 1613
 +
|-
 +
| Glycerine
 +
| 56-81-5
 +
| style="text-align: right;" | 5
 +
| style="text-align: right;" | 0.00002593
 +
| style="text-align: right;" | 39
 +
|-
 +
| Methanol
 +
| 67-56-1
 +
| style="text-align: right;" | 60
 +
| style="text-align: right;" | 0.000266653
 +
| style="text-align: right;" | 401
 +
|-
 +
| Acetic acid
 +
| 64-19-7
 +
| style="text-align: right;" | 60
 +
| style="text-align: right;" | 0.000649011
 +
| style="text-align: right;" | 976
 +
|-
 +
| Alcohols, C12-13, ethoxylated
 +
| 66455-14-9
 +
| style="text-align: right;" | 30
 +
| style="text-align: right;" | 0.000154938
 +
| style="text-align: right;" | 233
 +
|-
 +
| Ethylene oxide
 +
| 75-21-8
 +
| style="text-align: right;" | 0.01
 +
| style="text-align: right;" | 0.00000066
 +
| style="text-align: right;" | 1
 +
|-
 +
| Reaction product of acetophenone, formaldehyde, thiourea and oleic acid in dimethyl formamide
 +
| 68527-49-1
 +
| style="text-align: right;" | 30
 +
| style="text-align: right;" | 0.000133659
 +
| style="text-align: right;" | 201
 +
|-
 +
| Ethoxylated alcohols
 +
| Proprietary
 +
| style="text-align: right;" | 30
 +
| style="text-align: right;" | 0.000133659
 +
| style="text-align: right;" | 201
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| HYDROCHLORIC ACID
 +
| rowspan="1"| Halliburton
 +
| rowspan="1"| Solvent
 +
| Listed Below
 +
| Listed Below
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| SAND-COMMON WHITE-100 MESH, SSA-2
 +
| rowspan="1"| Halliburton
 +
| rowspan="1"| Proppant
 +
| Listed Below
 +
| Listed Below
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| Fresh Water
 +
| rowspan="1"| Operator
 +
| rowspan="1"| Base Fluid
 +
| Water
 +
| 7732-18-5
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 88.1818
 +
| style="text-align: right;" | 132,610,000.0
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| HAI-OS ACID INHIBITOR
 +
| rowspan="1"| Halliburton
 +
| rowspan="1"| Corrosion Inhibitor
 +
| Listed Below
 +
| Listed Below
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
|- valign="top"
 +
| rowspan="1"| Ingredients
 +
| rowspan="1"| Listed Above
 +
| rowspan="1"| Listed Above
 +
| Water
 +
| 7732-18-5
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 0.245358
 +
| style="text-align: right;" | 368976
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = FracFocus Fracking Chemicals Database
 +
| date = 2019-04-02
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-06-19 }}</ref>
 +
== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 1419210446
 
| 2014-12-16
 
 
|  
 
|  
| Pre-job safety meeting was held with all Eclipse personnel, Nomac crew, & Halliburton crew. We established circulation & washed down the last 13
 
 
|  
 
|  
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|  
 
|  
 
|  
 
|  
 
|-
 
|-
 +
| 2016-11-17
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 420130 Gal
 +
| style="text-align: right;" | 0
 +
| [[Halliburton]]
 +
| STAGE 1/45
 +
STAGES 2-44 SEE IMAGES
 +
|-
 +
| 2016-12-03
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 313300 Gal
 +
| style="text-align: right;" | 384500
 +
| [[Halliburton]]
 +
| STAGE 45/45
 +
STAGES 2-44 SEE IMAGES
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 2017
 +
| [[ECLIPSE RESOURCES I LP]]
 +
| style="text-align: right;" | 1028883
 +
| style="text-align: right;" | 121237
 +
| style="text-align: right;" | 349
 +
|-
 +
| 2018
 +
| [[ECLIPSE RESOURCES I LP]]
 +
| style="text-align: right;" | 619728
 +
| style="text-align: right;" | 28195
 +
| style="text-align: right;" | 362
 +
|-
 +
| 2019
 +
| [[ECLIPSE RESOURCES I LP]]
 +
| style="text-align: right;" | 101748
 +
| style="text-align: right;" | 3302
 +
| style="text-align: right;" | 90
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 2017
 +
| [[ECLIPSE RESOURCES I LP]]
 +
| Brine
 +
| style="text-align: right;" | 24801
 +
| style="text-align: right;" | 349
 +
|-
 +
| 2018
 +
| [[ECLIPSE RESOURCES I LP]]
 +
| Brine
 +
| style="text-align: right;" | 10649
 +
| style="text-align: right;" | 362
 +
|-
 +
| 2019
 +
| [[ECLIPSE RESOURCES I LP]]
 +
| Brine
 +
| style="text-align: right;" | 1580
 +
| style="text-align: right;" | 90
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Inspection Data ==
 +
==== Inspections Performed ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Inspection Date
 +
!scope="col" style="text-align: center"| Inspection Type
 +
!scope="col" style="text-align: center"| Inspection Result
 +
!scope="col" style="text-align: center"| Inspection Comments
 +
|-
 +
| 0138502282
 +
| 2017-02-07
 +
| Production Wells
 +
| No Violations
 +
| The well was equipped with a plunger lift system with valves in the open position. Gauges present read 3220 pounds per square inch on the casing and 3105 pounds per square inch on the tubing. Annular pressure monitoring was present along with proper identification in place. Production equipment included a sand trap, a line heater and a GP Unit. Also present 8-400 barrel tanks within containment, a horizontal heated separator, 2- vapor recovery towers, 2-compressor
 
|-
 
|-
| -953343945
+
| 0156899111
 +
| 2019-05-20
 +
| Production Wells
 +
| No Violations
 +
| The purpose of my inspection was a status check.  On 4/25/2019 inspection found two slips have developed along the access road and on the topsoil stockpile. I contacted ODNR horizontal well pad Engineer Mark Atkinson and made him aware of the problem areas. During my inspection today the slips remain but have not increased in severability. The current slips will not effect pad stability and performance.
 +
|-
 +
| 0229986434
 +
| 2016-09-21
 +
| Completion Testing
 +
| No Violations
 +
| On the day of my inspection I witnessed the Sweco tubing head installation and successful pressure testing at 10,000 pounds per square inch. Nine wireline will complete bond log on the 5.5 inch production casing upon completion of installation of FMH frac valve. I completed walk around with Consultant Cristo Giannareas revealing that secondary containment was in place with plans to begin toe prep tomorrow.
 +
|-
 +
| 0292375143
 +
| 2017-01-10
 +
| Completion Testing
 +
| No Violations
 +
| The well was equipped with a plunger lift system with valves in the closed position with annular pressure monitoring in place. Tetra Technologies was onsite setting flowback equipment with flowback to begin on Friday. Production equipment included a sand trap, a line heater and a GP Unit. Also present 8-400 barrel tanks within containment, a horizontal heated separator, 2- vapor recovery towers, 2-compressor units, a flare stack and a gas combustor all shared with the Abe Troyer 2H, 4H, 6H and 10H. I met with Consultant Cristo Giannareas and completed walk around revealing installation of production equipment was on going.
 +
|-
 +
| 0549057601
 +
| 2017-02-07
 +
| Production Wells
 +
| No Violations
 +
| The well was equipped with a plunger lift system with valves in the open position. Gauges present read 3220 pounds per square inch on the casing and 3105 pounds per square inch on the tubing. Annular pressure monitoring was present along with proper identification in place. Production equipment included a sand trap, a line heater and a GP Unit. Also present 8-400 barrel tanks within containment, a horizontal heated separator, 2- vapor recovery towers, 2-compressor
 +
|-
 +
| 0705960663
 +
| 2018-10-04
 +
| Production Wells
 +
| No Violations
 +
| The purpose of my inspection was a status check. During my inspection the well was equipped with a production tree style wellhead with valves in the open position. Annular pressure monitoring was present and evaluated. The production equipment consisted of eight 400-barrel tanks, two vapor recovery towers, five sand traps, five gas production units, one compressor, one vent scrubber, and one combustor. Identification was located on the well.
 +
|-
 +
| 0772193187
 +
| 2017-06-06
 +
| Production Wells
 +
| No Violations
 +
| The well was equipped with a plunger lift system with valves in the open position. Gauges present read 1920 pounds per square inch on the casing and 2190 pounds per square inch on the tubing. Annular pressure monitoring was present along with proper identification in place. Production equipment included a sand trap, a line heater and a GP Unit. Also present 8-400 barrel tanks within containment, a horizontal heated separator, 2- vapor recovery towers, 2-compressor units, a flare stack and a gas combustor all shared with the Abe Troyer 2H, 4H, 6H and 10H.
 +
|-
 +
| 0953343945
 
| 2015-04-09
 
| 2015-04-09
|  
+
| Preliminary Restoration
 +
| No Violations
 
| On the day of my inspection the site passed preliminary restoration according to ORC 1509.072A.
 
| On the day of my inspection the site passed preliminary restoration according to ORC 1509.072A.
|  
+
|-
|  
+
| 0992764735
|  
+
| 2018-07-10
 +
| Production Wells
 +
| No Violations
 +
| The purpose of my inspection was a status check. During my inspection the well was equipped with a production tree style wellhead with valves in the open position. Annular pressure monitoring was present. The production equipment consisted of eight 400 barrel tanks, two vapor recovery towers, five sand traps, five gas production units, one compressor, one vent scrubber, and one flare. Identification was located on the well.
 +
|-
 +
| 1128933019
 +
| 2019-04-25
 +
| Production Wells
 +
| No Violations
 +
| The purpose of my inspection was a status check. During my inspection the well was equipped with a production tree style wellhead with valves in the open position. Annular pressure monitoring was present and evaluated. The production equipment consisted of eight 400-barrel tanks, two vapor recovery towers, five sand traps, five gas production units, one compressor, one vent scrubber, and one combustor. Identification was located on the well. Upon entering the access road, a slip was noticed developing on the left side of the access road at the point of entry and an additional slip had developed on the stack pile. I made ODNR Engineer Mark Atkinson aware of my findings.
 +
|-
 +
| 1418653519
 +
| 2014-12-15
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| On the day of my inspection I witnessed that Nomac Drilling Rig #359 was drilling a 17.5 inch diameter vertical hole at a depth of 587 feet with a planned td of 1359 feet. 13.375 inch casing and cementing to follow early Tuesday morning. Site inspection revealed no violations.
 +
|-
 +
| 1419210446
 +
| 2014-12-16
 +
| Casing String Witnessed
 +
| No Violations
 +
| Pre-
 +
|-
 +
| 1479753308
 +
| 2016-11-21
 +
| Completion Testing
 +
| No Violations
 +
| On the day of my inspection I witnessed Nine Wireline was onsite to plug and perforate stage 13 of 45. Tools were pumped down with 100 barrels of produced water at 14 barrels per minute with 5600 pounds per square inch. Nine Wireline successfully set the plug at 13872 feet and perforated the casing with 36 shots from 13847 feet to 13747 feet.
 +
|-
 +
| 1526812137
 +
| 2017-09-11
 +
| Production Wells
 +
| No Violations
 +
| The well was equipped with a plunger lift system with valves in the open position. Gauges present read 1575 pounds per square inch on the casing and 1186 pounds per square inch on the tubing. Annular pressure monitoring was present along with proper identification in place. Production equipment included a sand trap, a line heater and a GP Unit. Also present 8-400 barrel tanks within containment, a horizontal heated separator, 2- vapor recovery towers, 2-compressor units, a flare stack and a gas combustor all shared with the Abe Troyer 2H, 4H, 6H and 10H.
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]
 +
[[Category:FracFocus]]

Revision as of 21:31, 30 July 2019

Well Details

Well ID: 34-059-24410
Loading map...
Country: United States
State: Ohio
County: Guernsey
Municipality: Londonderry Township
Operator Name: ECLIPSE RESOURCES I LP
Well Pad ID: US-OH-001087
Farm/Lease Name: ABE TROYER
License Status: Producing
License Date: 2014-08-08
Spud Date: 2014-09-25
Spud Drilling Contractor: NOMAC DRILLING CORP
Final Drill Date: 2014-12-27
Well Total Depth: 14953 ft
Configuration: Horizontal
Latitude: 40.084703143
Longitude: -81.26495495

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2014-08-08 Proposed Formations:POINT PLEASANT, Issued Date:8/8/2014, Expired Date:8/7/2016 12:00:00 PM, Drilling unit acres:698.607, Proposed Well Type:OG, Proposed Well Class:EDPW
Reached Total Depth 2014-12-27
Construction Permit Expires 2016-08-07
Completion Report Received 2017-05-23
Record Last Modified 2019-06-11

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2017-05-30 7993 8149 36
2017-05-30 14639 14811 48

For data sources see[3]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 11/17/2016 12/03/2016 7929 15,919,600.0 0

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 FE-1A ACIDIZING COMPOSITION Halliburton Additive Listed Below Listed Below 0 0 0
FDP-S1225-15 Halliburton Surfactant Listed Below Listed Below 0 0 0
SAND-PREMIUM WHITE-40/70 Halliburton Proppant Listed Below Listed Below 0 0 0
Crystalline silica, quartz 14808-60-7 100 11.5714 17,401,300.0
Fatty acids, tall oil Proprietary 30 0.000133659 201
Hydrochloric acid 7647-01-0 15 0.0367263 55230
Olefins Proprietary 5 0.00005453 82
Propargyl alcohol 107-19-7 10 0.00004455 67
Alcohols, C12-16, ethoxylated 68551-12-2 5 0.00002593 39
Acetic anhydride 108-24-7 100 0.0010726 1613
Glycerine 56-81-5 5 0.00002593 39
Methanol 67-56-1 60 0.000266653 401
Acetic acid 64-19-7 60 0.000649011 976
Alcohols, C12-13, ethoxylated 66455-14-9 30 0.000154938 233
Ethylene oxide 75-21-8 0.01 0.00000066 1
Reaction product of acetophenone, formaldehyde, thiourea and oleic acid in dimethyl formamide 68527-49-1 30 0.000133659 201
Ethoxylated alcohols Proprietary 30 0.000133659 201
HYDROCHLORIC ACID Halliburton Solvent Listed Below Listed Below 0 0 0
SAND-COMMON WHITE-100 MESH, SSA-2 Halliburton Proppant Listed Below Listed Below 0 0 0
Fresh Water Operator Base Fluid Water 7732-18-5 100 88.1818 132,610,000.0
HAI-OS ACID INHIBITOR Halliburton Corrosion Inhibitor Listed Below Listed Below 0 0 0
Ingredients Listed Above Listed Above Water 7732-18-5 100 0.245358 368976

For data sources see[4]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0
2016-11-17 H2O 15 420130 Gal 0 Halliburton STAGE 1/45

STAGES 2-44 SEE IMAGES

2016-12-03 H2O 15 313300 Gal 384500 Halliburton STAGE 45/45

STAGES 2-44 SEE IMAGES

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2017 ECLIPSE RESOURCES I LP 1028883 121237 349
2018 ECLIPSE RESOURCES I LP 619728 28195 362
2019 ECLIPSE RESOURCES I LP 101748 3302 90

For data sources see[6] [7]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2017 ECLIPSE RESOURCES I LP Brine 24801 349
2018 ECLIPSE RESOURCES I LP Brine 10649 362
2019 ECLIPSE RESOURCES I LP Brine 1580 90

For data sources see[8] [9]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0138502282 2017-02-07 Production Wells No Violations The well was equipped with a plunger lift system with valves in the open position. Gauges present read 3220 pounds per square inch on the casing and 3105 pounds per square inch on the tubing. Annular pressure monitoring was present along with proper identification in place. Production equipment included a sand trap, a line heater and a GP Unit. Also present 8-400 barrel tanks within containment, a horizontal heated separator, 2- vapor recovery towers, 2-compressor
0156899111 2019-05-20 Production Wells No Violations The purpose of my inspection was a status check. On 4/25/2019 inspection found two slips have developed along the access road and on the topsoil stockpile. I contacted ODNR horizontal well pad Engineer Mark Atkinson and made him aware of the problem areas. During my inspection today the slips remain but have not increased in severability. The current slips will not effect pad stability and performance.
0229986434 2016-09-21 Completion Testing No Violations On the day of my inspection I witnessed the Sweco tubing head installation and successful pressure testing at 10,000 pounds per square inch. Nine wireline will complete bond log on the 5.5 inch production casing upon completion of installation of FMH frac valve. I completed walk around with Consultant Cristo Giannareas revealing that secondary containment was in place with plans to begin toe prep tomorrow.
0292375143 2017-01-10 Completion Testing No Violations The well was equipped with a plunger lift system with valves in the closed position with annular pressure monitoring in place. Tetra Technologies was onsite setting flowback equipment with flowback to begin on Friday. Production equipment included a sand trap, a line heater and a GP Unit. Also present 8-400 barrel tanks within containment, a horizontal heated separator, 2- vapor recovery towers, 2-compressor units, a flare stack and a gas combustor all shared with the Abe Troyer 2H, 4H, 6H and 10H. I met with Consultant Cristo Giannareas and completed walk around revealing installation of production equipment was on going.
0549057601 2017-02-07 Production Wells No Violations The well was equipped with a plunger lift system with valves in the open position. Gauges present read 3220 pounds per square inch on the casing and 3105 pounds per square inch on the tubing. Annular pressure monitoring was present along with proper identification in place. Production equipment included a sand trap, a line heater and a GP Unit. Also present 8-400 barrel tanks within containment, a horizontal heated separator, 2- vapor recovery towers, 2-compressor
0705960663 2018-10-04 Production Wells No Violations The purpose of my inspection was a status check. During my inspection the well was equipped with a production tree style wellhead with valves in the open position. Annular pressure monitoring was present and evaluated. The production equipment consisted of eight 400-barrel tanks, two vapor recovery towers, five sand traps, five gas production units, one compressor, one vent scrubber, and one combustor. Identification was located on the well.
0772193187 2017-06-06 Production Wells No Violations The well was equipped with a plunger lift system with valves in the open position. Gauges present read 1920 pounds per square inch on the casing and 2190 pounds per square inch on the tubing. Annular pressure monitoring was present along with proper identification in place. Production equipment included a sand trap, a line heater and a GP Unit. Also present 8-400 barrel tanks within containment, a horizontal heated separator, 2- vapor recovery towers, 2-compressor units, a flare stack and a gas combustor all shared with the Abe Troyer 2H, 4H, 6H and 10H.
0953343945 2015-04-09 Preliminary Restoration No Violations On the day of my inspection the site passed preliminary restoration according to ORC 1509.072A.
0992764735 2018-07-10 Production Wells No Violations The purpose of my inspection was a status check. During my inspection the well was equipped with a production tree style wellhead with valves in the open position. Annular pressure monitoring was present. The production equipment consisted of eight 400 barrel tanks, two vapor recovery towers, five sand traps, five gas production units, one compressor, one vent scrubber, and one flare. Identification was located on the well.
1128933019 2019-04-25 Production Wells No Violations The purpose of my inspection was a status check. During my inspection the well was equipped with a production tree style wellhead with valves in the open position. Annular pressure monitoring was present and evaluated. The production equipment consisted of eight 400-barrel tanks, two vapor recovery towers, five sand traps, five gas production units, one compressor, one vent scrubber, and one combustor. Identification was located on the well. Upon entering the access road, a slip was noticed developing on the left side of the access road at the point of entry and an additional slip had developed on the stack pile. I made ODNR Engineer Mark Atkinson aware of my findings.
1418653519 2014-12-15 Drill / Deepen / Reopen No Violations On the day of my inspection I witnessed that Nomac Drilling Rig #359 was drilling a 17.5 inch diameter vertical hole at a depth of 587 feet with a planned td of 1359 feet. 13.375 inch casing and cementing to follow early Tuesday morning. Site inspection revealed no violations.
1419210446 2014-12-16 Casing String Witnessed No Violations Pre-
1479753308 2016-11-21 Completion Testing No Violations On the day of my inspection I witnessed Nine Wireline was onsite to plug and perforate stage 13 of 45. Tools were pumped down with 100 barrels of produced water at 14 barrels per minute with 5600 pounds per square inch. Nine Wireline successfully set the plug at 13872 feet and perforated the casing with 36 shots from 13847 feet to 13747 feet.
1526812137 2017-09-11 Production Wells No Violations The well was equipped with a plunger lift system with valves in the open position. Gauges present read 1575 pounds per square inch on the casing and 1186 pounds per square inch on the tubing. Annular pressure monitoring was present along with proper identification in place. Production equipment included a sand trap, a line heater and a GP Unit. Also present 8-400 barrel tanks within containment, a horizontal heated separator, 2- vapor recovery towers, 2-compressor units, a flare stack and a gas combustor all shared with the Abe Troyer 2H, 4H, 6H and 10H.

For data sources see[10]

References