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Difference between revisions of "34-121-24380"

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__TOC__
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__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-121-24380
 
| Well ID: 34-121-24380
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.86810534, -81.42228788 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.868033277, -81.42244684 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Noble County, Ohio|Noble]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Noble_County,_Ohio|Noble]]
 +
|-
 +
| Municipality: [[Seneca_Township,_Noble_County,_Ohio|Seneca Township]]
 
|-
 
|-
 
| Operator Name: [[ANTERO RESOURCES  CORPORATION]]
 
| Operator Name: [[ANTERO RESOURCES  CORPORATION]]
 
|-
 
|-
| Well Pad ID:  
+
| Well Pad ID: [[000520]]
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: WAYNE UNIT
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2017-06-07
 
|-
 
|-
 
| Spud Date: 2012-10-10
 
| Spud Date: 2012-10-10
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor: [[PATTERSON DRILLING]]
 +
|-
 +
| Final Drill Date: 2012-10-20
 +
|-
 +
| Well Total Depth: 327 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status:  
+
| Latitude: 39.868033277
 
|-
 
|-
| Violations: 0
+
| Longitude: -81.42244684
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| APP
 +
| 2012-09-24
 +
| Proposed Formations:POINT PLEASANT, Issued Date:9/24/2012, Expired Date:9/24/2014 12:00:00 PM, Drilling unit acres:510.98, Proposed Well Type:OG, Proposed Well Class:EDPW
 
|-
 
|-
| Latitude: 39.86810534
+
| Correction to Well
 +
| 2012-10-05
 +
| CORRECTION TO CASING PROGRAM.
 
|-
 
|-
| Longitude: -81.42228788
+
| Reached Total Depth
 +
| 2012-10-20
 +
| LOST HOLE WHILE DRILLING SURFACE
 +
|-
 +
| Plugged/Abandoned
 +
| 2012-10-26
 +
| LOST HOLE WHILE DRILLING SURFACE
 +
|-
 +
| Completion Report Received
 +
| 2012-11-29
 +
| LOST HOLE WHILE DRILLING SURFACE
 +
|-
 +
| Construction Permit Expires
 +
| 2014-09-24
 +
| LOST HOLE WHILE DRILLING SURFACE
 +
|-
 +
| Record Last Modified
 +
| 2017-06-14
 +
| LOST HOLE WHILE DRILLING SURFACE
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 +
<!--== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 +
<!--== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
+
|-
!scope="col" | VIOLATION COMMENT
+
| 0875542022
 +
| 2012-10-15
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| My inspection today finds the rig is preparing to retrieve a joint of 18.625 casing from the well bore.  The current depth is 327.
 +
|-
 +
| 0929903584
 +
| 2017-06-07
 +
| Final Restoration
 +
| No Violations
 +
| The purpose of my inspection was a status check on a final restoration. During my inspection there was no evidence of the well existing, all debris from the plugging operations had been removed. A level graded gravel surface was left in place of the plugged well. The production equipment left behind belongs to the addition five producing wells on this pad. Location meets final restoration requirements 1509.072 (B).
 
|-
 
|-
 
| 1351007501
 
| 1351007501
 
| 2012-10-23
 
| 2012-10-23
|  
+
| Drill / Deepen /  Reopen
| My inspection today finds the rig crew trying to fish the lost joint of pipe.  Previous attempts have failed.  They are continuing to try.  The pipe is now at bottom 327'
+
| No Violations
|
+
| My inspection today finds the rig crew trying to fish the lost joint of pipe.  Previous attempts have failed.  They are continuing to try.  The pipe is now at bottom 327
|
 
|
 
|-
 
 
|-
 
|-
 
| 1351030531
 
| 1351030531
 
| 2012-10-21
 
| 2012-10-21
|  
+
| Drill / Deepen /  Reopen
| Operator called and stated they were ready to run 18.625 casing went to site and rig crew ran 331' of casing but they had to wash down 10' of casing while doing so bottom joint of casing broke off and decision was made to pull casing and attempt to retrieve broken section of casing and then ream out well bore and then try and run casing again and cement it in place.
+
| No Violations
|
+
| Operator called and stated they were ready to run 18.625 casing went to site and rig crew ran 331 of casing but they had to wash down 10 of casing while doing so bottom joint of casing broke off and decision was made to pull casing and attempt to retrieve broken section of casing and then ream out well bore and then try and run casing again and cement it in place.
|
 
|
 
|-
 
 
|-
 
|-
| -2128155280
+
| 2128155280
 
| 2012-10-26
 
| 2012-10-26
|  
+
| Plug / Plug Back
| My inspection today finds the well operator Antero, has after four days of fishing for the joint of 18.625 pipe that was lost in the hole, decided to plug the well.  The total depth reached on the well was 327'.  The rig has run 315' of 2.375 tubing in the well.  Allied Oil and Gas pumped 45 bbl of cement.  The rig crew pulled 4 joints of tubing.  Allied the pumped 70 bbl of cement slurry.  The rig crew pulled 4 more joints of tubing.  The last plug was 45 bbl of cement, this brought the cement to surface.  I instructed the company man James, to cut the conductor off 30 below ground level and put a steel plate on top of the well with the permit number on it.  I also asked him to put a cover over the cellar.
+
| No Violations
|
+
| My inspection today finds the well operator Antero, has after four days of fishing for the joint of 18.625 pipe that was lost in the hole, decided to plug the well.  The total depth reached on the well was 327.  The rig has run 315 of 2.375 tubing in the well.  Allied Oil and Gas pumped 45 bbl of cement.  The rig crew pulled 4 joints of tubing.  Allied the pumped 70 bbl of cement slurry.  The rig crew pulled 4 more joints of tubing.  The last plug was 45 bbl of cement, this brought the cement to surface.  I instructed the company man James, to cut the conductor off 30 below ground level and put a steel plate on top of the well with the permit number on it.  I also asked him to put a cover over the cellar.
|
 
|
 
 
|-
 
|-
 +
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 
|-
 
|-
| -875542022
+
|}-->
| 2012-10-15
 
|
 
| My inspection today finds the rig is preparing to retrieve a joint of 18.625 casing from the well bore.  The current depth is 327'.
 
|
 
|
 
|
 
|-
 
|}
 
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 05:08, 24 July 2019

Well Details

Well ID: 34-121-24380
Loading map...
Country: United States
State: Ohio
County: Noble
Municipality: Seneca Township
Operator Name: ANTERO RESOURCES CORPORATION
Well Pad ID: 000520
Farm/Lease Name: WAYNE UNIT
License Status: Final Restoration
License Date: 2017-06-07
Spud Date: 2012-10-10
Spud Drilling Contractor: PATTERSON DRILLING
Final Drill Date: 2012-10-20
Well Total Depth: 327 ft
Configuration: Vertical
Latitude: 39.868033277
Longitude: -81.42244684

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2012-09-24 Proposed Formations:POINT PLEASANT, Issued Date:9/24/2012, Expired Date:9/24/2014 12:00:00 PM, Drilling unit acres:510.98, Proposed Well Type:OG, Proposed Well Class:EDPW
Correction to Well 2012-10-05 CORRECTION TO CASING PROGRAM.
Reached Total Depth 2012-10-20 LOST HOLE WHILE DRILLING SURFACE
Plugged/Abandoned 2012-10-26 LOST HOLE WHILE DRILLING SURFACE
Completion Report Received 2012-11-29 LOST HOLE WHILE DRILLING SURFACE
Construction Permit Expires 2014-09-24 LOST HOLE WHILE DRILLING SURFACE
Record Last Modified 2017-06-14 LOST HOLE WHILE DRILLING SURFACE

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0875542022 2012-10-15 Drill / Deepen / Reopen No Violations My inspection today finds the rig is preparing to retrieve a joint of 18.625 casing from the well bore. The current depth is 327.
0929903584 2017-06-07 Final Restoration No Violations The purpose of my inspection was a status check on a final restoration. During my inspection there was no evidence of the well existing, all debris from the plugging operations had been removed. A level graded gravel surface was left in place of the plugged well. The production equipment left behind belongs to the addition five producing wells on this pad. Location meets final restoration requirements 1509.072 (B).
1351007501 2012-10-23 Drill / Deepen / Reopen No Violations My inspection today finds the rig crew trying to fish the lost joint of pipe. Previous attempts have failed. They are continuing to try. The pipe is now at bottom 327
1351030531 2012-10-21 Drill / Deepen / Reopen No Violations Operator called and stated they were ready to run 18.625 casing went to site and rig crew ran 331 of casing but they had to wash down 10 of casing while doing so bottom joint of casing broke off and decision was made to pull casing and attempt to retrieve broken section of casing and then ream out well bore and then try and run casing again and cement it in place.
2128155280 2012-10-26 Plug / Plug Back No Violations My inspection today finds the well operator Antero, has after four days of fishing for the joint of 18.625 pipe that was lost in the hole, decided to plug the well. The total depth reached on the well was 327. The rig has run 315 of 2.375 tubing in the well. Allied Oil and Gas pumped 45 bbl of cement. The rig crew pulled 4 joints of tubing. Allied the pumped 70 bbl of cement slurry. The rig crew pulled 4 more joints of tubing. The last plug was 45 bbl of cement, this brought the cement to surface. I instructed the company man James, to cut the conductor off 30 below ground level and put a steel plate on top of the well with the permit number on it. I also asked him to put a cover over the cellar.

For data sources see[3]

References