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Difference between revisions of "34-175-20344"

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__TOC__
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__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-175-20344
 
| Well ID: 34-175-20344
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.97303403, -83.18435178 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.973123893, -83.18419735 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Wyandot County, Ohio|Wyandot]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Wyandot_County,_Ohio|Wyandot]]
 +
|-
 +
| Municipality: [[Sycamore_Township,_Wyandot_County,_Ohio|Sycamore Township]]
 
|-
 
|-
 
| Operator Name: [[NORSTAR OPERATING LLC]]
 
| Operator Name: [[NORSTAR OPERATING LLC]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: OSBORN UNIT
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2005-03-24
 
|-
 
|-
 
| Spud Date: 2005-04-01
 
| Spud Date: 2005-04-01
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor: [[PROFESSIONAL WELL SVC-PWS]]
 +
|-
 +
| Final Drill Date: 2005-04-05
 +
|-
 +
| Well Total Depth: 2391 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Final Restoration
+
| Latitude: 40.973123893
 +
|-
 +
| Longitude: -83.18419735
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| APP
 +
| 2005-03-24
 +
| Proposed Formations:TRENTON TO KNOX, Issued Date:3/24/2005, Expired Date:3/24/2006 6:00:00 AM, Drilling unit acres:347.34, Proposed Well Type:OG, Proposed Well Class:EDPW
 +
|-
 +
| Original Spud
 +
| 2005-04-01
 +
| RBDMS Rec
 +
|-
 +
| Completed
 +
| 2005-04-05
 +
| RBDMS Rec
 +
|-
 +
| Reached Total Depth
 +
| 2005-04-05
 +
| RBDMS Rec
 +
|-
 +
| Plugged/Abandoned
 +
| 2005-04-08
 +
| RBDMS Rec
 
|-
 
|-
| Violations: 0
+
| Completion Report Received
 +
| 2006-02-24
 +
| RBDMS Rec
 
|-
 
|-
| Latitude: 40.97303403
+
| Construction Permit Expires
 +
| 2006-03-24
 +
| RBDMS Rec
 
|-
 
|-
| Longitude: -83.18435178
+
| Record Last Modified
 +
| 2013-03-14
 +
| RBDMS Rec
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 +
<!--== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 +
<!--== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
+
|-
!scope="col" | VIOLATION COMMENT
+
| 0422939706
 +
| 2005-04-01
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| Set surface casing at 706 foot.
 +
|-
 +
| 0692258637
 +
| 2005-04-07
 +
| Plug / Plug Back
 +
| No Violations
 +
| Attempt to set bottom plug.  A 330 foot plug was attempted to be set from 2358 to 2028  with 88 sacks cement in a 7 inch hole using 2 inch upset tubing. During the cementing process the cement setup and locked tubing in place Free point was calculated by stretch of 40K lb with 25 of stretch at 2027 feet. Upon determination of cemented in pipe circulation of upwards of 145 bbl water to wash out cement plug. Circulation of water was maintained throughout.  Suspect channeling occurred. Reverse circulation was attempted to free pipe. Pipe would need to be shot.
 
|-
 
|-
 
| 1543376881
 
| 1543376881
 
| 2005-04-18
 
| 2005-04-18
|  
+
| Final Restoration
 +
| No Violations
 
| Inspect location. Pits filled site graded. Crop field.
 
| Inspect location. Pits filled site graded. Crop field.
|
 
|
 
|
 
 
|-
 
|-
 +
| 1553605868
 +
| 2016-11-10
 +
| Final Restoration
 +
| No Violations
 +
| Final restoration status check. P & A date 4/08/2015. No visual evidence of the well at the RBDMS well spot.
 
|-
 
|-
 
| 1587742088
 
| 1587742088
 
| 2005-03-31
 
| 2005-03-31
|  
+
| Drill / Deepen /  Reopen
 +
| No Violations
 
| Inspect Site. Drilling, conductor set at 174 feet.
 
| Inspect Site. Drilling, conductor set at 174 feet.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1953007992
 
| 1953007992
 
| 2005-04-08
 
| 2005-04-08
|  
+
| Plug / Plug Back
 +
| No Violations
 
| Plug well. Shoot pipe at second collar above calculated free point of 2037. First collar at 2037, second collar shot off at 1994. Pull up 2 to 3 feet and set 100foot plug, and subsequent plugs for closing well.
 
| Plug well. Shoot pipe at second collar above calculated free point of 2037. First collar at 2037, second collar shot off at 1994. Pull up 2 to 3 feet and set 100foot plug, and subsequent plugs for closing well.
|
 
|
 
|
 
|-
 
|-
 
| 422939706
 
| 2005-04-01
 
|
 
| Set surface casing at 706 foot.
 
|
 
|
 
|
 
 
|-
 
|-
 +
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 
|-
 
|-
| -692258637
+
|}-->
| 2005-04-07
 
|
 
| Attempt to set bottom plug.  A 330 foot plug was attempted to be set from 2358 to 2028  with 88 sacks cement in a 7 inch hole using 2 inch upset tubing. During the cementing process the cement setup and locked tubing in place Free point was calculated by stretch of 40K lb with 25 of stretch at 2027 feet. Upon determination of cemented in pipe circulation of upwards of 145 bbl water to wash out cement plug. Circulation of water was maintained throughout.  Suspect channeling occurred. Reverse circulation was attempted to free pipe. Pipe would need to be shot.
 
|
 
|
 
|
 
|-
 
|}
 
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 17:59, 30 July 2019

Well Details

Well ID: 34-175-20344
Loading map...
Country: United States
State: Ohio
County: Wyandot
Municipality: Sycamore Township
Operator Name: NORSTAR OPERATING LLC
Well Pad ID:
Farm/Lease Name: OSBORN UNIT
License Status: Final Restoration
License Date: 2005-03-24
Spud Date: 2005-04-01
Spud Drilling Contractor: PROFESSIONAL WELL SVC-PWS
Final Drill Date: 2005-04-05
Well Total Depth: 2391 ft
Configuration: Vertical
Latitude: 40.973123893
Longitude: -83.18419735

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2005-03-24 Proposed Formations:TRENTON TO KNOX, Issued Date:3/24/2005, Expired Date:3/24/2006 6:00:00 AM, Drilling unit acres:347.34, Proposed Well Type:OG, Proposed Well Class:EDPW
Original Spud 2005-04-01 RBDMS Rec
Completed 2005-04-05 RBDMS Rec
Reached Total Depth 2005-04-05 RBDMS Rec
Plugged/Abandoned 2005-04-08 RBDMS Rec
Completion Report Received 2006-02-24 RBDMS Rec
Construction Permit Expires 2006-03-24 RBDMS Rec
Record Last Modified 2013-03-14 RBDMS Rec

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0422939706 2005-04-01 Drill / Deepen / Reopen No Violations Set surface casing at 706 foot.
0692258637 2005-04-07 Plug / Plug Back No Violations Attempt to set bottom plug. A 330 foot plug was attempted to be set from 2358 to 2028 with 88 sacks cement in a 7 inch hole using 2 inch upset tubing. During the cementing process the cement setup and locked tubing in place Free point was calculated by stretch of 40K lb with 25 of stretch at 2027 feet. Upon determination of cemented in pipe circulation of upwards of 145 bbl water to wash out cement plug. Circulation of water was maintained throughout. Suspect channeling occurred. Reverse circulation was attempted to free pipe. Pipe would need to be shot.
1543376881 2005-04-18 Final Restoration No Violations Inspect location. Pits filled site graded. Crop field.
1553605868 2016-11-10 Final Restoration No Violations Final restoration status check. P & A date 4/08/2015. No visual evidence of the well at the RBDMS well spot.
1587742088 2005-03-31 Drill / Deepen / Reopen No Violations Inspect Site. Drilling, conductor set at 174 feet.
1953007992 2005-04-08 Plug / Plug Back No Violations Plug well. Shoot pipe at second collar above calculated free point of 2037. First collar at 2037, second collar shot off at 1994. Pull up 2 to 3 feet and set 100foot plug, and subsequent plugs for closing well.

For data sources see[3]

References