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| License Status: Producing | | License Status: Producing | ||
|- | |- | ||
− | | License Date: | + | | License Date: 1992-11-08 |
|- | |- | ||
| Spud Date: 1992-11-13 | | Spud Date: 1992-11-13 |
Well ID: 34-029-21558 | Loading map...
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Country: United States | |
State: Ohio | |
County: Columbiana | |
Municipality: Wayne Township | |
Operator Name: EVERFLOW EASTERN PTNS L P | |
Well Pad ID: | |
Farm/Lease Name: TAYANITA | |
License Status: Producing | |
License Date: 1992-11-08 | |
Spud Date: 1992-11-13 | |
Spud Drilling Contractor: MOHAWK DRLG | |
Final Drill Date: 1992-11-15 | |
Well Total Depth: 1208 ft | |
Configuration: Vertical | |
Latitude: 40.677634579 | |
Longitude: -80.82957142 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1992-11-08 | 84 EVERFLOW EASTERN PTNS L P GeoDate 11/8/92 |
Oil and Gas | 1992-11-08 | Issued Date 11/9/92 Expired Date 11/9/93 Acres 0160000 Tool Type RTAF Proposed Formation BEREA Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1992-11-13 | |
Completed | 1992-11-15 | |
Reached Total Depth | 1992-11-15 | |
Construction Permit Expires | 1993-11-09 | |
Record Last Modified | 2019-06-10 |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2017 | EVERFLOW EASTERN PTNS L P | 0 | 0 | 0 |
2018 | EVERFLOW EASTERN PTNS L P | 0 | 0 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2017 | EVERFLOW EASTERN PTNS L P | Brine | 0 | 0 |
2018 | EVERFLOW EASTERN PTNS L P | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0000001992 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 9/28/93 INSPECTOR BRETT FARNSWORTH DATE 09/2819/93 DATA FROM OLD VAX INFO | |
0112931211 | 2018-03-16 | Production Wells | No Violations | The purpose of my inspection was to document the status of well #2-1558. No direct access to the well was present. The well location remained stable. A locked chain link fence enclosure was present around the well head with mature trees growing through the enclosure. Correct identification was present. The 8.625 well head contained a swage with a valve that was plugged. No leaks were observed. No production equipment was on location. |
0226776539 | 2018-05-24 | Production Wells | No Violations | The purpose of my inspection was to document the current status of well #2-1558. At the time of my inspection, no direct access was present to the well head. The well was enclosed within a locked chain link enclosure with mature trees growing through the top of the enclosure. Correct identification was present on the fence. The surface casing contained a swage and a closed valve that was plugged. No leaks were observed. I photographed the location at the request of ODNR-DOGRM Attorney Brendan Inscho who was finalizing a Chiefs Order to plug the well. |
1320287848 | 2017-11-30 | Production Wells | No Violations | The purpose of my inspection was to conduct a status check on well #2-1558. The operator has reported zero (0) production in the last two years. Access to the well was off of the township road through woodlands. No direct access to the well head was present. The well location was stable. A locked, chain-link fence enclosure remained around the well. Trees were growing through the roof of the enclosure. The production casing contained a swage with a closed and plugged valve. No leaks were observed. No production equipment was present. No identification was present. I called and spoke with Everflow Eastern field manager George Strawn concerning the status of the well. Mr. Strawn was not familiar with the well and requested time to investigate the well with the office. I will plan to follow up with Mr. Strawn regarding the status of well #2-1558. |
1431626729 | 2015-05-06 | Production Wells | No Violations | |
1512410013 | 2017-12-04 | Production Wells | No Violations | The purpose of my inspection was to conduct a status check on well #2-1558. No direct access to the well was present. I made a trail through woodlands to locate the well head. The well location was stable. A locked chain-link fence enclosure was constructed around the well. Trees were growing through the top of the fenced enclosure. No identification was present. The 8.625 well casing was equipped with a swage that was topped with a closed and plugged valve. No leaks were observed. I called and spoke with Everflow Eastern field manager George Strawn concerning the well. Mr. Strawn was unfamiliar with the well and stated that he would discuss the situation with the office and communicate back with the status of well #2-1558. |
1528457548 | 2018-06-08 | Production Wells | No Violations | The purpose of my inspection was to document the status of well #2-1558. No direct access to the well was present. The well location remained stable. A locked chain link fence enclosure was present around the well head with mature trees growing through the enclosure. Correct identification was present. The 8.625 well head contained a swage with a valve that was closed and plugged. No leaks were observed. No production equipment was on location. The completion record on file indicated total drilling depth was reached on 11/15/1992. ODNR-DOGRM has no documentation that the well was ever completed. The well owner has not reported production from 1992 through 2016. The well owner reported zero (0) production in 2017. The well is currently incapable of production and Everflow Eastern /Partners LP shall submit a written plugging schedule to Inspector Kenneth Frye at the Ohio Department of Natural /Resources, Division of Oil and Gas Resources Management, 3575 Forest Lake Drive, Suite 150, Uniontown, OH 44685, within 30 days, per OAC 1501:9-11-05(B), and plug the well within 180 days. Everflow Eastern Partners LP will be notified if the plugging schedule is approved or denied. |
For data sources see[7]