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| County: [[Mahoning_County,_Ohio|Mahoning]] | | County: [[Mahoning_County,_Ohio|Mahoning]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Austintown Township,_Mahoning_County,_Ohio|Austintown Township]] |
|- | |- | ||
| Operator Name: [[EVERFLOW EASTERN PTNS L P]] | | Operator Name: [[EVERFLOW EASTERN PTNS L P]] |
Well ID: 34-099-22190 | Loading map...
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Country: United States | |
State: Ohio | |
County: Mahoning | |
Municipality: Austintown Township | |
Operator Name: EVERFLOW EASTERN PTNS L P | |
Well Pad ID: | |
Farm/Lease Name: KARNDFEL UNIT | |
License Status: Producing | |
License Date: 1987-10-21 | |
Spud Date: 1987-12-01 | |
Spud Drilling Contractor: [[JL COATS [COATS-GOFF]]] | |
Final Drill Date: 1987-12-07 | |
Well Total Depth: 5320 ft | |
Configuration: Vertical | |
Latitude: 41.063401688 | |
Longitude: -80.78571471 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1987-10-21 | Issued Date 10/21/87 Expired Date 10/20/88 Acres 0095160 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05320 Proposed Drill Depth 05320 |
Original Spud | 1987-12-01 | |
Completed | 1987-12-07 | |
Reached Total Depth | 1987-12-07 | |
CO | 1987-12-11 | 84 EVERFLOW EASTERN PTNS L P GeoDate 10/21/87 |
Completion Report Received | 1987-12-23 | |
Construction Permit Expires | 1988-10-20 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5065 | 5186 | 0 |
2006-09-11 | 5078 | 5138 | 31 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 101230 Gal | 65000 | FRAC: H2O,SAND42 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
000PL12619 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
1487102730 | 2017-02-09 | Production Wells | No Violations | I received a call at 10:19 AM from the Austintown Fire Department ( 330-799-8502 ) . They had received a call from a person walking the Mill Creek Hike and Bike about and odor and a sheen of oil inside the tank battery at the above location. Terry Whitehair Northeast Emergency Response Supervisor an myself responded to the call. I called George Stramm from Everflow Eastern and he explained to me that they had discovered a small leak (pen hole) at the 3 fitting at the bottom of the tank. He also had his field foreman Kevin Dow to respond also. The tank at that time had 26 25.8 bbls of fluid. The fluid was removed and the tank was laid over on its side until they can get into the location to remove it. The access road is the property owners yard at this time. There is a dike constructed around the tank battery. The dike had some water and some frozen ice. They will notify me when they remove it. There is a Complaint Status Report # 5529 on this incident |
1547491008 | 2019-01-14 | Production Wells | No Violations | I was on location to perform an inspection on this well and tank battery regarding complaint #5529. A call was received by the Austintown Fire Dept. on 2/8/17 from a hiker who had been walking on the Mill Creek Hike and Bike Trail. The Austintown Fire Dept. Chief said the hiker had seen an oil sheen inside the containment of the dike as the company had been disassembling the tank. The tank was removed by Strawn Oilfield and the site remediated of the oil sheen. A new 50bbl tank has been set in the dike with the existing horizontal separator. The tank battery contains proper identification. The well is a producing plunger lift well with the 8.625 casing plumber to the surface with no violations. The tank battery has been reclaimed and the new production equipment installed. At this time the complaint can be closed. |
For data sources see[9]