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| County: [[Portage_County,_Ohio|Portage]] | | County: [[Portage_County,_Ohio|Portage]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Hiram Township,_Portage_County,_Ohio|Hiram Township]] |
|- | |- | ||
| Operator Name: [[EQUITY OIL & GAS FUNDS INC]] | | Operator Name: [[EQUITY OIL & GAS FUNDS INC]] |
Well ID: 34-133-20815 | Loading map...
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Country: United States | |
State: Ohio | |
County: Portage | |
Municipality: Hiram Township | |
Operator Name: EQUITY OIL & GAS FUNDS INC | |
Well Pad ID: | |
Farm/Lease Name: CARLISLE HM | |
License Status: Producing | |
License Date: 1976-05-18 | |
Spud Date: 1976-09-21 | |
Spud Drilling Contractor: | |
Final Drill Date: 1976-09-30 | |
Well Total Depth: 4300 ft | |
Configuration: Vertical | |
Latitude: 41.289140884 | |
Longitude: -81.11974860 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1976-05-18 | 9 EDC GeoDate 5/18/76 |
Original Spud | 1976-09-21 | |
Completed | 1976-09-30 | |
Reached Total Depth | 1976-09-30 | |
Change of Owner | 2007-06-13 | Operator changed from 9, POWER GAS MARKETING & TRANS to 1171, EQUITY OIL & GAS FUNDS IN |
Record Last Modified | 2019-06-04 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4170 | 4220 | 75 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 60000 Gal | 80000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0759365754 | 2004-03-25 | Production Wells | Violations Noted | The 210 bbl stock tank is leaking and needs to be replaced. The impacted soil inside of the dike area needs to be removed and disposed. The tank battery also needs the required identification. |
1010534360 | 2011-08-25 | Production Wells | No Violations | I performed a follow-up inspection on this tank battery. The new ID sign is posted. The flame arrester, ground wire installed, and the enardo valve installed. This complaint is resolved. |
1016755408 | 2004-12-08 | Production Wells | Violations Noted | No corrective action has occurred. Replace the 210 bbl tank and remove and dispose of the imapcted soil in the tank battery. |
1314095168 | 2011-08-22 | Production Wells | No Violations | Complaint number 3284. I received a call from the Uniontown office about a lightening strike complaint. I called Ms. Sue Pence(330-425-8472ext 236). She stated that she wanted the tank battery moved. I investigated the incident. I met Don Toth,Pumper(330-478-2156) about the lightening strike. Less than 1 quart of oil was spilled. The stock tank did not blow out but the top and the bottom were swelled out. The new 210 barrel tank was already in place. I discussed with Don the possibility of going to a smaller tank like a 140 barrel tank. He stated that both wells, permit #s 814,815 go into this tank battery and both wells make a large amount of water. I agreed to keep the 210 barrel tank in place. The stock tank will have installed a flame arrester, a ground wire and a anardo valve. The installation of the tank will be done by tomorrow. A new ID sign will be posted on the stock tank. I called Ms. Sue Pence back and left her a message about what I had found at the site. This complaint continues. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0759365754 | US-OH-128639 | 2004-04-08 | Well operation causing pollution and contamination | |
0759365754 | US-OH-128640 | 2004-04-08 | Failure to legibly identify well | |
1016755408 | US-OH-100090 | 2004-04-08 | Well operation causing pollution and contamination | |
1016755408 | US-OH-100091 | 2004-04-08 | Failure to legibly identify well |
For data sources see[9]