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Difference between revisions of "34-031-22184"

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| County: [[Coshocton_County,_Ohio|Coshocton]]
 
| County: [[Coshocton_County,_Ohio|Coshocton]]
 
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| Municipality: [[Crawford Township,_Coshocton_County,_Ohio|Crawford Township]]
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| Municipality: [[Crawford_Township,_Coshocton_County,_Ohio|Crawford Township]]
 
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| Operator Name: [[BETHEL RESOURCES INC]]
 
| Operator Name: [[BETHEL RESOURCES INC]]
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| Configuration: Vertical
 
| Configuration: Vertical
 
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| Latitude: <Latitude>
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| Latitude: 40.377818812
 
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|-
 
| Longitude: -81.76321150
 
| Longitude: -81.76321150

Revision as of 00:45, 30 August 2019

Well Details

Well ID: 34-031-22184
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Country: United States
State: Ohio
County: Coshocton
Municipality: Crawford Township
Operator Name: BETHEL RESOURCES INC
Well Pad ID:
Farm/Lease Name: SHROYER JAMES J
License Status: Orphan Well - Pending
License Date: 1973-05-30
Spud Date: 1973-06-01
Spud Drilling Contractor:
Final Drill Date: 1973-07-02
Well Total Depth: 998 ft
Configuration: Vertical
Latitude: 40.377818812
Longitude: -81.76321150

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1801-01-02 55 BETHEL RESOURCES INC
Original Spud 1973-06-01

-ALE 06/22/2016

Completed 1973-07-02

-ALE 06/22/2016

Reached Total Depth 1973-07-02

-ALE 06/22/2016

Completion Report Received 1975-09-01

-ALE 06/22/2016

Correction to Well 2008-07-18 ADDED THE FOLLOWING TO THE DATABASE: FOOTAGE= 680'NL & 1790'WL OF SW QTR., SEC. 23 (SCALED); X= 2,205,284; Y= 259,955; ELEV= 820' AND NEW BEDFORD QUAD.
Changed to Orphan Well Pending 2019-03-25 Changed Well To Orphan Pending
Record Last Modified 2019-03-25

-ALE 06/22/2016

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
Not Treated 0 0 0

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0538879446 2016-05-19 Orphan No Violations On the day of my inspection I accompanied orphan well inspector Jeff Fry to the well site, where we took updated photographs and assessed the site for potential access routes to the well. Jeff also gathered data on the casing size and current state of the well.
0964427879 2003-10-14 Production Wells No Violations Well is idle , No lead line hooked up to well head , Well is equipped with 7 casing , 7 swedge . There is a new land owner for property . Bill Seal is new owner . 52811 co rd 227 Fresno Oh 43824 . Phone # 740-545-7837 . Said he would like well plugged , right of entry was no problem .
1461082567 2016-04-19 Orphan No Violations This inspection was conducted in response to a request to confirm the status or existence of this well. On the day of my inspection I found that the well was equipped with 8.625 conductor casing and 7 surface casing. The surface casing was open. There was a swage loosely set on top, but not screwed on. When I removed the swage I found that the casing was filled with an oily sludge to within 3 feet of the surface. There was active bubbling from the sludge. I did not get a strong gas odor, but it was windy. There was no oil or water visibly leaking from the well and there was no impacted soil or vegetation around the well. The well was 30 feet from a run-off stream that cuts through the property. There was a water well on the property that was 190 feet from the oil and gas well. I met with the landowner Mark Cutshall. He claimed that he has lived in the home since 2006 and he has never had any problems with the well leaking. He also claimed that his water well was showing no signs of being affected by the abandoned well. The records indicate that this well was referred to the orphan well program in 2003 by inspector Rocky King. The records also indicate that the well was capped after drilling and never produced.

For data sources see[4]

References