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| State: Ohio | | State: Ohio | ||
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− | | County: | + | | County: [[Washington_County,_Ohio|Washington]] |
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Grandview_Township,_Washington_County,_Ohio|Grandview Township]] |
|- | |- | ||
| Operator Name: [[PD VALENTINE OIL & GAS LLC]] | | Operator Name: [[PD VALENTINE OIL & GAS LLC]] |
Well ID: 34-167-61774 | Loading map...
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Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Grandview Township | |
Operator Name: PD VALENTINE OIL & GAS LLC | |
Well Pad ID: | |
Farm/Lease Name: MYERS WH | |
License Status: Producing | |
License Date: | |
Spud Date: | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: 1700 ft | |
Configuration: Vertical | |
Latitude: 39.509246238 | |
Longitude: -81.10825077 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Change of Owner | 2018-12-19 | Operator changed from 6151, P & D VALENTINE OIL CO to 10284, P D VALENTINE OIL & GAS LLC |
Record Last Modified | 2018-12-19 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 0 | 30 Qts | 0 | |||
ACID | 0 | 20 Qts | 0 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1998 | P & D VALENTINE OIL CO | 15 | 0 | 365 |
1999 | P & D VALENTINE OIL CO | 18 | 0 | 365 |
2000 | P & D VALENTINE OIL CO | 10 | 0 | 365 |
2001 | P & D VALENTINE OIL CO | 0 | 0 | 365 |
2005 | P & D VALENTINE OIL CO | 20 | 0 | 0 |
2007 | P & D VALENTINE OIL CO | 30 | 10 | 0 |
2012 | P & D VALENTINE OIL CO | 100 | 0 | 366 |
2013 | P & D VALENTINE OIL CO | 20 | 0 | 365 |
2014 | P & D VALENTINE OIL CO | 200 | 0 | 300 |
2015 | P & D VALENTINE OIL CO | 335 | 0 | 365 |
2016 | P & D VALENTINE OIL CO | 512 | 0 | 366 |
2017 | P & D VALENTINE OIL CO | 369 | 0 | 365 |
2018 | P & D VALENTINE OIL CO | 77 | 0 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1998 | P & D VALENTINE OIL CO | Brine | 0 | 365 |
1999 | P & D VALENTINE OIL CO | Brine | 0 | 365 |
2000 | P & D VALENTINE OIL CO | Brine | 0 | 365 |
2001 | P & D VALENTINE OIL CO | Brine | 0 | 365 |
2005 | P & D VALENTINE OIL CO | Brine | 0 | 0 |
2007 | P & D VALENTINE OIL CO | Brine | 0 | 0 |
2012 | P & D VALENTINE OIL CO | Brine | 0 | 366 |
2013 | P & D VALENTINE OIL CO | Brine | 0 | 365 |
2014 | P & D VALENTINE OIL CO | Brine | 0 | 300 |
2015 | P & D VALENTINE OIL CO | Brine | 0 | 365 |
2016 | P & D VALENTINE OIL CO | Brine | 0 | 366 |
2017 | P & D VALENTINE OIL CO | Brine | 0 | 365 |
2018 | P & D VALENTINE OIL CO | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
1014428007 | 2018-03-29 | Production Wells | No Violations | This well was issued a violation on 07/22/14 by Inspector Lynn Parkins for failure to legibly identify well, no SPCC dike/or failure to keep dike free of water or oil, and statement of annual production not filed. The inspection this day revealed that this well is equipped with a pumping unit, 6 5/8 inch diameter production casing, and production tubing. The valves are open on the wellhead for production and legible identification is posted at the well. The 80 barrel production tank has had the contaminated soil removed and the tank has a proper dike built around it. Production in RBDMS is up to date for this well for 2016. The well is in production and all compliances have been resolved. |
1219734765 | 2015-03-17 | Production Wells | No Violations | Upon inspection, it was observed that this well is still being serviced. There is a new gasoline powered pumping unit standing over 6.625 surface casing, 2 tubing, and 1 tubing on a gas escape packer. There is a black plastic line extending approximately 30 from the well head with oil/paraffin sludge around the end of it and on the ground around it from cleaning the well out with solvent. I spoke with Mr. Paul Valentine and instructed him to clean up the oily sludge and agreed. Mr. Valentine stated that production records for the entire lease have been submitted to the Division. Since the records have yet to show up on RBDMS, I instructed Mr. Valentine to mail the records to the ODNR DOGRM Zanesville Office so they can be scanned into the system. |
1345178029 | 2014-09-03 | Production Wells | No Violations | Upon inspection, it was observed that this well is equipped for production. New identification information has been posted at the well head. I spoke with Mr. Paul Valentine in person, and he stated that he is in the process of acquiring pumping units for all the wells on the property. Mr. Valentine also stated that current production records for all wells on this property will be submitted this month. |
1406142843 | 2014-07-22 | Production Wells | Violations Noted | Performed an inspection on this well in response to a landowner complaint. Upon inspection , it was observed that this well is equipped for gas production only. The well consists of 6.625 casing with a gas escape packer with 2 production tubing and rods. There is no line attached to the fitting on the 2 tubing. There is a 1 poly line attached to the 1 gas escape tubing feeding into a nearby gathering line. The scissor jack pumping unit is still in place and the polish rod is very corroded. The central power unit for the shackle line system is not operational. The 100 bbl production tank for this well is full and has spilled over. The spill appears to have happened some time ago and there is oily sludge around the tank bottom extending approx. 10 away from the tank toward Sheets Run, a nearby creek. There is no dike built around the tank. The tank will have to be pumped down, oily sludge must be removed, and a dike must be built to SPCC standards. Photos were taken of the location to support these findings. There is no identification information posted at the well or production tank. According to RBDMS production records, this well produced 100 mcf of gas in 2012. No production records were submitted for 2013. P&D Valentine Oil Co. will have 14 days upon receipt of this notice to fix these issues and bring the well into compliance. |
1407521290 | 2014-08-08 | Production Wells | No Violations | Upon inspection, it was observed that no changes have been made to this well location. I spoke with Mr. Paul Valentine in person and he stated that he is in the process of making new ID tags for all the wells on this lease. Mr. Valentine also stated that updated production records will be submitted for all of the wells on this lease. The production tank which had overflowed is still full of fluid and the oily sludge is still present on the ground surrounding the tank. I instructed Mr. Valentine to pump the tank down and clean up the contaminated area as soon as possible. Mr. Valentine agreed to take prompt action on bringing this well into compliance. |
1819710585 | 2015-10-05 | Production Wells | No Violations | Upon inspection, it was observed that this well is now in production of oil. There is now a pumping unit standing over 6.625 casing, 2 tubing with rods, and 1 gas escape tubing. Mr. Paul Valentine pumped the well at the time of inspection and fluid could be heard flowing into the production tank. The gas escape tubing will be tapped into the sales line once enough fluid is pumped off the well to allow sufficient gas pressure to return. Legible and correct ID information is posted at the well. The 80 bbl production tank has yet to have a dike built around it, and there is still oily soil around the base of it. Mr. Valentine stated he would address these issues this week and call me to re-inspect once it is done. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1406142843 | US-OH-111961 | 2014-07-24 | Failure to legibly identify well | |
1406142843 | US-OH-111962 | 2014-07-24 | No SPCC dike/or failure to keep dike free of water or oil | |
1406142843 | US-OH-111963 | 2014-07-24 | Statement of annual production not filed |
For data sources see[8]