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Difference between revisions of "34-175-20344"

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| State: Ohio
 
| State: Ohio
 
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| County: <County>
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| County: [[Wyandot_County,_Ohio|Wyandot]]
 
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| Municipality: [[Sycamore Township,_Wyandot_County,_Ohio|Sycamore Township]]
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| Municipality: [[Sycamore_Township,_Wyandot_County,_Ohio|Sycamore Township]]
 
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| Operator Name: [[NORSTAR OPERATING LLC]]
 
| Operator Name: [[NORSTAR OPERATING LLC]]

Revision as of 23:31, 31 August 2019

Well Details

Well ID: 34-175-20344
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Country: United States
State: Ohio
County: Wyandot
Municipality: Sycamore Township
Operator Name: NORSTAR OPERATING LLC
Well Pad ID:
Farm/Lease Name: OSBORN UNIT
License Status: Final Restoration
License Date: 2005-03-24
Spud Date: 2005-04-01
Spud Drilling Contractor: PROFESSIONAL WELL SVC-PWS
Final Drill Date: 2005-04-05
Well Total Depth: 2391 ft
Configuration: Vertical
Latitude: 40.973123893
Longitude: -83.18419735

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2005-03-24 Proposed Formations:TRENTON TO KNOX, Issued Date:3/24/2005, Expired Date:3/24/2006 6:00:00 AM, Drilling unit acres:347.34, Proposed Well Type:OG, Proposed Well Class:EDPW
Original Spud 2005-04-01 RBDMS Rec
Completed 2005-04-05 RBDMS Rec
Reached Total Depth 2005-04-05 RBDMS Rec
Plugged/Abandoned 2005-04-08 RBDMS Rec
Completion Report Received 2006-02-24 RBDMS Rec
Construction Permit Expires 2006-03-24 RBDMS Rec
Record Last Modified 2013-03-14 RBDMS Rec

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0422939706 2005-04-01 Drill / Deepen / Reopen No Violations Set surface casing at 706 foot.
0692258637 2005-04-07 Plug / Plug Back No Violations Attempt to set bottom plug. A 330 foot plug was attempted to be set from 2358 to 2028 with 88 sacks cement in a 7 inch hole using 2 inch upset tubing. During the cementing process the cement setup and locked tubing in place Free point was calculated by stretch of 40K lb with 25 of stretch at 2027 feet. Upon determination of cemented in pipe circulation of upwards of 145 bbl water to wash out cement plug. Circulation of water was maintained throughout. Suspect channeling occurred. Reverse circulation was attempted to free pipe. Pipe would need to be shot.
1543376881 2005-04-18 Final Restoration No Violations Inspect location. Pits filled site graded. Crop field.
1553605868 2016-11-10 Final Restoration No Violations Final restoration status check. P & A date 4/08/2015. No visual evidence of the well at the RBDMS well spot.
1587742088 2005-03-31 Drill / Deepen / Reopen No Violations Inspect Site. Drilling, conductor set at 174 feet.
1953007992 2005-04-08 Plug / Plug Back No Violations Plug well. Shoot pipe at second collar above calculated free point of 2037. First collar at 2037, second collar shot off at 1994. Pull up 2 to 3 feet and set 100foot plug, and subsequent plugs for closing well.

For data sources see[3]

References