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Difference between revisions of "34-175-20349"

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| State: Ohio
 
| State: Ohio
 
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| County: <County>
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| County: [[Wyandot_County,_Ohio|Wyandot]]
 
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| Municipality: [[Tymochtee Township,_Wyandot_County,_Ohio|Tymochtee Township]]
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| Municipality: [[Tymochtee_Township,_Wyandot_County,_Ohio|Tymochtee Township]]
 
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| Operator Name: [[NORSTAR OPERATING LLC]]
 
| Operator Name: [[NORSTAR OPERATING LLC]]

Revision as of 23:32, 31 August 2019

Well Details

Well ID: 34-175-20349
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Country: United States
State: Ohio
County: Wyandot
Municipality: Tymochtee Township
Operator Name: NORSTAR OPERATING LLC
Well Pad ID:
Farm/Lease Name: KESSLER
License Status: Final Restoration
License Date: 2015-10-21
Spud Date: 2005-11-14
Spud Drilling Contractor: BOB HUWER DRLG
Final Drill Date: 2005-11-24
Well Total Depth:
Configuration: Vertical
Latitude: 40.906541932
Longitude: -83.23372857

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2005-09-01 Proposed Formations:TRENTON-BLACK RIVER, Issued Date:9/1/2005, Expired Date:9/1/2006 6:00:00 AM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:EDPW
Original Spud 2005-11-14 DRY PER WCR.TO BE P&A
Completed 2005-11-24 DRY PER WCR.TO BE P&A
Reached Total Depth 2005-11-24 DRY PER WCR.TO BE P&A
Completion Report Received 2007-03-19 DRY PER WCR.TO BE P&A
APP 2015-10-21 Proposed Formations:BLACK RIVER, Issued Date:10/21/2015, Expired Date:10/20/2017 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2016-10-11 DRY PER WCR.TO BE P&A
Record Last Modified 2016-12-06 DRY PER WCR.TO BE P&A
Construction Permit Expires 2017-10-20 DRY PER WCR.TO BE P&A

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
Not Treated 0 0 0 OPEN HOLE, NOT TREATED

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2006 NORSTAR OPERATING LLC 0 0 0
2008 NORSTAR OPERATING LLC 0 0 0
2009 NORSTAR OPERATING LLC 0 0 0
2010 NORSTAR OPERATING LLC 0 0 0
2011 NORSTAR OPERATING LLC 0 0 0
2012 NORSTAR OPERATING LLC 0 0 0
2013 NORSTAR OPERATING LLC 0 0 0
2014 NORSTAR OPERATING LLC 0 0 0
2015 NORSTAR OPERATING LLC 0 0 0
2016 NORSTAR OPERATING LLC 0 0 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2006 NORSTAR OPERATING LLC Brine 0 0
2008 NORSTAR OPERATING LLC Brine 0 0
2009 NORSTAR OPERATING LLC Brine 0 0
2010 NORSTAR OPERATING LLC Brine 0 0
2011 NORSTAR OPERATING LLC Brine 0 0
2012 NORSTAR OPERATING LLC Brine 0 0
2013 NORSTAR OPERATING LLC Brine 0 0
2014 NORSTAR OPERATING LLC Brine 0 0
2015 NORSTAR OPERATING LLC Brine 0 0
2016 NORSTAR OPERATING LLC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0028170167 2016-01-14 Production Wells No Violations No change-in-status from previous inspection. All valves closed and no leaks noted.
0039637036 2015-09-17 Production Wells No Violations Inspected the Kessler #1 (#349) as part of a standard Chiefs Order (#2015-145) follow-up. Status: no change-in-status from previous inspection the well is currently in corn.
0085888230 2006-09-11 Preliminary Restoration No Violations preliminary restoration completed.
0108877018 2014-09-04 Production Wells Violations Noted This inspection was done as a follow-up to Compliance Notice #1354812080 written on 12-6-2012. At the time of the inspection . The well has no access lane and is in a soybean field so no visual inspection could be done at this time. The operator, Norstar Operating LLC, would like to sell the well but has been unable to do so. The well has not been put into production and the well needs to be plugged.
0217527535 2005-11-14 Drill / Deepen / Reopen No Violations Rig setup on hole.
0378071426 2016-05-24 Production Wells No Violations No change-in-status from previous inspection. The field has not been planted.
0461317062 2014-10-31 Production Wells No Violations Location Information for the Kessler #1-34 (#349). WELL HEAD: Lat. 40.90663 Long. -83.23367 / CENTER-OF-STORAGE: none / ENTRANCE: Lat. 40.90603 Long. -83.23328.
0481290349 2016-10-31 Final Restoration No Violations All equipment used for plugging has been removed from location. The farmer has plowed through the location. Status: final restoration complete.
0810783440 2016-10-11 Plug / Plug Back No Violations Ogg Brothers ready mix truck #20 on location. Huwer hooked up and displaced 40 sacks of Class A cement for the bottom-of-surface plug through 2.875 inch tubing. Huwer lay down tubing, hook up and displace 30 sacks Class A cement for the top-of-surface plug, which held. Plug down 10:58 am. Plugging operations co-witnessed by Mr. Bob and Aaron Huwer. **The Kessler #1-34 (#349) is officially plugged and abandoned.**
0825543332 2005-11-16 Drill / Deepen / Reopen No Violations Set Sruface casing.
0972653697 2017-05-31 Final Restoration No Violations Inspected the Kessler #1 as part of a standard final restoration status check. Status: ok, corn has established through the well location, final restoration complete.
1022636556 2016-09-15 Plug / Plug Back No Violations OGG concrete cement truck delivered 40 sacks of Class A ready mix cement to location which was pumped away by Huwer Well Service through 2.875 inch tubing set at 1620 feet. Bottom hole plug down: 9:56 am. Huwer lay down tubing, rigged down and moved off location for another job.
1046175594 2016-10-05 Plug / Plug Back No Violations Jet wireline run in hole, found cement top at approximately 922 feet and shot off 4.5 inch casing at 870 feet. Rig down and move off location.
1324863225 2015-04-30 Administrative Inspection No Violations Chiefs order #2015-145 Plugging Required issued 4/10/2015.
1330625629 2015-12-15 Administrative Inspection No Violations Plug permit issued 10/21/2015. expires 10/20/2017.
1354812080 2012-12-05 Production Wells Violations Noted Inspect well. well shut in. No identification posted. There is 4.25 inch production casing and well head; 2.875 inch tubing. No production equipment, no tanks. Well incapable of production. Completion reports has not been submitted. Production reports have not been submitted since 2006. Plug well.
1361550935 2012-12-05 Production Wells Violations Noted FOLLOW UP TO NOV # 1354812080 Inspect well. well shut in. No identification posted. There is 4.25 inch production casing and well head; 2.875 inch tubing. No production equipment, no tanks. Well incapable of production. Completion reports has not been submitted. Production reports have not been submitted since 2006. Plug well.
1410540003 2014-09-12 Production Wells No Violations Inspected the Kessler #1 (#349) as a standard compliance action follow up. Status: unable to reach well as it is in mature crops. Will continue to monitor.
1415023353 2014-10-31 Production Wells No Violations Inspected the Kessler #1-34 (#349) as part of a standard compliance action follow up. Recent harvest has provided access to the well head. There is no access road, storage, pump jack or identification. The well is shut-in as per previous inspections. Status: non-compliant for plug and/or produce. Photo documented and obtained GPS coordinates.
1476715684 2016-10-12 Final Restoration No Violations The operator has cut off the casing 4 feet below grade, identified the well with a brazed cap and buried the well and graded the well site which is in cropland. The tubing is on a trailer off to the side of the location by the barn.
1487882052 2016-09-08 Production Wells No Violations Bob Huwer Well Service is on the well for plugging, tubing set, no one working today.
1564697128 2015-04-30 Production Wells No Violations Inspected the Kessler #1 (#349) as part of a standard compliance action follow up. Status: no change-in-status from previous inspection.
1857541622 2016-10-05 Production Wells No Violations On site with inspector Eric Daugstrup witnessing the process of separating and removing production string.
1913420254 2006-02-27 Production Wells No Violations Inspect location. Pits open. Pipe run in place. Shut in.
1971186769 2015-06-18 Administrative Inspection No Violations Inspected the Kessler #1 (#349) as part of a standard Chiefs Order (#2015-145) follow-up. Status: no change-in-status from previous inspection, non-compliant.
2076025878 2007-04-24 Production Wells No Violations Inspect well. Well completed, shut in. Pits open. Restoration incomplete.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0108877018 US-OH-102042 2014-09-12 Well shall be plugged
1354812080 US-OH-110264 2012-12-06 Failure to legibly identify well
1354812080 US-OH-110265 2012-12-06 Well shall be plugged
1354812080 US-OH-110266 2012-12-06 Statement of annual production not filed
1361550935 US-OH-110368 2019-01-17 NONE Well shall be plugged

For data sources see[8]

References