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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-121-24380 | | Well ID: 34-121-24380 | ||
− | | style="height=100%; align=center" rowspan="17" | {{#display_map: 39. | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 39.86, -81.42 | width=100% | height=100% }} |
|- | |- | ||
| Country: United States | | Country: United States | ||
Line 29: | Line 29: | ||
| Final Drill Date: 2012-10-20 | | Final Drill Date: 2012-10-20 | ||
|- | |- | ||
− | | Well Total Depth: 327 ft | + | | Well Total Depth: 327.00 ft |
|- | |- | ||
| Configuration: Vertical | | Configuration: Vertical | ||
|- | |- | ||
− | | Latitude: 39. | + | | Latitude: 39.860000 |
|- | |- | ||
− | | Longitude: -81. | + | | Longitude: -81.420000 |
|} | |} | ||
For data sources see<ref>{{cite web | For data sources see<ref>{{cite web | ||
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | ||
|publisher = [[Ohio Department of Natural Resources]] | |publisher = [[Ohio Department of Natural Resources]] | ||
− | | date = | + | | date = 2020-11-16 |
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
== Well History == | == Well History == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 81: | Line 81: | ||
| title = Risk Based Data Management System - Well and WellHistry Tables | | title = Risk Based Data Management System - Well and WellHistry Tables | ||
|publisher = [[Ohio Department of Natural Resources]] | |publisher = [[Ohio Department of Natural Resources]] | ||
− | | date = | + | | date = 2020-11-16 |
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
<!--== Perforation Treatments == | <!--== Perforation Treatments == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 153: | Line 153: | ||
!scope="col" style="text-align: center"| Inspection Result | !scope="col" style="text-align: center"| Inspection Result | ||
!scope="col" style="text-align: center"| Inspection Comments | !scope="col" style="text-align: center"| Inspection Comments | ||
+ | |- | ||
+ | | -2128155280 | ||
+ | | 2012-10-26 0:00 | ||
+ | | PB | ||
+ | | No Violations | ||
+ | | 6.00 | ||
+ | |- | ||
+ | | -875542022 | ||
+ | | 2012-10-15 0:00 | ||
+ | | DD | ||
+ | | No Violations | ||
+ | | 2.00 | ||
|- | |- | ||
| 0875542022 | | 0875542022 | ||
Line 183: | Line 195: | ||
| No Violations | | No Violations | ||
| My inspection today finds the well operator Antero, has after four days of fishing for the joint of 18.625 pipe that was lost in the hole, decided to plug the well. The total depth reached on the well was 327. The rig has run 315 of 2.375 tubing in the well. Allied Oil and Gas pumped 45 bbl of cement. The rig crew pulled 4 joints of tubing. Allied the pumped 70 bbl of cement slurry. The rig crew pulled 4 more joints of tubing. The last plug was 45 bbl of cement, this brought the cement to surface. I instructed the company man James, to cut the conductor off 30 below ground level and put a steel plate on top of the well with the permit number on it. I also asked him to put a cover over the cellar. | | My inspection today finds the well operator Antero, has after four days of fishing for the joint of 18.625 pipe that was lost in the hole, decided to plug the well. The total depth reached on the well was 327. The rig has run 315 of 2.375 tubing in the well. Allied Oil and Gas pumped 45 bbl of cement. The rig crew pulled 4 joints of tubing. Allied the pumped 70 bbl of cement slurry. The rig crew pulled 4 more joints of tubing. The last plug was 45 bbl of cement, this brought the cement to surface. I instructed the company man James, to cut the conductor off 30 below ground level and put a steel plate on top of the well with the permit number on it. I also asked him to put a cover over the cellar. | ||
+ | |- | ||
+ | | 929903584 | ||
+ | | 2017-6-7 0:00:0 | ||
+ | | FR | ||
+ | | No Violations | ||
+ | | 1.00 | ||
|- | |- | ||
|} | |} | ||
Line 197: | Line 215: | ||
| title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables | | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables | ||
|publisher = [[Ohio Department of Natural Resources]] | |publisher = [[Ohio Department of Natural Resources]] | ||
− | | date = | + | | date = 2020-11-16 |
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
==References== | ==References== | ||
<references/> | <references/> | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Ohio Wells]] | [[Category:Ohio Wells]] |
Well ID: 34-121-24380 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Seneca Township | |
Operator Name: ANTERO RESOURCES CORPORATION | |
Well Pad ID: US-OH-000520 | |
Farm/Lease Name: WAYNE UNIT | |
License Status: Final Restoration | |
License Date: 2012-09-24 | |
Spud Date: 2012-10-10 | |
Spud Drilling Contractor: PATTERSON DRILLING | |
Final Drill Date: 2012-10-20 | |
Well Total Depth: 327.00 ft | |
Configuration: Vertical | |
Latitude: 39.860000 | |
Longitude: -81.420000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2012-09-24 | Proposed Formations:POINT PLEASANT, Issued Date:9/24/2012, Expired Date:9/24/2014 12:00:00 PM, Drilling unit acres:510.98, Proposed Well Type:OG, Proposed Well Class:EDPW |
Correction to Well | 2012-10-05 | CORRECTION TO CASING PROGRAM. |
Reached Total Depth | 2012-10-20 | LOST HOLE WHILE DRILLING SURFACE |
Plugged/Abandoned | 2012-10-26 | LOST HOLE WHILE DRILLING SURFACE |
Completion Report Received | 2012-11-29 | LOST HOLE WHILE DRILLING SURFACE |
Construction Permit Expires | 2014-09-24 | LOST HOLE WHILE DRILLING SURFACE |
Record Last Modified | 2017-06-14 | LOST HOLE WHILE DRILLING SURFACE |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-2128155280 | 2012-10-26 0:00 | PB | No Violations | 6.00 |
-875542022 | 2012-10-15 0:00 | DD | No Violations | 2.00 |
0875542022 | 2012-10-15 | Drill / Deepen / Reopen | No Violations | My inspection today finds the rig is preparing to retrieve a joint of 18.625 casing from the well bore. The current depth is 327. |
0929903584 | 2017-06-07 | Final Restoration | No Violations | The purpose of my inspection was a status check on a final restoration. During my inspection there was no evidence of the well existing, all debris from the plugging operations had been removed. A level graded gravel surface was left in place of the plugged well. The production equipment left behind belongs to the addition five producing wells on this pad. Location meets final restoration requirements 1509.072 (B). |
1351007501 | 2012-10-23 | Drill / Deepen / Reopen | No Violations | My inspection today finds the rig crew trying to fish the lost joint of pipe. Previous attempts have failed. They are continuing to try. The pipe is now at bottom 327 |
1351030531 | 2012-10-21 | Drill / Deepen / Reopen | No Violations | Operator called and stated they were ready to run 18.625 casing went to site and rig crew ran 331 of casing but they had to wash down 10 of casing while doing so bottom joint of casing broke off and decision was made to pull casing and attempt to retrieve broken section of casing and then ream out well bore and then try and run casing again and cement it in place. |
2128155280 | 2012-10-26 | Plug / Plug Back | No Violations | My inspection today finds the well operator Antero, has after four days of fishing for the joint of 18.625 pipe that was lost in the hole, decided to plug the well. The total depth reached on the well was 327. The rig has run 315 of 2.375 tubing in the well. Allied Oil and Gas pumped 45 bbl of cement. The rig crew pulled 4 joints of tubing. Allied the pumped 70 bbl of cement slurry. The rig crew pulled 4 more joints of tubing. The last plug was 45 bbl of cement, this brought the cement to surface. I instructed the company man James, to cut the conductor off 30 below ground level and put a steel plate on top of the well with the permit number on it. I also asked him to put a cover over the cellar. |
929903584 | 2017-6-7 0:00:0 | FR | No Violations | 1.00 |
For data sources see[3]