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Difference between revisions of "34-105-21580"

m
 
m
Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-105-21580
 
| Well ID: 34-105-21580
 +
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.01579142, -81.98705875 | width=100% | height=100% }}
 
|-
 
|-
| County:
+
| County: [[Meigs County, Ohio|Meigs]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[PROGRESSIVE OIL & GAS]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
| Spud Date:
+
| Spud Date: 1974-11-28
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing:
+
| Well Status: Producing
 
|-
 
|-
| Violations:
+
| Violations: 0
 
|-
 
|-
| Latitude:
+
| Latitude: 39.01579142
 
|-
 
|-
| Longitude:
+
| Longitude: -81.98705875
 
|-
 
|-
 
|}
 
|}
Line 42: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
|}
 
== Waste Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | TYPE
 
!scope="col" | QUANTITY
 
!scope="col" | UNITS
 
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | INSPECTION ID
 
!scope="col" | DATE
 
!scope="col" | DESCRIPTION
 
!scope="col" | COMMENT
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION_COMMENT
 
 
|-
 
|-
| -1203716503
+
| 1988-0
| 2007-10-22
+
| style="text-align:right;" | 0.0
|
+
|  
| Spoke with Junior Merkle regarding the status of the well.  He plans on putting the well into production, which is next on his schedule.
+
|  
|
+
|  
|
+
| style="text-align:right;" | 0.0
|
+
|  
 
|-
 
|-
 
|-
 
|-
| -1385348692
+
| 1989-0
| 2013-12-11
+
| style="text-align:right;" | 0.0
|
+
|  
| Follow up to -512939495.  Rods and tubing on a rack next to the well. well not in production. No lines or equipment at well.
+
|  
|
+
|  
|
+
| style="text-align:right;" | 0.0
|
+
|  
 
|-
 
|-
 
|-
 
|-
| -1471841176
+
| 1990-0
| 2012-02-02
+
| style="text-align:right;" | 0.0
|
+
|  
| NOV follow up. The pumping unit is still disconnected and still has no power supply. The production records still show no production recorded.
+
|  
|
+
|  
|
+
| style="text-align:right;" | 0.0
|
+
|  
 
|-
 
|-
 
|-
 
|-
| -1692843040
+
| 1991-0
| 2007-09-24
+
| style="text-align:right;" | 0.0
|
+
|  
| No action has been taken to repair the well.
+
|  
|
+
|  
|
+
| style="text-align:right;" | 0.0
|
+
|  
 
|-
 
|-
 
|-
 
|-
| -1750563137
+
| 1993-0
| 2012-03-22
+
| style="text-align:right;" | 206.0
|
+
|  
| Well not set up for annular disposal. Water being stored in 100 Bbl tanks.
+
|  
|
+
|  
|
+
| style="text-align:right;" | 0.0
|
+
|  
 
|-
 
|-
 
|-
 
|-
| -303490300
+
| 1994-0
| 2013-06-06
+
| style="text-align:right;" | 233.0
|
+
|  
| Follow up to -512939495.  Rods and tubing on a rack next to the well. well not in production. No lines or equipment at well.
+
|  
|
+
|  
|
+
| style="text-align:right;" | 0.0
|
+
|  
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
 +
| accessdate = 2015-06-20 }}</ref>
 +
== Inspection Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | INSPECTION ID
 +
!scope="col" | DATE
 +
!scope="col" | DESCRIPTION
 +
!scope="col" | COMMENT
 +
!scope="col" | VIOLATION ID
 +
!scope="col" | VIOLATION CODE
 +
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
| -431824855
+
| 1159282664
| 2008-02-25
+
| 2006-09-06
|
+
|  
| The well remains incapable of productionThe service rig was still on the well.
+
| According to Junior Merckle, the well needs drilled out with a rigDue to the circumstances, a two month extension was given.
|
+
|  
|
+
|  
|
+
| Compliance Notice
 
|-
 
|-
 
|-
 
|-
| -512939495
+
| 1159282664
| 2011-10-25
+
| 2006-09-06
|
+
|  
| Upon inspection well appeared idle, but capable of production all equipment was on well. No records have been filled since 1994. Valve on tubing open and will allow oil and or gas to escape from well. Well shall be plugged, produced, or put into temporary inactive status. Submit production to Division from years 1994 to 2010.
+
| According to Junior Merckle, the well needs drilled out with a rig. Due to the circumstances, a two month extension was given.
|
+
|  
| 9-9-05(A)1
+
|  
|
+
| Compliance Notice
 
|-
 
|-
 
|-
 
|-
| -512939495
+
| 1159282664
| 2011-10-25
+
| 2006-09-06
|
+
|  
| Upon inspection well appeared idle, but capable of production all equipment was on well. No records have been filled since 1994. Valve on tubing open and will allow oil and or gas to escape from well. Well shall be plugged, produced, or put into temporary inactive status. Submit production to Division from years 1994 to 2010.
+
| According to Junior Merckle, the well needs drilled out with a rig. Due to the circumstances, a two month extension was given.
|
+
|  
| NONEC
+
|  
|
+
| Compliance Notice
 
|-
 
|-
 
|-
 
|-
| -515721213
+
| 1159282664
| 2001-10-03
+
| 2006-09-06
|
+
|  
| FOLLOW UP TO NOV #  1269i413  An inspection revealed well is incapable of producing , 3" tubing open with 2" tubing on rack. No production lines hooked up to well and no means of producing well at this time.
+
| According to Junior Merckle, the well needs drilled out with a rig. Due to the circumstances, a two month extension was given.
|
+
|  
| NONE E
+
|  
|
+
| Compliance Notice
 
|-
 
|-
 
|-
 
|-
| -684925931
+
| 1159282664
| 2006-12-12
+
| 2006-09-06
|
+
|  
| No action taken since last inspection.
+
| According to Junior Merckle, the well needs drilled out with a rigDue to the circumstances, a two month extension was given.
|
+
|  
|
+
|  
|
+
| Compliance Notice
|-
 
|-
 
| -737400936
 
| 2013-01-07
 
|
 
| Follow up to -512939495. The well is incapable of production so is not leaking gas. No production records have been submitted to the division as of yet. The attempt to bring the well into production last year was unsuccessful. Rods and tubing on a rack next to the well.
 
|
 
|
 
|
 
|-
 
|-
 
| -814346187
 
| 2006-10-23
 
|
 
| A tank and mud pump were moved on location.
 
|
 
|
 
|
 
|-
 
|-
 
| -8280590
 
| 2007-08-23
 
|
 
| Spoke with Mike Merkle regarding the company's plans for the well.  He claimed that the well had production potential and planed to repair it as soon as possible.
 
|
 
|
 
|
 
|-
 
|-
 
| -833893413
 
| 2006-08-09
 
|
 
| No action was taken to remedy the violation.
 
|
 
|
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 1159282664
 
| 1159282664
 
| 2006-09-06
 
| 2006-09-06
|
+
|  
 
| According to Junior Merckle, the well needs drilled out with a rig.  Due to the circumstances, a two month extension was given.
 
| According to Junior Merckle, the well needs drilled out with a rig.  Due to the circumstances, a two month extension was given.
|
+
|  
|
+
|  
|
+
| Compliance Notice
 
|-
 
|-
 
|-
 
|-
 
| 1187625855
 
| 1187625855
 
| 2007-08-15
 
| 2007-08-15
|
+
|  
 
| The well remains incapable of production.
 
| The well remains incapable of production.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1203716503
 +
| 2007-10-22
 +
|
 +
| Spoke with Junior Merkle regarding the status of the well.  He plans on putting the well into production, which is next on his schedule.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 1222747845
 
| 1222747845
 
| 2005-12-08
 
| 2005-12-08
|
+
|  
 
| The well was not equipped for annular disposal.
 
| The well was not equipped for annular disposal.
|
+
|  
| NONE E
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1269i1049
 
| 1269i1049
 
| 2002-05-16
 
| 2002-05-16
|
+
|  
 
| Follow-up on NOV, In-Compliance.                      Ted Dobbins also on inspection.
 
| Follow-up on NOV, In-Compliance.                      Ted Dobbins also on inspection.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1269i413
 
| 1269i413
 
| 2001-10-03
 
| 2001-10-03
|
+
|  
| An inspection revealed well is incapable of producing , 3" tubing open with 2" tubing on rack. No production lines hooked up to well and no means of producing well at this time.
+
| An inspection revealed well is incapable of producing , 3 tubing open with 2 tubing on rack. No production lines hooked up to well and no means of producing well at this time.
|
+
|  
| NONE E
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1329422493
 
| 1329422493
 
| 2012-02-16
 
| 2012-02-16
|
+
|  
 
| I spoke with Junior Merkle of Progressive Oil and we discussed bringing the well into compliance. I granted him an extension to bring in a service rig to swab out the well. Due to the topography he will need dry ground to get the rig on site.
 
| I spoke with Junior Merkle of Progressive Oil and we discussed bringing the well into compliance. I granted him an extension to bring in a service rig to swab out the well. Due to the topography he will need dry ground to get the rig on site.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1335900345
 
| 1335900345
 
| 2012-05-01
 
| 2012-05-01
|
+
|  
 
| Spoke with Mr. Merkle of Progressive Oil, he will be moving the rig onto the site after he is finished working on the current well he is working on.
 
| Spoke with Mr. Merkle of Progressive Oil, he will be moving the rig onto the site after he is finished working on the current well he is working on.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1336421560
 
| 1336421560
 
| 2012-05-07
 
| 2012-05-07
|
+
|  
 
| Well unproductive in past because squeeze job left cement inside casing 30 feet above perfs. Pulling rods today. Will be moving drilling rig onto site to drill out cement and bring well into production.
 
| Well unproductive in past because squeeze job left cement inside casing 30 feet above perfs. Pulling rods today. Will be moving drilling rig onto site to drill out cement and bring well into production.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1385348692
 +
| 2013-12-11
 +
|
 +
| Follow up to -512939495.  Rods and tubing on a rack next to the well. well not in production. No lines or equipment at well.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 1393596152
 
| 1393596152
 
| 2014-02-28
 
| 2014-02-28
|
+
|  
 
| Follow up to -512939495.  Rods and tubing on a rack next to the well. well not in production. No lines or equipment at well.
 
| Follow up to -512939495.  Rods and tubing on a rack next to the well. well not in production. No lines or equipment at well.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1471841176
 +
| 2012-02-02
 +
|
 +
| NOV follow up. The pumping unit is still disconnected and still has no power supply. The production records still show no production recorded.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 1501121088
 
| 1501121088
 
| 2006-05-09
 
| 2006-05-09
|
+
|  
 
| The well was shut-in and disconnected.  There was tubing in the well and there were rods and tubing stacked on site.
 
| The well was shut-in and disconnected.  There was tubing in the well and there were rods and tubing stacked on site.
|
+
|  
| NONE
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1503204262
 
| 1503204262
 
| 2012-05-16
 
| 2012-05-16
|
+
|  
| Unable to pull 2 7/8" casing. Plan to bring mud pump next week to clean hole.
+
| Unable to pull 2 7/8 casing. Plan to bring mud pump next week to clean hole.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| 1567921763
 +
| 2015-04-28
 +
|
 +
| Follow up to -512939495.  Rods and tubing on a rack next to the well. Well not in production. No lines or equipment at well. The well is incapable of production.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -1692843040
 +
| 2007-09-24
 +
|
 +
| No action has been taken to repair the well.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -1750563137
 +
| 2012-03-22
 +
|
 +
| Well not set up for annular disposal. Water being stored in 100 Bbl tanks.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 18060535
 
| 18060535
 
| 2007-07-19
 
| 2007-07-19
|
+
|  
 
| The well remains incapable of production.
 
| The well remains incapable of production.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -303490300
 +
| 2013-06-06
 +
|
 +
| Follow up to -512939495.  Rods and tubing on a rack next to the well. well not in production. No lines or equipment at well.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 322375772
 
| 322375772
 
| 2005-12-08
 
| 2005-12-08
|
+
|  
 
| FOLLOW UP TO NOV #  1222747845 The well was not equipped for annular disposal.
 
| FOLLOW UP TO NOV #  1222747845 The well was not equipped for annular disposal.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -431824855
 +
| 2008-02-25
 +
|
 +
| The well remains incapable of production.  The service rig was still on the well.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 459276978
 
| 459276978
 
| 2013-08-20
 
| 2013-08-20
|
+
|  
 
| Follow up to -512939495. Well idle, no euipment or lines at well. tubing on rack at well site.
 
| Follow up to -512939495. Well idle, no euipment or lines at well. tubing on rack at well site.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -512939495
 +
| 2011-10-25
 +
|
 +
| Upon inspection well appeared idle, but capable of production all equipment was on well. No records have been filled since 1994. Valve on tubing open and will allow oil and or gas to escape from well. Well shall be plugged, produced, or put into temporary inactive status. Submit production to Division from years 1994 to 2010.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -515721213
 +
| 2001-10-03
 +
|
 +
| FOLLOW UP TO NOV #  1269i413  An inspection revealed well is incapable of producing , 3 tubing open with 2 tubing on rack. No production lines hooked up to well and no means of producing well at this time.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -684925931
 +
| 2006-12-12
 +
|
 +
| No action taken since last inspection.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 736100651
 
| 736100651
 
| 2012-05-10
 
| 2012-05-10
|
+
|  
| Tubing has been pulled. Plan to go back into to drill out the cement Monday 5/14/12. Well logs show the Berea Sandstone from 1655'-1668' was perforated with 28 shots from 1650'-1660'. A leak had developed in the 4.5", so a squeeze job was performed to isolate the area. The well has been unable to produce since the squeeze job because cement was found inside the 4.5" thirty feet above the perfs  in the Berea. This is the cement Mr. merle wants to drill out. 2 7/8" tubing will be run back into well on a packer below the Salt Sand and serve as casing. 1.5" will be run inside that for tubing.
+
| Tubing has been pulled. Plan to go back into to drill out the cement Monday 5/14/12. Well logs show the Berea Sandstone from 1655'-1668' was perforated with 28 shots from 1650'-1660'. A leak had developed in the 4.5, so a squeeze job was performed to isolate the area. The well has been unable to produce since the squeeze job because cement was found inside the 4.5 thirty feet above the perfs  in the Berea. This is the cement Mr. merle wants to drill out. 2 7/8 tubing will be run back into well on a packer below the Salt Sand and serve as casing. 1.5 will be run inside that for tubing.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -737400936
 +
| 2013-01-07
 +
|
 +
| Follow up to -512939495. The well is incapable of production so is not leaking gas. No production  records have been submitted to the division as of yet. The attempt to bring the well into production last year was unsuccessful. Rods and tubing on a rack next to the well.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -814346187
 +
| 2006-10-23
 +
|
 +
| A tank and mud pump were moved on location.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -8280590
 +
| 2007-08-23
 +
|
 +
| Spoke with Mike Merkle regarding the company's plans for the well.  He claimed that the well had production potential and planed to repair it as soon as possible.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -833893413
 +
| 2006-08-09
 +
|
 +
| No action was taken to remedy the violation.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 886929353
 
| 886929353
 
| 2008-01-14
 
| 2008-01-14
|
+
|  
 
| Service rig was still on the well.  No apparent action taken since last inspection.
 
| Service rig was still on the well.  No apparent action taken since last inspection.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 11:03, 14 July 2015

Well Details

Well ID: 34-105-21580
Loading map...
County: Meigs
Municipality:
Operator Name: PROGRESSIVE OIL & GAS
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1974-11-28
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.01579142
Longitude: -81.98705875

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1988-0 0.0 0.0
1989-0 0.0 0.0
1990-0 0.0 0.0
1991-0 0.0 0.0
1993-0 206.0 0.0
1994-0 233.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1159282664 2006-09-06 According to Junior Merckle, the well needs drilled out with a rig. Due to the circumstances, a two month extension was given. Compliance Notice
1159282664 2006-09-06 According to Junior Merckle, the well needs drilled out with a rig. Due to the circumstances, a two month extension was given. Compliance Notice
1159282664 2006-09-06 According to Junior Merckle, the well needs drilled out with a rig. Due to the circumstances, a two month extension was given. Compliance Notice
1159282664 2006-09-06 According to Junior Merckle, the well needs drilled out with a rig. Due to the circumstances, a two month extension was given. Compliance Notice
1159282664 2006-09-06 According to Junior Merckle, the well needs drilled out with a rig. Due to the circumstances, a two month extension was given. Compliance Notice
1159282664 2006-09-06 According to Junior Merckle, the well needs drilled out with a rig. Due to the circumstances, a two month extension was given. Compliance Notice
1187625855 2007-08-15 The well remains incapable of production.
-1203716503 2007-10-22 Spoke with Junior Merkle regarding the status of the well. He plans on putting the well into production, which is next on his schedule.
1222747845 2005-12-08 The well was not equipped for annular disposal.
1269i1049 2002-05-16 Follow-up on NOV, In-Compliance. Ted Dobbins also on inspection.
1269i413 2001-10-03 An inspection revealed well is incapable of producing , 3 tubing open with 2 tubing on rack. No production lines hooked up to well and no means of producing well at this time.
1329422493 2012-02-16 I spoke with Junior Merkle of Progressive Oil and we discussed bringing the well into compliance. I granted him an extension to bring in a service rig to swab out the well. Due to the topography he will need dry ground to get the rig on site.
1335900345 2012-05-01 Spoke with Mr. Merkle of Progressive Oil, he will be moving the rig onto the site after he is finished working on the current well he is working on.
1336421560 2012-05-07 Well unproductive in past because squeeze job left cement inside casing 30 feet above perfs. Pulling rods today. Will be moving drilling rig onto site to drill out cement and bring well into production.
-1385348692 2013-12-11 Follow up to -512939495. Rods and tubing on a rack next to the well. well not in production. No lines or equipment at well.
1393596152 2014-02-28 Follow up to -512939495. Rods and tubing on a rack next to the well. well not in production. No lines or equipment at well.
-1471841176 2012-02-02 NOV follow up. The pumping unit is still disconnected and still has no power supply. The production records still show no production recorded.
1501121088 2006-05-09 The well was shut-in and disconnected. There was tubing in the well and there were rods and tubing stacked on site.
1503204262 2012-05-16 Unable to pull 2 7/8 casing. Plan to bring mud pump next week to clean hole.
1567921763 2015-04-28 Follow up to -512939495. Rods and tubing on a rack next to the well. Well not in production. No lines or equipment at well. The well is incapable of production.
-1692843040 2007-09-24 No action has been taken to repair the well.
-1750563137 2012-03-22 Well not set up for annular disposal. Water being stored in 100 Bbl tanks.
18060535 2007-07-19 The well remains incapable of production.
-303490300 2013-06-06 Follow up to -512939495. Rods and tubing on a rack next to the well. well not in production. No lines or equipment at well.
322375772 2005-12-08 FOLLOW UP TO NOV # 1222747845 The well was not equipped for annular disposal.
-431824855 2008-02-25 The well remains incapable of production. The service rig was still on the well.
459276978 2013-08-20 Follow up to -512939495. Well idle, no euipment or lines at well. tubing on rack at well site.
-512939495 2011-10-25 Upon inspection well appeared idle, but capable of production all equipment was on well. No records have been filled since 1994. Valve on tubing open and will allow oil and or gas to escape from well. Well shall be plugged, produced, or put into temporary inactive status. Submit production to Division from years 1994 to 2010.
-515721213 2001-10-03 FOLLOW UP TO NOV # 1269i413 An inspection revealed well is incapable of producing , 3 tubing open with 2 tubing on rack. No production lines hooked up to well and no means of producing well at this time.
-684925931 2006-12-12 No action taken since last inspection.
736100651 2012-05-10 Tubing has been pulled. Plan to go back into to drill out the cement Monday 5/14/12. Well logs show the Berea Sandstone from 1655'-1668' was perforated with 28 shots from 1650'-1660'. A leak had developed in the 4.5, so a squeeze job was performed to isolate the area. The well has been unable to produce since the squeeze job because cement was found inside the 4.5 thirty feet above the perfs in the Berea. This is the cement Mr. merle wants to drill out. 2 7/8 tubing will be run back into well on a packer below the Salt Sand and serve as casing. 1.5 will be run inside that for tubing.
-737400936 2013-01-07 Follow up to -512939495. The well is incapable of production so is not leaking gas. No production records have been submitted to the division as of yet. The attempt to bring the well into production last year was unsuccessful. Rods and tubing on a rack next to the well.
-814346187 2006-10-23 A tank and mud pump were moved on location.
-8280590 2007-08-23 Spoke with Mike Merkle regarding the company's plans for the well. He claimed that the well had production potential and planed to repair it as soon as possible.
-833893413 2006-08-09 No action was taken to remedy the violation.
886929353 2008-01-14 Service rig was still on the well. No apparent action taken since last inspection.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.