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Difference between revisions of "34-081-61062"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-081-61062
 
| Well ID: 34-081-61062
 +
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.50765086, -80.6912731 | width=100% | height=100% }}
 
|-
 
|-
| County:
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| County: [[Jefferson County, Ohio|Jefferson]]
 
|-
 
|-
| Municipality:
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| Municipality:  
 
|-
 
|-
| Operator Name:
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| Operator Name: [[FIRSTENERGY GENERATION LLC]]
 
|-
 
|-
| Well Pad ID:
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| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
| Spud Date:
+
| Spud Date:  
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
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| Configuration: Vertical
 
|-
 
|-
| Producing:
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| Well Status: Final Restoration
 
|-
 
|-
| Violations:
+
| Violations: 0
 
|-
 
|-
| Latitude:
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| Latitude: 40.50765086
 
|-
 
|-
| Longitude:
+
| Longitude: -80.6912731
 
|-
 
|-
|}
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | GAS QUANTITY
 
!scope="col" | GAS PRODUCTION DAYS
 
!scope="col" | CONDENSATE QUANTITY
 
!scope="col" | CONDENSATE PRODUCTION DAYS
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
|}
 
== Waste Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | TYPE
 
!scope="col" | QUANTITY
 
!scope="col" | UNITS
 
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
 
|}
 
|}
 
== Inspection Data ==
 
== Inspection Data ==
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!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 +
|-
 +
| 1030951423
 +
| 2013-10-24
 +
|
 +
| I was on location for this well. The well was logged by Appalachian Services and shot off the 6.625 casing 200' down hole where free pipe was shown. 2 3/8 tubing was going to be run into 502' but the hole bridged off around 180'. We had to pull out of the hole, and put a cut collar on the tubing to allow us to wash it down. We had to pump on the hole for sometime before we circulated out the bridge. We were able to run down to 502' and set a 150 sack surface cement plug.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 1678127553
 +
| 2015-03-18
 +
|
 +
| On the date of inspection I am accompanied by SE Regional Manager Brent Bear to inspect the plugged and abandoned well for Final Restoration. The well passes Final Restoration per ORC 1509.072(B).
 +
|
 +
|
 +
|
 +
|-
 
|-
 
|-
 
| -874968115
 
| -874968115
 
| 2013-10-23
 
| 2013-10-23
|
+
|  
| I was on location with Inspector Lowdur to witness the pulling of the 2" tubing and the setting of the first cement plug. There was a delay in pulling the tubing as the rods parted inside the tubing and had to be cut off with each joint. A 145 sack cement plug was set and will checked tomorrow.
+
| I was on location with Inspector Lowdur to witness the pulling of the 2 tubing and the setting of the first cement plug. There was a delay in pulling the tubing as the rods parted inside the tubing and had to be cut off with each joint. A 145 sack cement plug was set and will checked tomorrow.
|
+
|  
|
+
|  
|
+
|  
|-
 
|-
 
| 1030951423
 
| 2013-10-24
 
|
 
| I was on location for this well. The well was logged by Appalachian Services and shot off the 6.625" casing 200' down hole where free pipe was shown. 2 3/8" tubing was going to be run into 502' but the hole bridged off around 180'. We had to pull out of the hole, and put a cut collar on the tubing to allow us to wash it down. We had to pump on the hole for sometime before we circulated out the bridge. We were able to run down to 502' and set a 150 sack surface cement plug.
 
|
 
|
 
|
 
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 12:11, 14 July 2015

Well Details

Well ID: 34-081-61062
Loading map...
County: Jefferson
Municipality:
Operator Name: FIRSTENERGY GENERATION LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 40.50765086
Longitude: -80.6912731

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1030951423 2013-10-24 I was on location for this well. The well was logged by Appalachian Services and shot off the 6.625 casing 200' down hole where free pipe was shown. 2 3/8 tubing was going to be run into 502' but the hole bridged off around 180'. We had to pull out of the hole, and put a cut collar on the tubing to allow us to wash it down. We had to pump on the hole for sometime before we circulated out the bridge. We were able to run down to 502' and set a 150 sack surface cement plug.
1678127553 2015-03-18 On the date of inspection I am accompanied by SE Regional Manager Brent Bear to inspect the plugged and abandoned well for Final Restoration. The well passes Final Restoration per ORC 1509.072(B).
-874968115 2013-10-23 I was on location with Inspector Lowdur to witness the pulling of the 2 tubing and the setting of the first cement plug. There was a delay in pulling the tubing as the rods parted inside the tubing and had to be cut off with each joint. A 145 sack cement plug was set and will checked tomorrow.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.