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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-167-29445 | | Well ID: 34-167-29445 | ||
− | | style="height=100%; align=center" rowspan="15" | {{#display_map: 39. | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 39.42992595, -81.51130419 | width=100% | height=100% }} |
|- | |- | ||
− | | County: | + | | County: [[Washington County, Ohio|Washington]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[HEINRICH ENT INC/WASHINGTON OP]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
| Spud Date: 1999-12-23 | | Spud Date: 1999-12-23 | ||
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | Producing | + | | Well Status: Producing |
|- | |- | ||
| Violations: 0 | | Violations: 0 | ||
|- | |- | ||
− | | Latitude: 39. | + | | Latitude: 39.42992595 |
|- | |- | ||
− | | Longitude: -81. | + | | Longitude: -81.51130419 |
|- | |- | ||
|} | |} | ||
Line 43: | Line 43: | ||
!scope="col" | OIL QUANTITY | !scope="col" | OIL QUANTITY | ||
!scope="col" | OIL PRODUCTION DAYS | !scope="col" | OIL PRODUCTION DAYS | ||
+ | |- | ||
+ | | 1999-0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2000-0 | ||
+ | | style="text-align:right;" | 25698.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 65.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2001-0 | ||
+ | | style="text-align:right;" | 12004.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2002-0 | ||
+ | | style="text-align:right;" | 10938.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 27.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2003-0 | ||
+ | | style="text-align:right;" | 8155.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2004-0 | ||
+ | | style="text-align:right;" | 6018.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 30.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2005-0 | ||
+ | | style="text-align:right;" | 5147.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2006-0 | ||
+ | | style="text-align:right;" | 3905.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2007-0 | ||
+ | | style="text-align:right;" | 2515.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2008-0 | ||
+ | | style="text-align:right;" | 1694.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2009-0 | ||
+ | | style="text-align:right;" | 1206.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2010-0 | ||
+ | | style="text-align:right;" | 938.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2011-0 | ||
+ | | style="text-align:right;" | 869.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2012-0 | ||
+ | | style="text-align:right;" | 223.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2013-0 | ||
+ | | style="text-align:right;" | 240.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2014-0 | ||
+ | | style="text-align:right;" | 5752.0 | ||
+ | | style="text-align:right;" | 365.0 | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 365.0 | ||
+ | |- | ||
|} | |} | ||
− | + | For data sources see<ref>{{cite web | |
− | + | | title = Ohio Department of Natural Resources RBDMS | |
− | + | | publisher = [http://oilandgas.ohiodnr.gov/] | |
− | + | | date = 2015-06-19 | |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production | |
− | + | | accessdate = 2015-06-20 }}</ref> | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
== Inspection Data == | == Inspection Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 64: | Line 202: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
+ | |- | ||
+ | | 1421515447 | ||
+ | | 2015-01-16 | ||
+ | | | ||
+ | | Inspected well for possible conversion to SWIW and in conversation with owner stating that he would like to get started on this project soon. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1427317582 | ||
+ | | 2015-03-25 | ||
+ | | | ||
+ | | On site to witness small 500 gal acid treatment on well to determine if it would possibly be a candidate well for injection purposes. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1427986033 | ||
+ | | 2015-03-30 | ||
+ | | | ||
+ | | On site to witness tubing and packer run into well. | ||
+ | New 2.875 tubing and Baker A-3 set lock packer with on/off tool. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1427986559 | ||
+ | | 2015-03-31 | ||
+ | | | ||
+ | | On site to witness MIT TEST Universal well services pressured up to 1515 psi and we monitored pressure for 15 minutes with minimal leak off (suspect trapped air within fluid column) passed testing requirements. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
|- | |- | ||
| 1636317047 | | 1636317047 | ||
| 2004-06-30 | | 2004-06-30 | ||
− | | | + | | |
− | + | | Inspection this day found no violations, well producing with rabbit, drill site has been reclaimed, cows been a little hard on it but will pass, well and tank (210 bbl) fenced, good dike but not good enough, good ID's, current chart - this is a great well!!!! I could live off this one | |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-167-29445 | Loading map...
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County: Washington | |
Municipality: | |
Operator Name: HEINRICH ENT INC/WASHINGTON OP | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1999-12-23 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 39.42992595 | |
Longitude: -81.51130419 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1999-0 | ||||||
2000-0 | 25698.0 | 65.0 | ||||
2001-0 | 12004.0 | 0.0 | ||||
2002-0 | 10938.0 | 27.0 | ||||
2003-0 | 8155.0 | 0.0 | ||||
2004-0 | 6018.0 | 30.0 | ||||
2005-0 | 5147.0 | 0.0 | ||||
2006-0 | 3905.0 | 0.0 | ||||
2007-0 | 2515.0 | 0.0 | ||||
2008-0 | 1694.0 | 0.0 | ||||
2009-0 | 1206.0 | 0.0 | ||||
2010-0 | 938.0 | 0.0 | ||||
2011-0 | 869.0 | 0.0 | ||||
2012-0 | 223.0 | 0.0 | ||||
2013-0 | 240.0 | 0.0 | ||||
2014-0 | 5752.0 | 365.0 | 0.0 | 365.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1421515447 | 2015-01-16 | Inspected well for possible conversion to SWIW and in conversation with owner stating that he would like to get started on this project soon. | ||||
1427317582 | 2015-03-25 | On site to witness small 500 gal acid treatment on well to determine if it would possibly be a candidate well for injection purposes. | ||||
1427986033 | 2015-03-30 | On site to witness tubing and packer run into well.
New 2.875 tubing and Baker A-3 set lock packer with on/off tool. |
||||
1427986559 | 2015-03-31 | On site to witness MIT TEST Universal well services pressured up to 1515 psi and we monitored pressure for 15 minutes with minimal leak off (suspect trapped air within fluid column) passed testing requirements. | ||||
1636317047 | 2004-06-30 | Inspection this day found no violations, well producing with rabbit, drill site has been reclaimed, cows been a little hard on it but will pass, well and tank (210 bbl) fenced, good dike but not good enough, good ID's, current chart - this is a great well!!!! I could live off this one |
For data sources see[2]