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Difference between revisions of "34-151-22250"

m
 
m
Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-151-22250
 
| Well ID: 34-151-22250
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.8607882425, -81.0941496561 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.86039136, -81.0946606 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Stark County, Ohio|Stark]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[ENERVEST OPERATING L]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1971-10-22
 
| Spud Date: 1971-10-22
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Producing
 
|-
 
|-
| Violations: 1
+
| Violations: 0
 
|-
 
|-
| Latitude: 40.8607882425
+
| Latitude: 40.86039136
 
|-
 
|-
| Longitude: -81.0941496561
+
| Longitude: -81.0946606
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1984-0
 +
| style="text-align:right;" | 2435.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1985-0
 +
| style="text-align:right;" | 2019.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1986-0
 +
| style="text-align:right;" | 5939.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1987-0
 +
| style="text-align:right;" | 10613.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 206.0
 +
|
 +
|-
 +
|-
 +
| 1988-0
 +
| style="text-align:right;" | 4086.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1989-0
 +
| style="text-align:right;" | 6358.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 153.0
 +
|
 +
|-
 +
|-
 +
| 1990-0
 +
| style="text-align:right;" | 6934.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 112.0
 +
|
 +
|-
 +
|-
 +
| 1991-0
 +
| style="text-align:right;" | 8764.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 169.0
 +
|
 +
|-
 +
|-
 +
| 1992-0
 +
| style="text-align:right;" | 12824.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 284.0
 +
|
 +
|-
 +
|-
 +
| 1993-0
 +
| style="text-align:right;" | 12637.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 188.0
 +
|
 +
|-
 +
|-
 +
| 1994-0
 +
| style="text-align:right;" | 13399.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 192.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 12852.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 195.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 3957.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 127.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 261.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 312.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1999-0
 +
| style="text-align:right;" | 8737.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 261.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 5000.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 156.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 3935.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 62.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 4018.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 105.0
 +
|
 +
|-
 +
|-
 +
| 2003-0
 +
| style="text-align:right;" | 3016.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 43.0
 +
|
 +
|-
 +
|-
 +
| 2004-0
 +
| style="text-align:right;" | 214.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2005-0
 +
| style="text-align:right;" | 114.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 27.0
 +
|
 +
|-
 +
|-
 +
| 2006-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2007-0
 +
| style="text-align:right;" | 847.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2008-0
 +
| style="text-align:right;" | 2031.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2009-0
 +
| style="text-align:right;" | 1286.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2010-0
 +
| style="text-align:right;" | 1109.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2011-0
 +
| style="text-align:right;" | 1776.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2012-0
 +
| style="text-align:right;" | 7194.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 268.0
 +
|
 +
|-
 +
|-
 +
| 2013-0
 +
| style="text-align:right;" | 6355.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 55.0
 +
|
 +
|-
 +
|-
 +
| 2014-0
 +
| style="text-align:right;" | 6620.0
 +
| style="text-align:right;" | 365.0
 +
|
 +
|
 +
| style="text-align:right;" | 141.0
 +
| style="text-align:right;" | 365.0
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 337:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 +
|-
 +
| 1079025121
 +
| 2004-03-10
 +
|
 +
| Investigated a possible line leak reported (3-8-04) by Doug Bruner (740-685-3064). Doug Bruner had informed Power Gas of the possible leak, but he didn't feel they were responding. Met Inspector Jonnie Patrick at the site. He had been called by Power Gas on 3-10-04, telling him the release was in Columbiana Co. Power Gas had repaired the line on the morning of 3-10-04. An area 150' x 150' was affected (GPS location 40.85877, 81.09348). There was oil on the vegetation and on the ponded water in the field. The release was contained in the 150' x 150' area. Discussed the method of clean-up with John Firko (Power Gas). Took digital photos of the release. Informed Doug Bruner of the findings. Will monitor the clean-up.
 +
|
 +
|
 +
| Phone Call
 +
|-
 
|-
 
|-
 
| -1082758553
 
| -1082758553
 
| 2004-08-10
 
| 2004-08-10
|
+
|  
 
| Site is 60% cleaned up. The site still needs additional remediation. I called and left a message for John Firko.
 
| Site is 60% cleaned up. The site still needs additional remediation. I called and left a message for John Firko.
|
+
|  
|
+
|  
|
+
|  
|-
 
|-
 
| -1207847892
 
| 2004-07-15
 
|
 
| N.O.V. has NOT been resolved. Water level is down; vegetation is dead; surrounding field has been cut. Access to the release area is very good for starting clean up. Call John Firko.
 
|
 
|
 
|
 
|-
 
|-
 
| -358971475
 
| 2004-10-12
 
|
 
| N.O.V. has not been resolved. I called Paul Cramer (Power Gas) and told him that the location is very dry and that he can access the east side of the former release to clean it up.
 
|
 
|
 
|
 
|-
 
|-
 
| -713514179
 
| 2008-11-20
 
|
 
| Located access road. I met with a North Coast pumper at the location. The access road appears to be the driveway to a newer home (gray, 1-story, on the west side). Also, when the home (white, 1-story, on the east side) was being built, the excavator hit the well flow line.
 
|
 
|
 
|
 
|-
 
|-
 
| 1079025121
 
| 2004-03-10
 
|
 
| Investigated a possible line leak reported (3-8-04) by Doug Bruner (740-685-3064). Doug Bruner had informed Power Gas of the possible leak, but he didn't feel they were responding. Met Inspector Jonnie Patrick at the site. He had been called by Power Gas on 3-10-04, telling him the release was in Columbiana Co. Power Gas had repaired the line on the morning of 3-10-04. An area 150' x 150' was affected (GPS location 40.85877, 81.09348). There was oil on the vegetation and on the ponded water in the field. The release was contained in the 150' x 150' area. Discussed the method of clean-up with John Firko (Power Gas). Took digital photos of the release. Informed Doug Bruner of the findings. Will monitor the clean-up.
 
|
 
| 9-1-07
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 1096314715
 
| 1096314715
 
| 2004-09-27
 
| 2004-09-27
|
+
|  
 
| Line leak clean up is still not finished. Will call John Firko or Paul Cramer.
 
| Line leak clean up is still not finished. Will call John Firko or Paul Cramer.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1098314391
 
| 1098314391
 
| 2004-10-20
 
| 2004-10-20
|
+
|  
 
| N.O.V. has been RESOLVED. The release has been cleaned up and the crude stained soil and vegetation has been removed from the site and placed at Power Gas's facility.
 
| N.O.V. has been RESOLVED. The release has been cleaned up and the crude stained soil and vegetation has been removed from the site and placed at Power Gas's facility.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1207847892
 +
| 2004-07-15
 +
|
 +
| N.O.V. has NOT been resolved. Water level is down; vegetation is dead; surrounding field has been cut. Access to the release area is very good for starting clean up. Call John Firko.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 1888678807
 
| 1888678807
 
| 2004-05-12
 
| 2004-05-12
|
+
|  
 
| Visited the location with Wayne Schalk, Tom Tugend, and Tom Hines. The cleanup from the line leak repair has not been completed.
 
| Visited the location with Wayne Schalk, Tom Tugend, and Tom Hines. The cleanup from the line leak repair has not been completed.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -358971475
 +
| 2004-10-12
 +
|
 +
| N.O.V. has not been resolved. I called Paul Cramer (Power Gas) and told him that the location is very dry and that he can access the east side of the former release to clean it up.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 426226869
 
| 426226869
 
| 2004-05-04
 
| 2004-05-04
|
+
|  
 
| Clean up has not been completed. Call John Firko.
 
| Clean up has not been completed. Call John Firko.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -713514179
 +
| 2008-11-20
 +
|
 +
| Located access road. I met with a North Coast pumper at the location. The access road appears to be the driveway to a newer home (gray, 1-story, on the west side). Also, when the home (white, 1-story, on the east side) was being built, the excavator hit the well flow line.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 916857163
 
| 916857163
 
| 2004-08-31
 
| 2004-08-31
|
+
|  
 
| The site still needs additional clean-up of stained soil and vegetation.
 
| The site still needs additional clean-up of stained soil and vegetation.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 972495950
 
| 972495950
 
| 2004-03-25
 
| 2004-03-25
|
+
|  
 
| No additional clean up has been done. N.O.V. is UNRESOLVED.
 
| No additional clean up has been done. N.O.V. is UNRESOLVED.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 03:19, 15 July 2015

Well Details

Well ID: 34-151-22250
Loading map...
County: Stark
Municipality:
Operator Name: ENERVEST OPERATING L
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1971-10-22
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 40.86039136
Longitude: -81.0946606

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 2435.0 0.0
1985-0 2019.0 0.0
1986-0 5939.0 0.0
1987-0 10613.0 206.0
1988-0 4086.0 0.0
1989-0 6358.0 153.0
1990-0 6934.0 112.0
1991-0 8764.0 169.0
1992-0 12824.0 284.0
1993-0 12637.0 188.0
1994-0 13399.0 192.0
1995-0 12852.0 195.0
1996-0 3957.0 127.0
1997-0 261.0 0.0
1998-0 312.0 0.0
1999-0 8737.0 261.0
2000-0 5000.0 156.0
2001-0 3935.0 62.0
2002-0 4018.0 105.0
2003-0 3016.0 43.0
2004-0 214.0 0.0
2005-0 114.0 27.0
2006-0 0.0 0.0
2007-0 847.0 0.0
2008-0 2031.0 0.0
2009-0 1286.0 0.0
2010-0 1109.0 0.0
2011-0 1776.0 0.0
2012-0 7194.0 268.0
2013-0 6355.0 55.0
2014-0 6620.0 365.0 141.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1079025121 2004-03-10 Investigated a possible line leak reported (3-8-04) by Doug Bruner (740-685-3064). Doug Bruner had informed Power Gas of the possible leak, but he didn't feel they were responding. Met Inspector Jonnie Patrick at the site. He had been called by Power Gas on 3-10-04, telling him the release was in Columbiana Co. Power Gas had repaired the line on the morning of 3-10-04. An area 150' x 150' was affected (GPS location 40.85877, 81.09348). There was oil on the vegetation and on the ponded water in the field. The release was contained in the 150' x 150' area. Discussed the method of clean-up with John Firko (Power Gas). Took digital photos of the release. Informed Doug Bruner of the findings. Will monitor the clean-up. Phone Call
-1082758553 2004-08-10 Site is 60% cleaned up. The site still needs additional remediation. I called and left a message for John Firko.
1096314715 2004-09-27 Line leak clean up is still not finished. Will call John Firko or Paul Cramer.
1098314391 2004-10-20 N.O.V. has been RESOLVED. The release has been cleaned up and the crude stained soil and vegetation has been removed from the site and placed at Power Gas's facility.
-1207847892 2004-07-15 N.O.V. has NOT been resolved. Water level is down; vegetation is dead; surrounding field has been cut. Access to the release area is very good for starting clean up. Call John Firko.
1888678807 2004-05-12 Visited the location with Wayne Schalk, Tom Tugend, and Tom Hines. The cleanup from the line leak repair has not been completed.
-358971475 2004-10-12 N.O.V. has not been resolved. I called Paul Cramer (Power Gas) and told him that the location is very dry and that he can access the east side of the former release to clean it up.
426226869 2004-05-04 Clean up has not been completed. Call John Firko.
-713514179 2008-11-20 Located access road. I met with a North Coast pumper at the location. The access road appears to be the driveway to a newer home (gray, 1-story, on the west side). Also, when the home (white, 1-story, on the east side) was being built, the excavator hit the well flow line.
916857163 2004-08-31 The site still needs additional clean-up of stained soil and vegetation.
972495950 2004-03-25 No additional clean up has been done. N.O.V. is UNRESOLVED.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.