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Difference between revisions of "34-053-20480"

m
 
m
Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-053-20480
 
| Well ID: 34-053-20480
| style="height=100%; align=center" rowspan="15" | {{#display_map: 38.9013549914, -82.3847327226 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 38.90118266, -82.38511334 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Gallia County, Ohio|Gallia]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[ENERGY SEARCH INC]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 2009-10-06
 
| Spud Date: 2009-10-06
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Final Restoration
 
|-
 
|-
| Violations: 10
+
| Violations: 0
 
|-
 
|-
| Latitude: 38.9013549914
+
| Latitude: 38.90118266
 
|-
 
|-
| Longitude: -82.3847327226
+
| Longitude: -82.38511334
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1999-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
|
 +
|
 +
|
 +
|
 +
|
 +
|
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 103:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
| -133791555
+
| 1036086491
| 2009-05-13
+
| 2002-10-31
|
+
|  
| Called Gary Smith (Energy Search) 5-13-09 at 11:05am 742-743-2722 and asked when they are going to plug the well. Gary told me that he is waiting on a check and then they will plug the well in 30-45 days.
+
| Inspection of the well site revealed well incapable of production. 5 1/2 casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease.    WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED. FAILURE TO COMPLY WILL RESULT IN FORFEITURE OF BOND
|
+
|  
|
+
|  
|
+
| Compliance Notice
 
|-
 
|-
 
|-
 
|-
| -1707659132
+
| 1036086491
| 2009-10-08
 
|
 
| Flaring gas during the inspection.
 
|
 
|
 
|
 
|-
 
|-
 
| -1952516690
 
| 2007-07-18
 
|
 
| Called Rick Green (EOG) at 11:19am on 7-18-07  About the status of this well. Rick told me that it is on the plug list but that his boss told him to stop plugging wells and to stop spending money until the wells are sold. I told Rick that they need to write a letter if the time frame cannot be met requesting an extension.  If they did not it could go to a Chiefs order.
 
|
 
|
 
|
 
|-
 
|-
 
| -2126055392
 
 
| 2002-10-31
 
| 2002-10-31
|
+
|  
| FOLLOW UP TO NOV #  1036086491  Inspection of the well site revealed well incapable of production.  5 1/2" casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease.    WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED.  FAILU
+
| Inspection of the well site revealed well incapable of production.  5 1/2 casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease.    WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED.  FAILURE TO COMPLY WILL RESULT IN FORFEITURE OF BOND
|
+
|  
| NONE
+
|  
|
+
| Compliance Notice
 
|-
 
|-
 
|-
 
|-
| -2126055392
+
| 1036086491
 
| 2002-10-31
 
| 2002-10-31
|
+
|  
| FOLLOW UP TO NOV #  1036086491  Inspection of the well site revealed well incapable of production.  5 1/2" casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease.    WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED.  FAILU
+
| Inspection of the well site revealed well incapable of production.  5 1/2 casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease.    WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED.  FAILURE TO COMPLY WILL RESULT IN FORFEITURE OF BOND
|
+
|  
| NONE F
+
|  
|
+
| Compliance Notice
|-
 
|-
 
| -2137672647
 
| 2003-03-20
 
|
 
| The well has never produced oil or gas and remains incapable of production..  The well lacks all the necessary surface equipment.  There have been no apparent attempts made to produce the well.
 
|
 
|
 
|
 
|-
 
|-
 
| -329400781
 
| 2009-10-08
 
|
 
| Received a call from Greg Lawson 11:00am Re: The well kicked off and they are building a flare. I reminded Greg of the 100 foot spacing from the well to flare.
 
|
 
|
 
|
 
|-
 
|-
 
| -331686160
 
| 2009-10-21
 
|
 
| Drilled out to 3401 feet. Logged well and revealed the cement top to be at 276 feet. Cut 4.5" at 240 feet.
 
|
 
|
 
|
 
|-
 
|-
 
| -51408162
 
| 2003-01-30
 
|
 
| Well is still idle.  No action has been taken to produce the well.
 
|
 
|
 
|
 
|-
 
|-
 
| -841229755
 
| 2004-01-30
 
|
 
| Well head completely disconnected; probably never produced.
 
|
 
|
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 1036086491
 
| 1036086491
 
| 2002-10-31
 
| 2002-10-31
|
+
|  
| Inspection of the well site revealed well incapable of production.  5 1/2" casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease.    WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED.  FAILURE TO COMPLY WILL RESULT IN FORFEITURE OF BOND
+
| Inspection of the well site revealed well incapable of production.  5 1/2 casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease.    WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED.  FAILURE TO COMPLY WILL RESULT IN FORFEITURE OF BOND
|
+
|  
| NONE
+
|  
|
+
| Compliance Notice
 
|-
 
|-
 
|-
 
|-
 
| 1036086491
 
| 1036086491
 
| 2002-10-31
 
| 2002-10-31
|
+
|  
| Inspection of the well site revealed well incapable of production.  5 1/2" casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease.    WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED.  FAILURE TO COMPLY WILL RESULT IN FORFEITURE OF BOND
+
| Inspection of the well site revealed well incapable of production.  5 1/2 casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease.    WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED.  FAILURE TO COMPLY WILL RESULT IN FORFEITURE OF BOND
|
+
|  
| NONE F
+
|  
|
+
| Compliance Notice
 
|-
 
|-
 
|-
 
|-
 
| 1045045045
 
| 1045045045
 
| 2009-10-13
 
| 2009-10-13
|
+
|  
 
| Plug job, TD top of plug at 549' Drilling out cement squeeze plug now. Have installed stripping head on well. Salt Sand is still making gas. Flared all weekend.
 
| Plug job, TD top of plug at 549' Drilling out cement squeeze plug now. Have installed stripping head on well. Salt Sand is still making gas. Flared all weekend.
|
+
|  
|
+
|  
|
+
|  
|-
 
|-
 
| 1062607346
 
| 2002-10-31
 
|
 
| FOLLOW UP TO NOV #  1036086491  Inspection of the well site revealed well incapable of production.  5 1/2" casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease.    WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED.  FAILURE TO COMPLY MAY RESULT IN FORFEITURE OF BOND.
 
|
 
| NONE
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 1062607346
 
| 1062607346
 
| 2002-10-31
 
| 2002-10-31
|
+
|  
| FOLLOW UP TO NOV #  1036086491  Inspection of the well site revealed well incapable of production.  5 1/2" casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease.    WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED.  FAILURE TO COMPLY MAY RESULT IN FORFEITURE OF BOND.
+
| FOLLOW UP TO NOV #  1036086491  Inspection of the well site revealed well incapable of production.  5 1/2 casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease.    WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED.  FAILURE TO COMPLY MAY RESULT IN FORFEITURE OF BOND.
|
+
|  
| NONE F
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 115001541
 
| 115001541
 
| 2010-09-29
 
| 2010-09-29
|
+
|  
 
| Site graded. Good vegetative cover established.
 
| Site graded. Good vegetative cover established.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1219398554
 
| 1219398554
 
| 2007-07-10
 
| 2007-07-10
|
+
|  
 
| Meeting at well site 9am with the landowner Allen Smith. Allen was thinking of buying the well from Energy Search. He would be using the gas to heat a commercial business. I gave him the regestration requirements for ownership. I explained the insurance he would have to get. After talking to his insurance agent Mr. Smith decided to not take the well and now wants the well plugged.
 
| Meeting at well site 9am with the landowner Allen Smith. Allen was thinking of buying the well from Energy Search. He would be using the gas to heat a commercial business. I gave him the regestration requirements for ownership. I explained the insurance he would have to get. After talking to his insurance agent Mr. Smith decided to not take the well and now wants the well plugged.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1228750023
 
| 1228750023
 
| 2008-12-08
 
| 2008-12-08
|
+
|  
 
| I called Energy Search (EOG) Gary Smith (724) 743-2722 at 10:25am on 12-8-2008. I talked to Gary about the status of the Cennamo-Blankenship 1-10 well. This well did not transfer during the North Coast Energy buy out of Energy Search last year. This well had a current plug permit issued at the time of sale. Gary said that the well should have transferred to North Coast. I told Gary that The well needs to be capable of production or plugged. I informed Gary that the well has outstanding violations. Gary said that he will make some calls and call me back on 12-9-08. I gave him my cell number and office number.
 
| I called Energy Search (EOG) Gary Smith (724) 743-2722 at 10:25am on 12-8-2008. I talked to Gary about the status of the Cennamo-Blankenship 1-10 well. This well did not transfer during the North Coast Energy buy out of Energy Search last year. This well had a current plug permit issued at the time of sale. Gary said that the well should have transferred to North Coast. I told Gary that The well needs to be capable of production or plugged. I informed Gary that the well has outstanding violations. Gary said that he will make some calls and call me back on 12-9-08. I gave him my cell number and office number.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
| 1376332089
+
| -133791555
| 2007-06-13
+
| 2009-05-13
|
+
|  
| No id. Well is idle no lines are ran to or  connected to the well. The well is capped off. Not capable of production.
+
| Called Gary Smith (Energy Search) 5-13-09 at 11:05am 742-743-2722 and asked when they are going to plug the well. Gary told me that he is waiting on a check and then they will plug the well in 30-45 days.
|
+
|  
| 9-9-05(A)10
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1376332089
 
| 1376332089
 
| 2007-06-13
 
| 2007-06-13
|
+
|  
 
| No id. Well is idle no lines are ran to or  connected to the well. The well is capped off. Not capable of production.
 
| No id. Well is idle no lines are ran to or  connected to the well. The well is capped off. Not capable of production.
|
+
|  
| NONE
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1424610964
 
| 1424610964
 
| 2009-01-13
 
| 2009-01-13
|
+
|  
| No identification on wellhead. Well is not capable of production. There are no production lines or surface equipment on location. Well consists of 8 5/8" surface casing, 4 1/2" production casing, 2" tubing and valves. All valves are shut off. Well is not open at the surface. This inspection was to verify the well status, in order to continue enforcement action to get the well in production or plugged. Pictures were taken of the wellhead. I talked to the landowner Allen Smith on the phone and he stated to me that he is not interested in owning the well at all. He stated that he wants the well plugged. I have verified with Erica Freeman (ODNR) that the Well is still under the Energy Search Inc. Bond.
+
| No identification on wellhead. Well is not capable of production. There are no production lines or surface equipment on location. Well consists of 8 5/8 surface casing, 4 1/2 production casing, 2 tubing and valves. All valves are shut off. Well is not open at the surface. This inspection was to verify the well status, in order to continue enforcement action to get the well in production or plugged. Pictures were taken of the wellhead. I talked to the landowner Allen Smith on the phone and he stated to me that he is not interested in owning the well at all. He stated that he wants the well plugged. I have verified with Erica Freeman (ODNR) that the Well is still under the Energy Search Inc. Bond.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1707659132
 +
| 2009-10-08
 +
|
 +
| Flaring gas during the inspection.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -1952516690
 +
| 2007-07-18
 +
|
 +
| Called Rick Green (EOG) at 11:19am on 7-18-07  About the status of this well. Rick told me that it is on the plug list but that his boss told him to stop plugging wells and to stop spending money until the wells are sold. I told Rick that they need to write a letter if the time frame cannot be met requesting an extension.  If they did not it could go to a Chiefs order.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 1990512689
 
| 1990512689
 
| 2009-10-22
 
| 2009-10-22
|
+
|  
 
| Plug from 3400' to 2996'. 35 sks displace 11 bbls. 24 bbls 6% gel, 1500' plug gel, Lime plug 200' 3 bbls cement, 15 sks, from 2364' to 2160'. 2160' to 1310' gel, 1310' to 0 feet 104 sks 22 bbls.
 
| Plug from 3400' to 2996'. 35 sks displace 11 bbls. 24 bbls 6% gel, 1500' plug gel, Lime plug 200' 3 bbls cement, 15 sks, from 2364' to 2160'. 2160' to 1310' gel, 1310' to 0 feet 104 sks 22 bbls.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -2126055392
 +
| 2002-10-31
 +
|
 +
| FOLLOW UP TO NOV #  1036086491  Inspection of the well site revealed well incapable of production.  5 1/2 casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease.    WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED.  FAILU
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 2127248725
 
| 2127248725
 
| 2009-11-23
 
| 2009-11-23
|
+
|  
 
| Pit has been filled in. Site has been graded, Seed and mulch applied. No violations observed during inspection. Will inspect at later date to verify vegetative growth.
 
| Pit has been filled in. Site has been graded, Seed and mulch applied. No violations observed during inspection. Will inspect at later date to verify vegetative growth.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -2137672647
 +
| 2003-03-20
 +
|
 +
| The well has never produced oil or gas and remains incapable of production..  The well lacks all the necessary surface equipment.  There have been no apparent attempts made to produce the well.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -329400781
 +
| 2009-10-08
 +
|
 +
| Received a call from Greg Lawson 11:00am Re: The well kicked off and they are building a flare. I reminded Greg of the 100 foot spacing from the well to flare.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -331686160
 +
| 2009-10-21
 +
|
 +
| Drilled out to 3401 feet. Logged well and revealed the cement top to be at 276 feet. Cut 4.5 at 240 feet.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -450095869
 +
| 2014-12-04
 +
|
 +
| Preliminary Restoration requirements met.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -51408162
 +
| 2003-01-30
 +
|
 +
| Well is still idle.  No action has been taken to produce the well.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 526534478
 
| 526534478
 
| 2009-10-06
 
| 2009-10-06
|
+
|  
 
| Digging pit and install plastic liner. Moving rig on location.
 
| Digging pit and install plastic liner. Moving rig on location.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
| 871732079
+
| -841229755
| 2002-10-31
+
| 2004-01-30
|
+
|  
| FOLLOW UP TO NOV #  1062607346 1036086491 FOLLOW UP TO NOV #  1036086491  Inspection of the well site revealed well incapable of production.  5 1/2" casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease.   WELL NEEDS TO
+
| Well head completely disconnected; probably never produced.
|
+
|  
| NONE
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 871732079
 
| 871732079
 
| 2002-10-31
 
| 2002-10-31
|
+
|  
| FOLLOW UP TO NOV #  1062607346 1036086491 FOLLOW UP TO NOV #  1036086491  Inspection of the well site revealed well incapable of production.  5 1/2" casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease.    WELL NEEDS TO
+
| FOLLOW UP TO NOV #  1062607346 1036086491 FOLLOW UP TO NOV #  1036086491  Inspection of the well site revealed well incapable of production.  5 1/2 casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease.    WELL NEEDS TO
|
+
|  
| NONE F
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 90614187
 
| 90614187
 
| 2010-01-27
 
| 2010-01-27
|
+
|  
 
| Pit filled in. Seed and mulch applied to location. Snow covering half of site. Unable to determine extent of vegetative cover at this time. No problems observed during inspection.
 
| Pit filled in. Seed and mulch applied to location. Snow covering half of site. Unable to determine extent of vegetative cover at this time. No problems observed during inspection.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 947375549
 
| 947375549
 
| 2009-10-07
 
| 2009-10-07
|
+
|  
 
| Plugging operations. 230 psi on the tubing and casing. Viking rig was flowing gas at wellhead. My gas meter signaled an dangerous level of gas near the rig. I told the rig operator to get the gas flow under control. Either by a flare located 100 feet from the well or by fluid to kill the gas. They tried using their mud pump to kill the gas flow.
 
| Plugging operations. 230 psi on the tubing and casing. Viking rig was flowing gas at wellhead. My gas meter signaled an dangerous level of gas near the rig. I told the rig operator to get the gas flow under control. Either by a flare located 100 feet from the well or by fluid to kill the gas. They tried using their mud pump to kill the gas flow.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 09:35, 15 July 2015

Well Details

Well ID: 34-053-20480
Loading map...
County: Gallia
Municipality:
Operator Name: ENERGY SEARCH INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2009-10-06
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 38.90118266
Longitude: -82.38511334

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1996-0 0.0 0.0
1997-0 0.0 0.0
1998-0 0.0 0.0
1999-0 0.0 0.0
2000-0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1036086491 2002-10-31 Inspection of the well site revealed well incapable of production. 5 1/2 casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease. WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED. FAILURE TO COMPLY WILL RESULT IN FORFEITURE OF BOND Compliance Notice
1036086491 2002-10-31 Inspection of the well site revealed well incapable of production. 5 1/2 casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease. WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED. FAILURE TO COMPLY WILL RESULT IN FORFEITURE OF BOND Compliance Notice
1036086491 2002-10-31 Inspection of the well site revealed well incapable of production. 5 1/2 casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease. WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED. FAILURE TO COMPLY WILL RESULT IN FORFEITURE OF BOND Compliance Notice
1036086491 2002-10-31 Inspection of the well site revealed well incapable of production. 5 1/2 casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease. WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED. FAILURE TO COMPLY WILL RESULT IN FORFEITURE OF BOND Compliance Notice
1036086491 2002-10-31 Inspection of the well site revealed well incapable of production. 5 1/2 casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease. WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED. FAILURE TO COMPLY WILL RESULT IN FORFEITURE OF BOND Compliance Notice
1045045045 2009-10-13 Plug job, TD top of plug at 549' Drilling out cement squeeze plug now. Have installed stripping head on well. Salt Sand is still making gas. Flared all weekend.
1062607346 2002-10-31 FOLLOW UP TO NOV # 1036086491 Inspection of the well site revealed well incapable of production. 5 1/2 casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease. WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED. FAILURE TO COMPLY MAY RESULT IN FORFEITURE OF BOND.
115001541 2010-09-29 Site graded. Good vegetative cover established.
1219398554 2007-07-10 Meeting at well site 9am with the landowner Allen Smith. Allen was thinking of buying the well from Energy Search. He would be using the gas to heat a commercial business. I gave him the regestration requirements for ownership. I explained the insurance he would have to get. After talking to his insurance agent Mr. Smith decided to not take the well and now wants the well plugged.
1228750023 2008-12-08 I called Energy Search (EOG) Gary Smith (724) 743-2722 at 10:25am on 12-8-2008. I talked to Gary about the status of the Cennamo-Blankenship 1-10 well. This well did not transfer during the North Coast Energy buy out of Energy Search last year. This well had a current plug permit issued at the time of sale. Gary said that the well should have transferred to North Coast. I told Gary that The well needs to be capable of production or plugged. I informed Gary that the well has outstanding violations. Gary said that he will make some calls and call me back on 12-9-08. I gave him my cell number and office number.
-133791555 2009-05-13 Called Gary Smith (Energy Search) 5-13-09 at 11:05am 742-743-2722 and asked when they are going to plug the well. Gary told me that he is waiting on a check and then they will plug the well in 30-45 days.
1376332089 2007-06-13 No id. Well is idle no lines are ran to or connected to the well. The well is capped off. Not capable of production.
1424610964 2009-01-13 No identification on wellhead. Well is not capable of production. There are no production lines or surface equipment on location. Well consists of 8 5/8 surface casing, 4 1/2 production casing, 2 tubing and valves. All valves are shut off. Well is not open at the surface. This inspection was to verify the well status, in order to continue enforcement action to get the well in production or plugged. Pictures were taken of the wellhead. I talked to the landowner Allen Smith on the phone and he stated to me that he is not interested in owning the well at all. He stated that he wants the well plugged. I have verified with Erica Freeman (ODNR) that the Well is still under the Energy Search Inc. Bond.
-1707659132 2009-10-08 Flaring gas during the inspection.
-1952516690 2007-07-18 Called Rick Green (EOG) at 11:19am on 7-18-07 About the status of this well. Rick told me that it is on the plug list but that his boss told him to stop plugging wells and to stop spending money until the wells are sold. I told Rick that they need to write a letter if the time frame cannot be met requesting an extension. If they did not it could go to a Chiefs order.
1990512689 2009-10-22 Plug from 3400' to 2996'. 35 sks displace 11 bbls. 24 bbls 6% gel, 1500' plug gel, Lime plug 200' 3 bbls cement, 15 sks, from 2364' to 2160'. 2160' to 1310' gel, 1310' to 0 feet 104 sks 22 bbls.
-2126055392 2002-10-31 FOLLOW UP TO NOV # 1036086491 Inspection of the well site revealed well incapable of production. 5 1/2 casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease. WELL NEEDS TO BE PLACED IN PRODUCTION OR PLUGGED. FAILU
2127248725 2009-11-23 Pit has been filled in. Site has been graded, Seed and mulch applied. No violations observed during inspection. Will inspect at later date to verify vegetative growth.
-2137672647 2003-03-20 The well has never produced oil or gas and remains incapable of production.. The well lacks all the necessary surface equipment. There have been no apparent attempts made to produce the well.
-329400781 2009-10-08 Received a call from Greg Lawson 11:00am Re: The well kicked off and they are building a flare. I reminded Greg of the 100 foot spacing from the well to flare.
-331686160 2009-10-21 Drilled out to 3401 feet. Logged well and revealed the cement top to be at 276 feet. Cut 4.5 at 240 feet.
-450095869 2014-12-04 Preliminary Restoration requirements met.
-51408162 2003-01-30 Well is still idle. No action has been taken to produce the well.
526534478 2009-10-06 Digging pit and install plastic liner. Moving rig on location.
-841229755 2004-01-30 Well head completely disconnected; probably never produced.
871732079 2002-10-31 FOLLOW UP TO NOV # 1062607346 1036086491 FOLLOW UP TO NOV # 1036086491 Inspection of the well site revealed well incapable of production. 5 1/2 casing with tubing and valves locked, no production lines, no sales meters, and no other production equipment on lease. WELL NEEDS TO
90614187 2010-01-27 Pit filled in. Seed and mulch applied to location. Snow covering half of site. Unable to determine extent of vegetative cover at this time. No problems observed during inspection.
947375549 2009-10-07 Plugging operations. 230 psi on the tubing and casing. Viking rig was flowing gas at wellhead. My gas meter signaled an dangerous level of gas near the rig. I told the rig operator to get the gas flow under control. Either by a flare located 100 feet from the well or by fluid to kill the gas. They tried using their mud pump to kill the gas flow.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.