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Difference between revisions of "34-133-20968"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-133-20968
 
| Well ID: 34-133-20968
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.274135666, -81.1318915868 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.27441431, -81.13243971 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Portage County, Ohio|Portage]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[EDC
 +
]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1976-11-27
 
| Spud Date: 1976-11-27
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Producing
 
|-
 
|-
| Violations: 4
+
| Violations: 0
 
|-
 
|-
| Latitude: 41.274135666
+
| Latitude: 41.27441431
 
|-
 
|-
| Longitude: -81.1318915868
+
| Longitude: -81.13243971
 
|-
 
|-
 
|}
 
|}
Line 43: Line 44:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1984-0
 +
| style="text-align:right;" | 1078.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 1508.0
 +
|
 +
|-
 +
|-
 +
| 1985-0
 +
| style="text-align:right;" | 1286.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 1435.0
 +
|
 +
|-
 +
|-
 +
| 1987-0
 +
| style="text-align:right;" | 1801.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 1100.0
 +
|
 +
|-
 +
|-
 +
| 1988-0
 +
| style="text-align:right;" | 1744.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 1091.0
 +
|
 +
|-
 +
|-
 +
| 1989-0
 +
| style="text-align:right;" | 2009.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 912.0
 +
|
 +
|-
 +
|-
 +
| 1990-0
 +
| style="text-align:right;" | 1684.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 872.0
 +
|
 +
|-
 +
|-
 +
| 1991-0
 +
| style="text-align:right;" | 1326.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 716.0
 +
|
 +
|-
 +
|-
 +
| 1992-0
 +
| style="text-align:right;" | 918.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 755.0
 +
|
 +
|-
 +
|-
 +
| 1993-0
 +
| style="text-align:right;" | 1094.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 20.0
 +
|
 +
|-
 +
|-
 +
| 1994-0
 +
| style="text-align:right;" | 1156.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 517.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 935.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 492.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 999.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 619.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 871.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 435.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 858.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 408.0
 +
|
 +
|-
 +
|-
 +
| 1999-0
 +
| style="text-align:right;" | 834.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 579.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 685.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 384.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 372.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 392.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 465.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 328.0
 +
|
 +
|-
 +
|-
 +
| 2003-0
 +
| style="text-align:right;" | 511.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 229.0
 +
|
 +
|-
 +
|-
 +
| 2004-0
 +
| style="text-align:right;" | 174.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 392.0
 +
|
 +
|-
 +
|-
 +
| 2005-0
 +
| style="text-align:right;" | 337.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 304.0
 +
|
 +
|-
 +
|-
 +
| 2006-0
 +
| style="text-align:right;" | 258.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 165.0
 +
|
 +
|-
 +
|-
 +
| 2007-0
 +
| style="text-align:right;" | 263.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 314.0
 +
|
 +
|-
 +
|-
 +
| 2008-0
 +
| style="text-align:right;" | 360.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 217.0
 +
|
 +
|-
 +
|-
 +
| 2009-0
 +
| style="text-align:right;" | 201.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 228.0
 +
|
 +
|-
 +
|-
 +
| 2010-0
 +
| style="text-align:right;" | 326.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 206.0
 +
|
 +
|-
 +
|-
 +
| 2011-0
 +
| style="text-align:right;" | 329.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 154.0
 +
|
 +
|-
 +
|-
 +
| 2012-0
 +
| style="text-align:right;" | 558.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 304.0
 +
|
 +
|-
 +
|-
 +
| 2013-0
 +
| style="text-align:right;" | 497.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 213.0
 +
|
 +
|-
 +
|-
 +
| 2014-0
 +
| style="text-align:right;" | 467.0
 +
| style="text-align:right;" | 365.0
 +
|
 +
|
 +
| style="text-align:right;" | 199.0
 +
| style="text-align:right;" | 365.0
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 329:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
 
| 1216i183
 
| 1216i183
 
| 2002-01-23
 
| 2002-01-23
|
+
|  
 
| 01-23-2002 Inspection this date revealed that the stuffing box on the well head has leaked oil onto the ground. Was not leaking at this time but does require clean-up.
 
| 01-23-2002 Inspection this date revealed that the stuffing box on the well head has leaked oil onto the ground. Was not leaking at this time but does require clean-up.
|
+
|  
| 9-1-07
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 2154i322
 
| 2154i322
 
| 2002-07-29
 
| 2002-07-29
|
+
|  
 
| Stuffing box is still leaking. Clean up has not been initiated. Met with John Firko and suggested that he initiate the clean up immediately.
 
| Stuffing box is still leaking. Clean up has not been initiated. Met with John Firko and suggested that he initiate the clean up immediately.
|
+
|  
| 9-1-07
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 2154i463
 
| 2154i463
 
| 2002-09-20
 
| 2002-09-20
|
+
|  
 
| VIOLATIONS RESOLVED.
 
| VIOLATIONS RESOLVED.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 21879171
 
| 21879171
 
| 2002-06-10
 
| 2002-06-10
|
+
|  
 
| Stuffing box has been leaking. Clean up around the wellhead. Met with John Firko at Power Gas office and informed him of the inspection.
 
| Stuffing box has been leaking. Clean up around the wellhead. Met with John Firko at Power Gas office and informed him of the inspection.
|
+
|  
|
+
|  
|
+
|  
|-
 
|-
 
| 723896511
 
| 2002-01-23
 
|
 
| FOLLOW UP TO NOV #  1216i183  01-23-2002 Inspection this date revealed that the stuffing box on the well head has leaked oil onto the ground. Was not leaking at this time but does require clean-up.
 
|
 
| 9-1-07
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 723896511
 
| 723896511
 
| 2002-01-23
 
| 2002-01-23
|
+
|  
 
| FOLLOW UP TO NOV #  1216i183  01-23-2002 Inspection this date revealed that the stuffing box on the well head has leaked oil onto the ground. Was not leaking at this time but does require clean-up.
 
| FOLLOW UP TO NOV #  1216i183  01-23-2002 Inspection this date revealed that the stuffing box on the well head has leaked oil onto the ground. Was not leaking at this time but does require clean-up.
|
+
|  
| 9-9-05(A)10
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 02:38, 16 July 2015

Well Details

Well ID: 34-133-20968
Loading map...
County: Portage
Municipality:
Operator Name: [[EDC

]]

Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1976-11-27
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.27441431
Longitude: -81.13243971

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 1078.0 1508.0
1985-0 1286.0 1435.0
1987-0 1801.0 1100.0
1988-0 1744.0 1091.0
1989-0 2009.0 912.0
1990-0 1684.0 872.0
1991-0 1326.0 716.0
1992-0 918.0 755.0
1993-0 1094.0 20.0
1994-0 1156.0 517.0
1995-0 935.0 492.0
1996-0 999.0 619.0
1997-0 871.0 435.0
1998-0 858.0 408.0
1999-0 834.0 579.0
2000-0 685.0 384.0
2001-0 372.0 392.0
2002-0 465.0 328.0
2003-0 511.0 229.0
2004-0 174.0 392.0
2005-0 337.0 304.0
2006-0 258.0 165.0
2007-0 263.0 314.0
2008-0 360.0 217.0
2009-0 201.0 228.0
2010-0 326.0 206.0
2011-0 329.0 154.0
2012-0 558.0 304.0
2013-0 497.0 213.0
2014-0 467.0 365.0 199.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1216i183 2002-01-23 01-23-2002 Inspection this date revealed that the stuffing box on the well head has leaked oil onto the ground. Was not leaking at this time but does require clean-up.
2154i322 2002-07-29 Stuffing box is still leaking. Clean up has not been initiated. Met with John Firko and suggested that he initiate the clean up immediately.
2154i463 2002-09-20 VIOLATIONS RESOLVED.
21879171 2002-06-10 Stuffing box has been leaking. Clean up around the wellhead. Met with John Firko at Power Gas office and informed him of the inspection.
723896511 2002-01-23 FOLLOW UP TO NOV # 1216i183 01-23-2002 Inspection this date revealed that the stuffing box on the well head has leaked oil onto the ground. Was not leaking at this time but does require clean-up.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.