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Difference between revisions of "34-035-21513"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-035-21513
 
| Well ID: 34-035-21513
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.4422116325, -81.9669931859 | width=100% | height=100% }}
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| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.44221163, -81.96699319 | width=100% | height=100% }}  
 
|-
 
|-
| County:
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| County: [[Cuyahoga County, Ohio|Cuyahoga]]
 
|-
 
|-
| Municipality:
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| Municipality:  
 
|-
 
|-
| Operator Name:
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| Operator Name: [[BAKERWELL SERV RIGS INC]]
 
|-
 
|-
| Well Pad ID:
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| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
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| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
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| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
| Spud Date:
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| Spud Date:  
 
|-
 
|-
| Unconventional:
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| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Final Restoration
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 41.4422116325
+
| Latitude: 41.44221163
 
|-
 
|-
| Longitude: -81.9669931859
+
| Longitude: -81.96699319
 
|-
 
|-
|}
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | GAS QUANTITY
 
!scope="col" | GAS PRODUCTION DAYS
 
!scope="col" | CONDENSATE QUANTITY
 
!scope="col" | CONDENSATE PRODUCTION DAYS
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
|}
 
== Waste Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | TYPE
 
!scope="col" | QUANTITY
 
!scope="col" | UNITS
 
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
 
|}
 
|}
 
== Inspection Data ==
 
== Inspection Data ==
Line 64: Line 42:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
 
| 16114
 
| 16114
|
+
|  
|
+
|  
| PASSED Y WITNESSED 7/11/91 INSPECTOR NORBURT LOWDER DATE 07/1119/91 DATA FROM OLD VAX INFO
+
| PASSED Y WITNESSED 7/11/91 INSPECTOR NORBURT LOWDER DATE 07/1119/91 DATA FROM OLD VAX INFO
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 16115
 
| 16115
|
+
|  
|
+
|  
| PASSED  WITNESSED  INSPECTOR  DATE 00/0019/00 DATA FROM OLD VAX INFO
+
| PASSED  WITNESSED  INSPECTOR  DATE 00/0019/00 DATA FROM OLD VAX INFO
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1978596237
 
| 1978596237
 
| 2014-05-01
 
| 2014-05-01
|
+
|  
 
| A prospective buyer of the property where this well had formerly been located called asking about potential issues with formerly plugged wells and implications for building on or near former wells. The well was reportedly plugged and later vaulted and vented. Currently a vent is visible but nothing else. I inspected the location and found a 4-inch diameter PVC field-constructed vent stack on the east side of the parcel which is currently undeveloped. I did not observe any other surface expression of the former well. I evaluated the vent stack for the presence of gas leakage using a Sperian detector. No detections of methane or explosive gas were observed. I contacted the prospective buyer and related my findings. I advised them to contact local building officials for guidance on local building and zoning requirements.
 
| A prospective buyer of the property where this well had formerly been located called asking about potential issues with formerly plugged wells and implications for building on or near former wells. The well was reportedly plugged and later vaulted and vented. Currently a vent is visible but nothing else. I inspected the location and found a 4-inch diameter PVC field-constructed vent stack on the east side of the parcel which is currently undeveloped. I did not observe any other surface expression of the former well. I evaluated the vent stack for the presence of gas leakage using a Sperian detector. No detections of methane or explosive gas were observed. I contacted the prospective buyer and related my findings. I advised them to contact local building officials for guidance on local building and zoning requirements.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 06:18, 16 July 2015

Well Details

Well ID: 34-035-21513
Loading map...
County: Cuyahoga
Municipality:
Operator Name: BAKERWELL SERV RIGS INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 41.44221163
Longitude: -81.96699319

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
16114 PASSED Y WITNESSED 7/11/91 INSPECTOR NORBURT LOWDER DATE 07/1119/91 DATA FROM OLD VAX INFO
16115 PASSED WITNESSED INSPECTOR DATE 00/0019/00 DATA FROM OLD VAX INFO
1978596237 2014-05-01 A prospective buyer of the property where this well had formerly been located called asking about potential issues with formerly plugged wells and implications for building on or near former wells. The well was reportedly plugged and later vaulted and vented. Currently a vent is visible but nothing else. I inspected the location and found a 4-inch diameter PVC field-constructed vent stack on the east side of the parcel which is currently undeveloped. I did not observe any other surface expression of the former well. I evaluated the vent stack for the presence of gas leakage using a Sperian detector. No detections of methane or explosive gas were observed. I contacted the prospective buyer and related my findings. I advised them to contact local building officials for guidance on local building and zoning requirements.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.