X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

Difference between revisions of "34-111-21984"

m
 
m
Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-111-21984
 
| Well ID: 34-111-21984
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.8251084583, -81.1593239832 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.82510846, -81.15932398 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Monroe County, Ohio|Monroe]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[C G O INC]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1980-08-07
 
| Spud Date: 1980-08-07
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Producing
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 39.8251084583
+
| Latitude: 39.82510846
 
|-
 
|-
| Longitude: -81.1593239832
+
| Longitude: -81.15932398
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1989-0
 +
| style="text-align:right;" | 1254.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 68.0
 +
|
 +
|-
 +
|-
 +
| 1990-0
 +
| style="text-align:right;" | 1387.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 60.0
 +
|
 +
|-
 +
|-
 +
| 1991-0
 +
| style="text-align:right;" | 949.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 37.0
 +
|
 +
|-
 +
|-
 +
| 1993-0
 +
| style="text-align:right;" | 1000.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1994-0
 +
| style="text-align:right;" | 619.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 52.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 1280.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 43.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 1469.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 42.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 1854.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 27.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 1263.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 52.0
 +
|
 +
|-
 +
|-
 +
| 1999-0
 +
| style="text-align:right;" | 1295.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 31.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 958.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 47.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 1011.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 43.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 1132.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 21.0
 +
|
 +
|-
 +
|-
 +
| 2003-0
 +
| style="text-align:right;" | 1310.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 37.0
 +
|
 +
|-
 +
|-
 +
| 2004-0
 +
| style="text-align:right;" | 908.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 32.0
 +
|
 +
|-
 +
|-
 +
| 2005-0
 +
| style="text-align:right;" | 1311.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 36.0
 +
|
 +
|-
 +
|-
 +
| 2006-0
 +
| style="text-align:right;" | 436.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 15.0
 +
|
 +
|-
 +
|-
 +
| 2007-0
 +
| style="text-align:right;" | 568.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 12.0
 +
|
 +
|-
 +
|-
 +
| 2008-0
 +
| style="text-align:right;" | 801.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 10.0
 +
|
 +
|-
 +
|-
 +
| 2009-0
 +
| style="text-align:right;" | 701.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 8.0
 +
|
 +
|-
 +
|-
 +
| 2010-0
 +
| style="text-align:right;" | 620.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 5.0
 +
|
 +
|-
 +
|-
 +
| 2011-0
 +
| style="text-align:right;" | 280.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 3.0
 +
|
 +
|-
 +
|-
 +
| 2012-0
 +
| style="text-align:right;" | 272.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 2.0
 +
|
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 265:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
 
| -1230602412
 
| -1230602412
 
| 2013-04-16
 
| 2013-04-16
|
+
|  
 
| Follow up inspection on Oil spill from separator valve malfunction on 04/09/13 found the oil spill area cleaned up and the ditch line containment dike still in place. The spill rags in place have no discoloration from oil.
 
| Follow up inspection on Oil spill from separator valve malfunction on 04/09/13 found the oil spill area cleaned up and the ditch line containment dike still in place. The spill rags in place have no discoloration from oil.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1315025181
 
| 1315025181
 
| 2008-03-17
 
| 2008-03-17
|
+
|  
 
| WELL  SUPPLIED WITH A RABBIT AND A 100BBL TANK.TANK NEEDS DIKED AND ID.WELL IS PRODUCING.
 
| WELL  SUPPLIED WITH A RABBIT AND A 100BBL TANK.TANK NEEDS DIKED AND ID.WELL IS PRODUCING.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1365544061
 
| 1365544061
 
| 2013-04-09
 
| 2013-04-09
|
+
|  
 
| Administrative inspection entry to document notification of a oil spill from the malfunction of a separator valve. At 8:38 AM Troy Harmon called and said he had found where the separator had a valve fail blowing oil outside the containment dike. Troy indicated He would begin clean up immediately and protect a ditch line coming from a road culvert with spill rags and boomers. The EPA spoke with Troy and Myself through out the day and agreed with the clean up and containment actions taken. I was in a meeting and will follow up on the next day. The landowner also called. And I spoke with Ken Mettler with the EPA.
 
| Administrative inspection entry to document notification of a oil spill from the malfunction of a separator valve. At 8:38 AM Troy Harmon called and said he had found where the separator had a valve fail blowing oil outside the containment dike. Troy indicated He would begin clean up immediately and protect a ditch line coming from a road culvert with spill rags and boomers. The EPA spoke with Troy and Myself through out the day and agreed with the clean up and containment actions taken. I was in a meeting and will follow up on the next day. The landowner also called. And I spoke with Ken Mettler with the EPA.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1365598063
 
| 1365598063
 
| 2013-04-10
 
| 2013-04-10
|
+
|  
 
| Inspection and follow up on oil spill. Inspection found the cause of the oil spill to be a 2'' mechanical valve that separated at the bottom of the separator causing the separator to discharge it's contents under pressure outside the containment dike. The oil had been cleaned up upon inspection and a small ditch had a secondary containment dike constructed to protect any residue that may enter it. Containment will remain for a period of time per request of the Ohio EPA. Proper SPCC is in place around the 100 barrel tank and separator with proper well identification in place. Equipment present at the well head is 4.5'' production casing and 1.5'' tubing with the production valves open and the well being produced by the means of a pumping unit. The valve that failed was pressure rated above the pressure rating of the pop off valve on the separator, no producer related violations found to be the cause of the spill.
 
| Inspection and follow up on oil spill. Inspection found the cause of the oil spill to be a 2'' mechanical valve that separated at the bottom of the separator causing the separator to discharge it's contents under pressure outside the containment dike. The oil had been cleaned up upon inspection and a small ditch had a secondary containment dike constructed to protect any residue that may enter it. Containment will remain for a period of time per request of the Ohio EPA. Proper SPCC is in place around the 100 barrel tank and separator with proper well identification in place. Equipment present at the well head is 4.5'' production casing and 1.5'' tubing with the production valves open and the well being produced by the means of a pumping unit. The valve that failed was pressure rated above the pressure rating of the pop off valve on the separator, no producer related violations found to be the cause of the spill.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1400620533
 
| 1400620533
 
| 2014-05-20
 
| 2014-05-20
|
+
|  
|   Status check & complaint # 4625 follow up inspection found the mechanical separator has not been repaired and still has a bungee strap holding the pressure lift mechanism open. There is no reported production in the database for 2011 and the gas sales meter has a current 31 day chart that shows no sales activity.
+
| Status check & complaint # 4625 follow up inspection found the mechanical separator has not been repaired and still has a bungee strap holding the pressure lift mechanism open. There is no reported production in the database for 2011 and the gas sales meter has a current 31 day chart that shows no sales activity.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 521040460
 
| 521040460
 
| 2012-03-21
 
| 2012-03-21
|
+
|  
 
| On the day of my inspection well was complete with a plunger lift system. The tank battery contents included one 100 barrel oil storage tank and a mechanical separator. No violations noted.
 
| On the day of my inspection well was complete with a plunger lift system. The tank battery contents included one 100 barrel oil storage tank and a mechanical separator. No violations noted.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 71006217
 
| 71006217
 
| 2014-03-11
 
| 2014-03-11
|
+
|  
| Status check inspection as part of complaint # 4625 follow up. On this day, my inspection found the following equipment present at the well head-4.5'' production casing-1.5'' tubing with the production valves open and the well set up to be produced by the means of a plunger lift system. A single 100 barrel production tank along with a mechanical separator and gas sales meter is located in an established dike with proper well identification posted, a domestic hook up is present. I spoke with Troy Harmon on this day and he indicated the separator had froze off during the extreme cold on January 23rd causing the oil to enter the domestic house gas line. No violations noted on this day.
+
| Status check inspection as part of complaint # 4625 follow up. On this day, my inspection found the following equipment present at the well head-4.5'' production casing-1.5'' tubing with the production valves open and the well set up to be produced by the means of a plunger lift system. A single 100 barrel production tank along with a mechanical separator and gas sales meter is located in an established dike with proper well identification posted, a domestic hook up is present. I spoke with Troy Harmon on this day and he indicated the separator had froze off during the extreme cold on January 23rd causing the oil to enter the domestic house gas line. No violations noted on this day.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 06:25, 16 July 2015

Well Details

Well ID: 34-111-21984
Loading map...
County: Monroe
Municipality:
Operator Name: C G O INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1980-08-07
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.82510846
Longitude: -81.15932398

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1989-0 1254.0 68.0
1990-0 1387.0 60.0
1991-0 949.0 37.0
1993-0 1000.0 0.0
1994-0 619.0 52.0
1995-0 1280.0 43.0
1996-0 1469.0 42.0
1997-0 1854.0 27.0
1998-0 1263.0 52.0
1999-0 1295.0 31.0
2000-0 958.0 47.0
2001-0 1011.0 43.0
2002-0 1132.0 21.0
2003-0 1310.0 37.0
2004-0 908.0 32.0
2005-0 1311.0 36.0
2006-0 436.0 15.0
2007-0 568.0 12.0
2008-0 801.0 10.0
2009-0 701.0 8.0
2010-0 620.0 5.0
2011-0 280.0 3.0
2012-0 272.0 2.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1230602412 2013-04-16 Follow up inspection on Oil spill from separator valve malfunction on 04/09/13 found the oil spill area cleaned up and the ditch line containment dike still in place. The spill rags in place have no discoloration from oil.
1315025181 2008-03-17 WELL SUPPLIED WITH A RABBIT AND A 100BBL TANK.TANK NEEDS DIKED AND ID.WELL IS PRODUCING.
1365544061 2013-04-09 Administrative inspection entry to document notification of a oil spill from the malfunction of a separator valve. At 8:38 AM Troy Harmon called and said he had found where the separator had a valve fail blowing oil outside the containment dike. Troy indicated He would begin clean up immediately and protect a ditch line coming from a road culvert with spill rags and boomers. The EPA spoke with Troy and Myself through out the day and agreed with the clean up and containment actions taken. I was in a meeting and will follow up on the next day. The landowner also called. And I spoke with Ken Mettler with the EPA.
1365598063 2013-04-10 Inspection and follow up on oil spill. Inspection found the cause of the oil spill to be a 2 mechanical valve that separated at the bottom of the separator causing the separator to discharge it's contents under pressure outside the containment dike. The oil had been cleaned up upon inspection and a small ditch had a secondary containment dike constructed to protect any residue that may enter it. Containment will remain for a period of time per request of the Ohio EPA. Proper SPCC is in place around the 100 barrel tank and separator with proper well identification in place. Equipment present at the well head is 4.5 production casing and 1.5 tubing with the production valves open and the well being produced by the means of a pumping unit. The valve that failed was pressure rated above the pressure rating of the pop off valve on the separator, no producer related violations found to be the cause of the spill.
1400620533 2014-05-20 Status check & complaint # 4625 follow up inspection found the mechanical separator has not been repaired and still has a bungee strap holding the pressure lift mechanism open. There is no reported production in the database for 2011 and the gas sales meter has a current 31 day chart that shows no sales activity.
521040460 2012-03-21 On the day of my inspection well was complete with a plunger lift system. The tank battery contents included one 100 barrel oil storage tank and a mechanical separator. No violations noted.
71006217 2014-03-11 Status check inspection as part of complaint # 4625 follow up. On this day, my inspection found the following equipment present at the well head-4.5 production casing-1.5 tubing with the production valves open and the well set up to be produced by the means of a plunger lift system. A single 100 barrel production tank along with a mechanical separator and gas sales meter is located in an established dike with proper well identification posted, a domestic hook up is present. I spoke with Troy Harmon on this day and he indicated the separator had froze off during the extreme cold on January 23rd causing the oil to enter the domestic house gas line. No violations noted on this day.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.