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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-009-23137 | | Well ID: 34-009-23137 | ||
− | | style="height=100%; align=center" rowspan="15" | {{#display_map: 39. | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 39.37137193, -81.95688934 | width=100% | height=100% }} |
|- | |- | ||
− | | County: | + | | County: [[Athens County, Ohio|Athens]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[WOLFE R OIL & GAS]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
| Spud Date: 1985-03-08 | | Spud Date: 1985-03-08 | ||
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | Producing | + | | Well Status: Producing |
|- | |- | ||
− | | Violations: | + | | Violations: 0 |
|- | |- | ||
− | | Latitude: 39. | + | | Latitude: 39.37137193 |
|- | |- | ||
− | | Longitude: -81. | + | | Longitude: -81.95688934 |
|- | |- | ||
|} | |} | ||
Line 43: | Line 43: | ||
!scope="col" | OIL QUANTITY | !scope="col" | OIL QUANTITY | ||
!scope="col" | OIL PRODUCTION DAYS | !scope="col" | OIL PRODUCTION DAYS | ||
+ | |- | ||
+ | | 1990-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 50.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2005-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2006-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2007-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2008-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2009-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 4.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2010-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2011-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2012-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2013-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 12.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2014-0 | ||
+ | | style="text-align:right;" | 56.0 | ||
+ | | style="text-align:right;" | 365.0 | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 7.0 | ||
+ | | style="text-align:right;" | 365.0 | ||
+ | |- | ||
|} | |} | ||
− | + | For data sources see<ref>{{cite web | |
− | + | | title = Ohio Department of Natural Resources RBDMS | |
− | + | | publisher = [http://oilandgas.ohiodnr.gov/] | |
− | + | | date = 2015-06-19 | |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production | |
− | + | | accessdate = 2015-06-20 }}</ref> | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
== Inspection Data == | == Inspection Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 64: | Line 157: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
|- | |- | ||
− | | | + | | 1081058227 |
− | | | + | | 2011-06-14 |
− | | | + | | |
− | | | + | | Upon inspection well was noted to have no well head. All that was at the site was the 3 inch production string sticking out of the ground. Well was identified correctly however. Well shall be produced, plugged, or placed in temporary inactive status. Spoke with R. Wolfe and he said he is planning to swab and produce the well this summer. I gave him 3 months to bring the well into production. |
− | | | + | | |
− | | | + | | |
− | | | + | | Field Visit or Inspection |
|- | |- | ||
|- | |- | ||
− | | | + | | 1397751375 |
− | | | + | | 2014-04-17 |
− | | | + | | |
− | | Follow up | + | | Compliance Notice Follow-up 1081058227: The well is still idle with no production or flow lines hooked up to the wellhead. The identification is posted at the well location. I called and left Randy Wolfe e message regarding the well issues. There has been no resolution to any of the issues. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
− | | | + | | 1414172468 |
− | | | + | | 2014-10-24 |
− | | | + | | |
− | | | + | | Follow up to 1081058227. I met Bart Kasler, who will be taking over this lease soon, and we discussed bringing the well into production. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
− | | | + | | -1753089665 |
− | | | + | | 2012-10-23 |
− | | | + | | |
− | | | + | | The well was still not equipped with an well head, just open 4 1/2 and 3 casing. The well is identified. The well has no lines and no production equipment. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
− | | | + | | -925797241 |
− | | | + | | 2013-11-27 |
− | | | + | | |
− | | | + | | Follow up to 1081058227. Well equipped with 5 casing open at the surface and 3 casing open at the surface. No lines, tanks, or equipment associated with the well. The was adequately identified. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-009-23137 | Loading map...
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County: Athens | |
Municipality: | |
Operator Name: WOLFE R OIL & GAS | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1985-03-08 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 39.37137193 | |
Longitude: -81.95688934 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1990-0 | 0.0 | 50.0 | ||||
2005-0 | 0.0 | 0.0 | ||||
2006-0 | 0.0 | 0.0 | ||||
2007-0 | 0.0 | 0.0 | ||||
2008-0 | 0.0 | 0.0 | ||||
2009-0 | 0.0 | 4.0 | ||||
2010-0 | 0.0 | 0.0 | ||||
2011-0 | 0.0 | 0.0 | ||||
2012-0 | 0.0 | 0.0 | ||||
2013-0 | 0.0 | 12.0 | ||||
2014-0 | 56.0 | 365.0 | 7.0 | 365.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1081058227 | 2011-06-14 | Upon inspection well was noted to have no well head. All that was at the site was the 3 inch production string sticking out of the ground. Well was identified correctly however. Well shall be produced, plugged, or placed in temporary inactive status. Spoke with R. Wolfe and he said he is planning to swab and produce the well this summer. I gave him 3 months to bring the well into production. | Field Visit or Inspection | |||
1397751375 | 2014-04-17 | Compliance Notice Follow-up 1081058227: The well is still idle with no production or flow lines hooked up to the wellhead. The identification is posted at the well location. I called and left Randy Wolfe e message regarding the well issues. There has been no resolution to any of the issues. | ||||
1414172468 | 2014-10-24 | Follow up to 1081058227. I met Bart Kasler, who will be taking over this lease soon, and we discussed bringing the well into production. | ||||
-1753089665 | 2012-10-23 | The well was still not equipped with an well head, just open 4 1/2 and 3 casing. The well is identified. The well has no lines and no production equipment. | ||||
-925797241 | 2013-11-27 | Follow up to 1081058227. Well equipped with 5 casing open at the surface and 3 casing open at the surface. No lines, tanks, or equipment associated with the well. The was adequately identified. |
For data sources see[2]