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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-055-22149 | | Well ID: 34-055-22149 | ||
− | | style="height=100%; align=center" rowspan="15" | {{#display_map: 41. | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 41.3544886, -81.11892227 | width=100% | height=100% }} |
|- | |- | ||
− | | County: | + | | County: [[Geauga County, Ohio|Geauga]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[EXCALIBUR EXPLORATION INC]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
| Spud Date: 2014-08-29 | | Spud Date: 2014-08-29 | ||
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | | + | | Well Status: Drilling |
|- | |- | ||
| Violations: 0 | | Violations: 0 | ||
|- | |- | ||
− | | Latitude: 41. | + | | Latitude: 41.3544886 |
|- | |- | ||
− | | Longitude: -81. | + | | Longitude: -81.11892227 |
|- | |- | ||
|} | |} | ||
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!scope="col" | OIL QUANTITY | !scope="col" | OIL QUANTITY | ||
!scope="col" | OIL PRODUCTION DAYS | !scope="col" | OIL PRODUCTION DAYS | ||
+ | |- | ||
+ | | 2014-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | |- | ||
|} | |} | ||
− | + | For data sources see<ref>{{cite web | |
− | + | | title = Ohio Department of Natural Resources RBDMS | |
− | + | | publisher = [http://oilandgas.ohiodnr.gov/] | |
− | + | | date = 2015-06-19 | |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production | |
− | + | | accessdate = 2015-06-20 }}</ref> | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
== Inspection Data == | == Inspection Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 64: | Line 67: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1409683410 | | 1409683410 | ||
| 2014-08-29 | | 2014-08-29 | ||
− | | | + | | |
| I received a call from Roy Poulson from PDC Drilling that they had spudded the well at 8:00 AM on 8/29/2014. | | I received a call from Roy Poulson from PDC Drilling that they had spudded the well at 8:00 AM on 8/29/2014. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1409942118 | | 1409942118 | ||
| 2014-09-05 | | 2014-09-05 | ||
− | | | + | | |
− | | I was on location to witness the cementing of the production casing. Poulson Drilling drilled a 7 7/8 | + | | I was on location to witness the cementing of the production casing. Poulson Drilling drilled a 7 7/8 hole to 4275'. The 4.5 production casing was set at 4276'. Petroset was the cement contractor on location. Petroset broke circulation and pumped 230 sacks of Class A Cement that mudscaled at 15.6 ppg. The plug was displaced using 66 BBL's of water. The plug landed and pressure was held at 1500 psi. The location is in stable condition. The pit liner is in good repair. No violations found. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | -174750442 | ||
+ | | 2014-09-17 | ||
+ | | | ||
+ | | My inspection found the well has a guage and a pop off valve on the annulus. The guage reads zero psi. Hagans Well Service has installed the tubing and rods in the well. The pump jack is on location but has not been installed on the well. The pits are open and in stable condition. The pit liner is in good repair. The location is in stable condition. No violations found. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| 1829685265 | | 1829685265 | ||
| 2014-09-02 | | 2014-09-02 | ||
− | | | + | | |
| My inspection today found Poulson Drilling to have reached 1498'. The company has no issues to report while drilling the previous 1498'. The location is in stable condition and the pits are in good repair. No violations found. | | My inspection today found Poulson Drilling to have reached 1498'. The company has no issues to report while drilling the previous 1498'. The location is in stable condition and the pits are in good repair. No violations found. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | -1849199637 | ||
+ | | 2014-08-29 | ||
+ | | | ||
+ | | I was on location for the cementing of the conductor casing. The 14 3/4 hole was drilled to 93'. The 11 3/4 conductor casing was set to 78'. Petroset was the cement company on location. Petroset broke circulation and ran 200 sacks of Class A cement that mudscaled at 15.6 ppg. The cement was displaced using 8.5 bbls of fresh water. Cement returns were observed at the surface. The location is in stable condition. The lease road is stone half way to the well and then runs along a field to the location. The pits are stable and the liner is in good repair. The top soil is piled at the West side of the location. The cellar is constructed of a 4'6 plastic pipe. No violations found. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -1869691534 | ||
+ | | 2015-05-04 | ||
+ | | | ||
+ | | My inspection found the location has been graded and seeded. Vegetation is beginning to establish around the location. The landowner is using the trees that were cut down for fire wood. The well is currently being produced. The tank battery is in good repair. The lease road is in stable condition. I will pass preliminary restoration when the vegetation has been established. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| 1978958416 | | 1978958416 | ||
| 2014-08-30 | | 2014-08-30 | ||
− | | | + | | |
− | | I was on location for the cementing of the surface casing. The 11 | + | | I was on location for the cementing of the surface casing. The 11 hole was drilled to 431'. The 8 5/8 surface casing was set to 410'. The landing joint was set to 390'. Petroset was the cement company on location. Petroset broke circulation and ran 185 sacks of Class A cement that mudscaled at 15.6 ppg. The plug was released and displaced using 25 bbls of fresh water. The plug landed and was pressured up on for five minutes. The amount of cement returns was 14 bbls. The location is in stable condition. The pits are stable and the liner is in good repair. No violations found. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | -381652980 | ||
+ | | 2014-09-03 | ||
+ | | | ||
+ | | My inspection found PDC to have drilled to 3089'. No reported issues while drilling to the current depth. The pit liner is in good repair. The location is in stable condition. No violations found. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-055-22149 | Loading map...
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County: Geauga | |
Municipality: | |
Operator Name: EXCALIBUR EXPLORATION INC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2014-08-29 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Drilling | |
Violations: 0 | |
Latitude: 41.3544886 | |
Longitude: -81.11892227 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2014-0 | 0.0 | 0.0 | 0.0 | 0.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1409683410 | 2014-08-29 | I received a call from Roy Poulson from PDC Drilling that they had spudded the well at 8:00 AM on 8/29/2014. | ||||
1409942118 | 2014-09-05 | I was on location to witness the cementing of the production casing. Poulson Drilling drilled a 7 7/8 hole to 4275'. The 4.5 production casing was set at 4276'. Petroset was the cement contractor on location. Petroset broke circulation and pumped 230 sacks of Class A Cement that mudscaled at 15.6 ppg. The plug was displaced using 66 BBL's of water. The plug landed and pressure was held at 1500 psi. The location is in stable condition. The pit liner is in good repair. No violations found. | ||||
-174750442 | 2014-09-17 | My inspection found the well has a guage and a pop off valve on the annulus. The guage reads zero psi. Hagans Well Service has installed the tubing and rods in the well. The pump jack is on location but has not been installed on the well. The pits are open and in stable condition. The pit liner is in good repair. The location is in stable condition. No violations found. | ||||
1829685265 | 2014-09-02 | My inspection today found Poulson Drilling to have reached 1498'. The company has no issues to report while drilling the previous 1498'. The location is in stable condition and the pits are in good repair. No violations found. | ||||
-1849199637 | 2014-08-29 | I was on location for the cementing of the conductor casing. The 14 3/4 hole was drilled to 93'. The 11 3/4 conductor casing was set to 78'. Petroset was the cement company on location. Petroset broke circulation and ran 200 sacks of Class A cement that mudscaled at 15.6 ppg. The cement was displaced using 8.5 bbls of fresh water. Cement returns were observed at the surface. The location is in stable condition. The lease road is stone half way to the well and then runs along a field to the location. The pits are stable and the liner is in good repair. The top soil is piled at the West side of the location. The cellar is constructed of a 4'6 plastic pipe. No violations found. | ||||
-1869691534 | 2015-05-04 | My inspection found the location has been graded and seeded. Vegetation is beginning to establish around the location. The landowner is using the trees that were cut down for fire wood. The well is currently being produced. The tank battery is in good repair. The lease road is in stable condition. I will pass preliminary restoration when the vegetation has been established. | ||||
1978958416 | 2014-08-30 | I was on location for the cementing of the surface casing. The 11 hole was drilled to 431'. The 8 5/8 surface casing was set to 410'. The landing joint was set to 390'. Petroset was the cement company on location. Petroset broke circulation and ran 185 sacks of Class A cement that mudscaled at 15.6 ppg. The plug was released and displaced using 25 bbls of fresh water. The plug landed and was pressured up on for five minutes. The amount of cement returns was 14 bbls. The location is in stable condition. The pits are stable and the liner is in good repair. No violations found. | ||||
-381652980 | 2014-09-03 | My inspection found PDC to have drilled to 3089'. No reported issues while drilling to the current depth. The pit liner is in good repair. The location is in stable condition. No violations found. |
For data sources see[2]