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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-089-23306 | | Well ID: 34-089-23306 | ||
− | | style="height=100%; align=center" rowspan="15" | {{#display_map: 40. | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 40.00528331, -82.22603324 | width=100% | height=100% }} |
|- | |- | ||
− | | County: | + | | County: [[Licking County, Ohio|Licking]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[L & S OIL AND GAS]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
− | | Spud Date: | + | | Spud Date: |
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | | + | | Well Status: Plugged and Abandoned |
|- | |- | ||
| Violations: 0 | | Violations: 0 | ||
|- | |- | ||
− | | Latitude: 40. | + | | Latitude: 40.00528331 |
|- | |- | ||
− | | Longitude: -82. | + | | Longitude: -82.22603324 |
|- | |- | ||
|} | |} | ||
Line 43: | Line 43: | ||
!scope="col" | OIL QUANTITY | !scope="col" | OIL QUANTITY | ||
!scope="col" | OIL PRODUCTION DAYS | !scope="col" | OIL PRODUCTION DAYS | ||
+ | |- | ||
+ | | 1984-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 1015.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1985-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 1015.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1986-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 415.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1987-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 415.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1988-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 463.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1989-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 213.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1990-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 276.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1991-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 213.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1997-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 218.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1998-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 259.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1999-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 228.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2000-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 218.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2001-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 150.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2002-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 164.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2003-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 122.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2004-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2005-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2007-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 190.0 | ||
+ | | | ||
+ | |- | ||
|} | |} | ||
− | + | For data sources see<ref>{{cite web | |
− | + | | title = Ohio Department of Natural Resources RBDMS | |
− | + | | publisher = [http://oilandgas.ohiodnr.gov/] | |
− | + | | date = 2015-06-19 | |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production | |
− | + | | accessdate = 2015-06-20 }}</ref> | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
== Inspection Data == | == Inspection Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 64: | Line 220: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
+ | |- | ||
+ | | 1178803510 | ||
+ | | 2007-05-09 | ||
+ | | | ||
+ | | John Loveridge hired Mike's Power Tong Service to come and turn on the tubing to try and free it up. They tried several things. They were able to unscrew a couple of time above the tool, but never below the tool. They gave up and are going to try jacking it out with a bigger set a jacks. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1179150236 | ||
+ | | 2007-05-07 | ||
+ | | | ||
+ | | Two 100 ton jacks were used to try and break the tubing free. They jacked on it with a lot of pressure and were afraid to go any farther. They decided to let it sit overnight with the pressure on it. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
|- | |- | ||
| -118864792 | | -118864792 | ||
| 2007-05-07 | | 2007-05-07 | ||
− | | | + | | |
| I inspected this well with Jeff Fry. John Loveridge is plugging the well. The tubing parted at 1200 feet. There is a colar looking up that has part threads in it. He ran back in with a 2 inch spear and grabbed a hold of the tubing. Now he can't go up or down. | | I inspected this well with Jeff Fry. John Loveridge is plugging the well. The tubing parted at 1200 feet. There is a colar looking up that has part threads in it. He ran back in with a 2 inch spear and grabbed a hold of the tubing. Now he can't go up or down. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | 1347560630 | ||
+ | | 2007-05-15 | ||
+ | | | ||
+ | | I stopped by to witness plugging operations today. They are still trying to pull the tubing with two 100 ton jacks. There is about 3 feet of stretch on the tubing. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| -1639980443 | | -1639980443 | ||
| 2007-05-24 | | 2007-05-24 | ||
− | | | + | | |
| I witnessed plugging operations today. | | I witnessed plugging operations today. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| -1651729685 | | -1651729685 | ||
| 2007-05-14 | | 2007-05-14 | ||
− | | | + | | |
| I stopped by well to see what progress has been made on the plugging operations. The tubing is still stuck in the hole and they are continuing to put pressure on the tubing with two 100 ton jacks. | | I stopped by well to see what progress has been made on the plugging operations. The tubing is still stuck in the hole and they are continuing to put pressure on the tubing with two 100 ton jacks. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | 1714346694 | ||
+ | | 2007-07-18 | ||
+ | | | ||
+ | | I stopped by the well location today to check on the plugging progress. Nobody was on location. They are still rigged up on the well and trying to recover the tubing and tool that is stuck in the hole. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| -1744642278 | | -1744642278 | ||
| 2007-06-11 | | 2007-06-11 | ||
− | | | + | | |
| I witnessed plugging operations today. | | I witnessed plugging operations today. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| -1961291236 | | -1961291236 | ||
| 2007-12-12 | | 2007-12-12 | ||
− | | | + | | |
| I stopped by to check the plugging status of this well. Nobody was on location and the lease road was gated closed. | | I stopped by to check the plugging status of this well. Nobody was on location and the lease road was gated closed. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| -272625254 | | -272625254 | ||
| 2007-07-24 | | 2007-07-24 | ||
− | | | + | | |
| Jeff Fry and I stopped by to check on the status of plugging progress of this well, however there was nobody on location. | | Jeff Fry and I stopped by to check on the status of plugging progress of this well, however there was nobody on location. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| -594031884 | | -594031884 | ||
| 2007-05-08 | | 2007-05-08 | ||
− | | | + | | |
| Two twenty tons jacks were used to try and pull the tubing. This was tried several times with no success. They have scheduled for power tongs to come in the morning and will try again tomorrow. | | Two twenty tons jacks were used to try and pull the tubing. This was tried several times with no success. They have scheduled for power tongs to come in the morning and will try again tomorrow. | ||
− | + | | | |
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− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
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− | |||
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− | |||
− | |||
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− | |||
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− | |||
− | | | ||
− | | | ||
− | | | ||
|- | |- | ||
|- | |- | ||
| 63793951 | | 63793951 | ||
| 2007-05-23 | | 2007-05-23 | ||
− | | | + | | |
| I witnessed plugging operations today. | | I witnessed plugging operations today. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-089-23306 | Loading map...
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County: Licking | |
Municipality: | |
Operator Name: L & S OIL AND GAS | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Plugged and Abandoned | |
Violations: 0 | |
Latitude: 40.00528331 | |
Longitude: -82.22603324 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1984-0 | 0.0 | 1015.0 | ||||
1985-0 | 0.0 | 1015.0 | ||||
1986-0 | 0.0 | 415.0 | ||||
1987-0 | 0.0 | 415.0 | ||||
1988-0 | 0.0 | 463.0 | ||||
1989-0 | 0.0 | 213.0 | ||||
1990-0 | 0.0 | 276.0 | ||||
1991-0 | 0.0 | 213.0 | ||||
1997-0 | 0.0 | 218.0 | ||||
1998-0 | 0.0 | 259.0 | ||||
1999-0 | 0.0 | 228.0 | ||||
2000-0 | 0.0 | 218.0 | ||||
2001-0 | 0.0 | 150.0 | ||||
2002-0 | 0.0 | 164.0 | ||||
2003-0 | 0.0 | 122.0 | ||||
2004-0 | 0.0 | 0.0 | ||||
2005-0 | 0.0 | 0.0 | ||||
2007-0 | 0.0 | 190.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1178803510 | 2007-05-09 | John Loveridge hired Mike's Power Tong Service to come and turn on the tubing to try and free it up. They tried several things. They were able to unscrew a couple of time above the tool, but never below the tool. They gave up and are going to try jacking it out with a bigger set a jacks. | ||||
1179150236 | 2007-05-07 | Two 100 ton jacks were used to try and break the tubing free. They jacked on it with a lot of pressure and were afraid to go any farther. They decided to let it sit overnight with the pressure on it. | ||||
-118864792 | 2007-05-07 | I inspected this well with Jeff Fry. John Loveridge is plugging the well. The tubing parted at 1200 feet. There is a colar looking up that has part threads in it. He ran back in with a 2 inch spear and grabbed a hold of the tubing. Now he can't go up or down. | ||||
1347560630 | 2007-05-15 | I stopped by to witness plugging operations today. They are still trying to pull the tubing with two 100 ton jacks. There is about 3 feet of stretch on the tubing. | ||||
-1639980443 | 2007-05-24 | I witnessed plugging operations today. | ||||
-1651729685 | 2007-05-14 | I stopped by well to see what progress has been made on the plugging operations. The tubing is still stuck in the hole and they are continuing to put pressure on the tubing with two 100 ton jacks. | ||||
1714346694 | 2007-07-18 | I stopped by the well location today to check on the plugging progress. Nobody was on location. They are still rigged up on the well and trying to recover the tubing and tool that is stuck in the hole. | ||||
-1744642278 | 2007-06-11 | I witnessed plugging operations today. | ||||
-1961291236 | 2007-12-12 | I stopped by to check the plugging status of this well. Nobody was on location and the lease road was gated closed. | ||||
-272625254 | 2007-07-24 | Jeff Fry and I stopped by to check on the status of plugging progress of this well, however there was nobody on location. | ||||
-594031884 | 2007-05-08 | Two twenty tons jacks were used to try and pull the tubing. This was tried several times with no success. They have scheduled for power tongs to come in the morning and will try again tomorrow. | ||||
63793951 | 2007-05-23 | I witnessed plugging operations today. |
For data sources see[2]