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Difference between revisions of "34-005-20338"

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__TOC__
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__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-005-20338
 
| Well ID: 34-005-20338
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.77993905, -82.34690801 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.779881945, -82.34702305 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Ashland County, Ohio|Ashland]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 
|-
 
|-
| Operator Name: [[COLUMBIA GAS TRANSMISSION]]
+
| County: [[Ashland_County,_Ohio|Ashland]]
 +
|-
 +
| Municipality: [[Mifflin_Township,_Ashland_County,_Ohio|Mifflin Township]]
 +
|-
 +
| Operator Name: [[COLUMBIA GAS TRANSMISSION LLC]]
 
|-
 
|-
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: SHERIFF ESTELLA
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2014-02-20
 
|-
 
|-
 
| Spud Date: 1947-01-13
 
| Spud Date: 1947-01-13
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:  
 
|-
 
|-
| Configuration: Vertical
+
| Final Drill Date: 1947-02-28
 
|-
 
|-
| Well Status: Final Restoration
+
| Well Total Depth: 2730 ft
 
|-
 
|-
| Violations: 0
+
| Configuration: Vertical
|-
 
| Latitude: 40.77993905
 
 
|-
 
|-
| Longitude: -82.34690801
+
| Latitude: 40.779881945
 
|-
 
|-
 +
| Longitude: -82.34702305
 
|}
 
|}
== Inspection Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Well Status
!scope="col" | DATE
+
!scope="col" style="width: 15%;text-align: center"| Well Status Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Comment
!scope="col" | COMMENT
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
| 1386193791
+
| Original Spud
| 2013-12-04
+
| 1947-01-13
|
 
| The operator requested an inspection to witness setting the surface plug.
 
 
|  
 
|  
 +
|-
 +
| Completed
 +
| 1947-02-28
 
|  
 
|  
 +
|-
 +
| Reached Total Depth
 +
| 1947-02-28
 
|  
 
|  
 
|-
 
|-
 +
| APP
 +
| 2013-11-08
 +
| Proposed Formations:CLINTON, Issued Date:11/8/2013, Expired Date:11/8/2015 12:00:00 PM, Drilling unit acres:100, Proposed Well Type:SO, Proposed Well Class:
 
|-
 
|-
| 1386610438
+
| Plugged/Abandoned
| 2013-12-06
+
| 2013-12-04
|
 
| The operator has started restoring the site.  Whan Incorporated is the excavating contractor on location.  Oil was spilled on location during plugging of the Berea Formation.  Oil was contained on site and pumped to portable tanks.  Contaminated soil is being loaded into dumpsters.  No personnel on site today, location is very muddy, snowing.
 
 
|  
 
|  
 +
|-
 +
| Construction Permit Expires
 +
| 2015-11-08
 
|  
 
|  
 +
|-
 +
| Record Last Modified
 +
| 2017-02-10
 
|  
 
|  
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 +
<!--== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 1484866153
+
|}-->
| 2013-11-27
+
<!--== Waste Data ==
|  
+
{| class="wikitable sortable"
| The operator cut the 3.5 inch casing at 1800ft.  The 3.5 inch is being recovered.
+
!scope="col" style="text-align: center"| Period
|  
+
!scope="col" style="text-align: center"| Operator Name
|  
+
!scope="col" style="text-align: center"| Waste Type
|  
+
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
|}-->
 +
== Inspection Data ==
 +
==== Inspections Performed ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Inspection Date
 +
!scope="col" style="text-align: center"| Inspection Type
 +
!scope="col" style="text-align: center"| Inspection Result
 +
!scope="col" style="text-align: center"| Inspection Comments
 
|-
 
|-
| 187284207
+
| 0187284207
 
| 2014-02-20
 
| 2014-02-20
|  
+
| Final Restoration
 +
| No Violations
 
| Columbia Gas provided a waiver from the landowner allowing the access road to remain in place.  The remainder of restoration at the site is approved.
 
| Columbia Gas provided a waiver from the landowner allowing the access road to remain in place.  The remainder of restoration at the site is approved.
|
 
|
 
|
 
 
|-
 
|-
 +
| 1386193791
 +
| 2013-12-04
 +
| Storage Well
 +
| No Violations
 +
| The operator requested an inspection to witness setting the surface plug.
 +
|-
 +
| 1386610438
 +
| 2013-12-06
 +
| Final Restoration
 +
| No Violations
 +
| The operator has started restoring the site.  Whan Incorporated is the excavating contractor on location.  Oil was spilled on location during plugging of the Berea Formation.  Oil was contained on site and pumped to portable tanks.  Contaminated soil is being loaded into dumpsters.  No personnel on site today, location is very muddy, snowing.
 +
|-
 +
| 1484866153
 +
| 2013-11-27
 +
| Plug / Plug Back
 +
| No Violations
 +
| The operator cut the 3.5 inch casing at 1800ft.  The 3.5 inch is being recovered.
 
|-
 
|-
 
| 2145059732
 
| 2145059732
 
| 2013-11-26
 
| 2013-11-26
|  
+
| Storage Well
 +
| No Violations
 
| Requested by the operator to witness setting the bottom plug in the well.  See the plug report for details.
 
| Requested by the operator to witness setting the bottom plug in the well.  See the plug report for details.
|
 
|
 
|
 
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 00:15, 24 July 2019

Well Details

Well ID: 34-005-20338
Loading map...
Country: United States
State: Ohio
County: Ashland
Municipality: Mifflin Township
Operator Name: COLUMBIA GAS TRANSMISSION LLC
Well Pad ID:
Farm/Lease Name: SHERIFF ESTELLA
License Status: Final Restoration
License Date: 2014-02-20
Spud Date: 1947-01-13
Spud Drilling Contractor:
Final Drill Date: 1947-02-28
Well Total Depth: 2730 ft
Configuration: Vertical
Latitude: 40.779881945
Longitude: -82.34702305

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1947-01-13
Completed 1947-02-28
Reached Total Depth 1947-02-28
APP 2013-11-08 Proposed Formations:CLINTON, Issued Date:11/8/2013, Expired Date:11/8/2015 12:00:00 PM, Drilling unit acres:100, Proposed Well Type:SO, Proposed Well Class:
Plugged/Abandoned 2013-12-04
Construction Permit Expires 2015-11-08
Record Last Modified 2017-02-10

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0187284207 2014-02-20 Final Restoration No Violations Columbia Gas provided a waiver from the landowner allowing the access road to remain in place. The remainder of restoration at the site is approved.
1386193791 2013-12-04 Storage Well No Violations The operator requested an inspection to witness setting the surface plug.
1386610438 2013-12-06 Final Restoration No Violations The operator has started restoring the site. Whan Incorporated is the excavating contractor on location. Oil was spilled on location during plugging of the Berea Formation. Oil was contained on site and pumped to portable tanks. Contaminated soil is being loaded into dumpsters. No personnel on site today, location is very muddy, snowing.
1484866153 2013-11-27 Plug / Plug Back No Violations The operator cut the 3.5 inch casing at 1800ft. The 3.5 inch is being recovered.
2145059732 2013-11-26 Storage Well No Violations Requested by the operator to witness setting the bottom plug in the well. See the plug report for details.

For data sources see[3]

References