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Difference between revisions of "34-005-23493"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-005-23493
 
| Well ID: 34-005-23493
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.8863524, -82.17329413 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.886295933, -82.17341614 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Ashland County, Ohio|Ashland]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 
|-
 
|-
| Operator Name: [[SHORTS RALPH E DRILLING]]
+
| County: [[Ashland_County,_Ohio|Ashland]]
 +
|-
 +
| Municipality: [[Perry_Township,_Ashland_County,_Ohio|Perry Township]]
 +
|-
 +
| Operator Name: [[RALPH E SHORTS DRILLING]]
 
|-
 
|-
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: FRONTZ ROY
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 1998-10-19
 
|-
 
|-
 
| Spud Date: 1982-07-20
 
| Spud Date: 1982-07-20
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor: [[SHORTS DRLG]]
 +
|-
 +
| Final Drill Date: 1982-07-22
 +
|-
 +
| Well Total Depth: 790 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Producing
+
| Latitude: 40.886295933
 +
|-
 +
| Longitude: -82.17341614
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| Oil and Gas
 +
| 1982-03-03
 +
| Issued Date 3/4/82 Expired Date 8/31/82 Acres 0002500 Tool Type RTAF Proposed Formation BEREA Proposed Depth 00790 Proposed Drill Depth 00790
 +
|-
 +
| Original Spud
 +
| 1982-07-20
 +
| IPN. OIL = 1/2 BBL.
 +
|-
 +
| Completed
 +
| 1982-07-22
 +
| IPN. OIL = 1/2 BBL.
 +
|-
 +
| Reached Total Depth
 +
| 1982-07-22
 +
| IPN. OIL = 1/2 BBL.
 +
|-
 +
| CO
 +
| 1982-07-28
 +
| 270  SHORTS RALPH E DRILLING  GeoDate  3/3/82
 +
|-
 +
| Completion Report Received
 +
| 1984-10-11
 +
| IPN. OIL = 1/2 BBL.
 +
|-
 +
| CO
 +
| 1994-03-22
 +
| 270  SHORTS RALPH E DRILLING  GeoDate  3/22/94
 +
|-
 +
| Unknown
 +
| 1994-03-22
 +
| Issued Date 3/22/94 Expired Date 3/22/95 Proposed Purpose OG Was Plug Supervised  Who Superivsed Plug and Abandon Date
 +
|-
 +
| CO
 +
| 1996-10-03
 +
| 270  SHORTS RALPH E DRILLING  GeoDate  10/3/96
 +
|-
 +
| Unknown
 +
| 1996-10-03
 +
| Issued Date 10/3/96 Expired Date 10/3/97 Proposed Purpose OG Was Plug Supervised  Who Superivsed Plug and Abandon Date
 +
|-
 +
| APP
 +
| 2010-07-02
 +
| Proposed Formations:BEREA, Issued Date:7/2/2010, Expired Date:7/2/2011 6:00:00 AM, Drilling unit acres:2.5, Proposed Well Type:OG, Proposed Well Class:
 
|-
 
|-
| Violations: 0
+
| APP
 +
| 2011-08-08
 +
| Proposed Formations:BEREA, Issued Date:8/8/2011, Expired Date:8/7/2013 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
 
|-
 
|-
| Latitude: 40.8863524
+
| APP
 +
| 2014-04-15
 +
| Proposed Formations:BEREA, Issued Date:4/15/2014, Expired Date:4/14/2016 12:00:00 PM, Drilling unit acres:2.5, Proposed Well Type:OG, Proposed Well Class:
 
|-
 
|-
| Longitude: -82.17329413
+
| Plugged/Abandoned
 +
| 2015-10-23
 +
| IPN. OIL = 1/2 BBL.
 +
|-
 +
| Construction Permit Expires
 +
| 2016-04-14
 +
| IPN. OIL = 1/2 BBL.
 +
|-
 +
| Record Last Modified
 +
| 2017-02-15
 +
| IPN. OIL = 1/2 BBL.
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
| 1997-06-29
 +
| style="text-align: right;" | 718
 +
| style="text-align: right;" | 760
 +
| style="text-align: right;" | 0
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
== Stimulations Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Stimulation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Chemical Agent
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Fracking Fluid Volume
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
!scope="col" | OIL QUANTITY
+
!scope="col" style="text-align: center"| Fracking Company
!scope="col" | OIL PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 1984-0
 
| style="text-align:right;" | 0.0
 
 
|  
 
|  
 +
| Not Treated
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 42 Qts
 +
| style="text-align: right;" | 0
 
|  
 
|  
|  
+
| SHOT: 42 QT NITRO
| style="text-align:right;" | 71.0
+
|-
|  
+
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 1984
 +
| [[RALPH E SHORTS DRILLING]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 71
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1985
 +
| [[RALPH E SHORTS DRILLING]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 38
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1987
 +
| [[RALPH E SHORTS DRILLING]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 38
 +
| style="text-align: right;" | 365
 
|-
 
|-
 +
| 1988
 +
| [[RALPH E SHORTS DRILLING]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 33
 +
| style="text-align: right;" | 180
 
|-
 
|-
| 1985-0
+
| 1992
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 26
|  
+
| style="text-align: right;" | 53
| style="text-align:right;" | 38.0
 
|
 
 
|-
 
|-
 +
| 1993
 +
| [[RALPH E SHORTS DRILLING]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1987-0
+
| 1995
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 38.0
 
|
 
 
|-
 
|-
 +
| 1996
 +
| [[RALPH E SHORTS DRILLING]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1988-0
+
| 1999
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 33.0
 
|
 
 
|-
 
|-
 +
| 2000
 +
| [[RALPH E SHORTS DRILLING]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1992-0
+
| 2001
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 26.0
 
|
 
 
|-
 
|-
 +
| 2002
 +
| [[RALPH E SHORTS DRILLING]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1993-0
+
| 2003
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2004
 +
| [[RALPH E SHORTS DRILLING]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1995-0
+
| 2005
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2006
 +
| [[RALPH E SHORTS DRILLING]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1996-0
+
| 2007
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2009
 +
| [[RALPH E SHORTS DRILLING]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1999-0
+
| 2010
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2011
 +
| [[RALPH E SHORTS DRILLING]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2000-0
+
| 2012
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2013
 +
| [[RALPH E SHORTS DRILLING]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2001-0
+
| 2014
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 335
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 2002-0
+
| 1984
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1985
 +
| [[RALPH E SHORTS DRILLING]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2003-0
+
| 1987
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1988
 +
| [[RALPH E SHORTS DRILLING]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 180
 
|-
 
|-
| 2004-0
+
| 1992
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 53
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1993
 +
| [[RALPH E SHORTS DRILLING]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2005-0
+
| 1995
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1996
 +
| [[RALPH E SHORTS DRILLING]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2006-0
+
| 1999
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2000
 +
| [[RALPH E SHORTS DRILLING]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2007-0
+
| 2001
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2002
 +
| [[RALPH E SHORTS DRILLING]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2009-0
+
| 2003
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2004
 +
| [[RALPH E SHORTS DRILLING]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2010-0
+
| 2005
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2006
 +
| [[RALPH E SHORTS DRILLING]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2011-0
+
| 2007
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2009
 +
| [[RALPH E SHORTS DRILLING]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2012-0
+
| 2010
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2011
 +
| [[RALPH E SHORTS DRILLING]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2013-0
+
| 2012
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2013
 +
| [[RALPH E SHORTS DRILLING]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2014-0
+
| 2014
| style="text-align:right;" | 0.0
+
| [[RALPH E SHORTS DRILLING]]
| style="text-align:right;" | 335.0
+
| Brine
|  
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 335
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 335.0
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2019-05-07
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2019-05-21 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
| -917736240
+
| 0191275220
 +
| 2015-12-02
 +
| Plug / Plug Back
 +
| No Violations
 +
| Cement has dropped in the well.  Ralph Shorts was advised to top up cement when he completes final restoration on the well.  He said he would do so and contact the inspector at that time.  The well was incorrectly given final restored status in 1998 by Mike Phelps.
 +
|-
 +
| 0194307156
 +
| 2016-07-21
 +
| Final Restoration
 +
| No Violations
 +
| The operator cut off the casing and topped up the well with dry bagged cement.  A plate was welded on the casing and the location was backfilled and graded.  There is no road to the well.  The landowner was on site while the work was done and will be providing a waiver to leave flowlines in place.  Mike Phelps incorrectly approved final restoration for the well in 1998.  All surface equipment is gone.
 +
|-
 +
| 0917736240
 
| 2014-04-02
 
| 2014-04-02
|  
+
| Production Wells
 +
| No Violations
 
| The well is located in a feed lot behind a barn.  Rods and tubing have been stripped.  The well is not in production.  The operator stated that he has applied for a plug permit on the well.
 
| The well is located in a feed lot behind a barn.  Rods and tubing have been stripped.  The well is not in production.  The operator stated that he has applied for a plug permit on the well.
|
 
|
 
|
 
 
|-
 
|-
 +
| 0974487480
 +
| 2017-02-21
 +
| Final Restoration
 +
| No Violations
 +
| The landowner submitted a waiver for buried flow lines.  The waiver is approved.  Final restoration is approved.
 +
|-
 +
| 1445617838
 +
| 2015-10-23
 +
| Plug / Plug Back
 +
| No Violations
 +
| The operator requested an inspection to witness plugging the well.  See the plug report for details.
 
|-
 
|-
| iDIAN000259
+
| iDIAN00025
 
| 1998-10-19
 
| 1998-10-19
|  
+
| Final Restoration
|  
+
| No Violations
|
 
|
 
 
|  
 
|  
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 06:25, 24 July 2019

Well Details

Well ID: 34-005-23493
Loading map...
Country: United States
State: Ohio
County: Ashland
Municipality: Perry Township
Operator Name: RALPH E SHORTS DRILLING
Well Pad ID:
Farm/Lease Name: FRONTZ ROY
License Status: Final Restoration
License Date: 1998-10-19
Spud Date: 1982-07-20
Spud Drilling Contractor: SHORTS DRLG
Final Drill Date: 1982-07-22
Well Total Depth: 790 ft
Configuration: Vertical
Latitude: 40.886295933
Longitude: -82.17341614

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1982-03-03 Issued Date 3/4/82 Expired Date 8/31/82 Acres 0002500 Tool Type RTAF Proposed Formation BEREA Proposed Depth 00790 Proposed Drill Depth 00790
Original Spud 1982-07-20 IPN. OIL = 1/2 BBL.
Completed 1982-07-22 IPN. OIL = 1/2 BBL.
Reached Total Depth 1982-07-22 IPN. OIL = 1/2 BBL.
CO 1982-07-28 270 SHORTS RALPH E DRILLING GeoDate 3/3/82
Completion Report Received 1984-10-11 IPN. OIL = 1/2 BBL.
CO 1994-03-22 270 SHORTS RALPH E DRILLING GeoDate 3/22/94
Unknown 1994-03-22 Issued Date 3/22/94 Expired Date 3/22/95 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
CO 1996-10-03 270 SHORTS RALPH E DRILLING GeoDate 10/3/96
Unknown 1996-10-03 Issued Date 10/3/96 Expired Date 10/3/97 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
APP 2010-07-02 Proposed Formations:BEREA, Issued Date:7/2/2010, Expired Date:7/2/2011 6:00:00 AM, Drilling unit acres:2.5, Proposed Well Type:OG, Proposed Well Class:
APP 2011-08-08 Proposed Formations:BEREA, Issued Date:8/8/2011, Expired Date:8/7/2013 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
APP 2014-04-15 Proposed Formations:BEREA, Issued Date:4/15/2014, Expired Date:4/14/2016 12:00:00 PM, Drilling unit acres:2.5, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2015-10-23 IPN. OIL = 1/2 BBL.
Construction Permit Expires 2016-04-14 IPN. OIL = 1/2 BBL.
Record Last Modified 2017-02-15 IPN. OIL = 1/2 BBL.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 718 760 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
Not Treated 0 42 Qts 0 SHOT: 42 QT NITRO

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 RALPH E SHORTS DRILLING 0 71 0
1985 RALPH E SHORTS DRILLING 0 38 365
1987 RALPH E SHORTS DRILLING 0 38 365
1988 RALPH E SHORTS DRILLING 0 33 180
1992 RALPH E SHORTS DRILLING 0 26 53
1993 RALPH E SHORTS DRILLING 0 0 0
1995 RALPH E SHORTS DRILLING 0 0 0
1996 RALPH E SHORTS DRILLING 0 0 0
1999 RALPH E SHORTS DRILLING 0 0 0
2000 RALPH E SHORTS DRILLING 0 0 0
2001 RALPH E SHORTS DRILLING 0 0 0
2002 RALPH E SHORTS DRILLING 0 0 0
2003 RALPH E SHORTS DRILLING 0 0 0
2004 RALPH E SHORTS DRILLING 0 0 0
2005 RALPH E SHORTS DRILLING 0 0 0
2006 RALPH E SHORTS DRILLING 0 0 0
2007 RALPH E SHORTS DRILLING 0 0 0
2009 RALPH E SHORTS DRILLING 0 0 0
2010 RALPH E SHORTS DRILLING 0 0 365
2011 RALPH E SHORTS DRILLING 0 0 0
2012 RALPH E SHORTS DRILLING 0 0 0
2013 RALPH E SHORTS DRILLING 0 0 0
2014 RALPH E SHORTS DRILLING 0 0 335

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 RALPH E SHORTS DRILLING Brine 0 0
1985 RALPH E SHORTS DRILLING Brine 0 365
1987 RALPH E SHORTS DRILLING Brine 0 365
1988 RALPH E SHORTS DRILLING Brine 0 180
1992 RALPH E SHORTS DRILLING Brine 0 53
1993 RALPH E SHORTS DRILLING Brine 0 0
1995 RALPH E SHORTS DRILLING Brine 0 0
1996 RALPH E SHORTS DRILLING Brine 0 0
1999 RALPH E SHORTS DRILLING Brine 0 0
2000 RALPH E SHORTS DRILLING Brine 0 0
2001 RALPH E SHORTS DRILLING Brine 0 0
2002 RALPH E SHORTS DRILLING Brine 0 0
2003 RALPH E SHORTS DRILLING Brine 0 0
2004 RALPH E SHORTS DRILLING Brine 0 0
2005 RALPH E SHORTS DRILLING Brine 0 0
2006 RALPH E SHORTS DRILLING Brine 0 0
2007 RALPH E SHORTS DRILLING Brine 0 0
2009 RALPH E SHORTS DRILLING Brine 0 0
2010 RALPH E SHORTS DRILLING Brine 0 365
2011 RALPH E SHORTS DRILLING Brine 0 0
2012 RALPH E SHORTS DRILLING Brine 0 0
2013 RALPH E SHORTS DRILLING Brine 0 0
2014 RALPH E SHORTS DRILLING Brine 0 335

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0191275220 2015-12-02 Plug / Plug Back No Violations Cement has dropped in the well. Ralph Shorts was advised to top up cement when he completes final restoration on the well. He said he would do so and contact the inspector at that time. The well was incorrectly given final restored status in 1998 by Mike Phelps.
0194307156 2016-07-21 Final Restoration No Violations The operator cut off the casing and topped up the well with dry bagged cement. A plate was welded on the casing and the location was backfilled and graded. There is no road to the well. The landowner was on site while the work was done and will be providing a waiver to leave flowlines in place. Mike Phelps incorrectly approved final restoration for the well in 1998. All surface equipment is gone.
0917736240 2014-04-02 Production Wells No Violations The well is located in a feed lot behind a barn. Rods and tubing have been stripped. The well is not in production. The operator stated that he has applied for a plug permit on the well.
0974487480 2017-02-21 Final Restoration No Violations The landowner submitted a waiver for buried flow lines. The waiver is approved. Final restoration is approved.
1445617838 2015-10-23 Plug / Plug Back No Violations The operator requested an inspection to witness plugging the well. See the plug report for details.
iDIAN00025 1998-10-19 Final Restoration No Violations

For data sources see[9]

References