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Difference between revisions of "34-035-21200"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-035-21200
 
| Well ID: 34-035-21200
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.2898224, -81.61803524 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.289908487, -81.61578448 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Cuyahoga County, Ohio|Cuyahoga]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Cuyahoga_County,_Ohio|Cuyahoga]]
 +
|-
 +
| Municipality: [[Brecksville,_Ohio|Brecksville]]
 
|-
 
|-
 
| Operator Name: [[NORTHWOOD ENERGY CORP]]
 
| Operator Name: [[NORTHWOOD ENERGY CORP]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: GOODRICH B F
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2003-09-11
 
|-
 
|-
 
| Spud Date: 1984-02-20
 
| Spud Date: 1984-02-20
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor: [[NANCY DRLG]]
 +
|-
 +
| Final Drill Date: 1984-02-26
 +
|-
 +
| Well Total Depth: 3620 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Final Restoration
+
| Latitude: 41.289908487
 +
|-
 +
| Longitude: -81.61578448
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| Oil and Gas
 +
| 1983-07-20
 +
| Issued Date 7/20/83 Expired Date 1/16/84 Acres 0020000 Tool Type CRAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
 +
|-
 +
| CO
 +
| 1984-02-07
 +
| 1422  WINDSOR ASSOCIATES INC  GeoDate  2/7/84
 
|-
 
|-
| Violations: 0
+
| Oil and Gas
 +
| 1984-02-07
 +
| Issued Date 2/7/84 Expired Date 8/5/84 Acres 0020000 Tool Type RTF Proposed Formation CLINTON Proposed Depth 03620 Proposed Drill Depth 03620
 
|-
 
|-
| Latitude: 41.2898224
+
| Original Spud
 +
| 1984-02-20
 +
| PLUGGED: 10/24/2000 R.I. 2-11-84
 
|-
 
|-
| Longitude: -81.61803524
+
| Completed
 +
| 1984-02-26
 +
| PLUGGED: 10/24/2000 R.I. 2-11-84
 +
|-
 +
| Reached Total Depth
 +
| 1984-02-26
 +
| PLUGGED: 10/24/2000 R.I. 2-11-84
 +
|-
 +
| CO
 +
| 1984-05-29
 +
| 13  APPALACHIAN EXPL INC  GeoDate  7/20/83
 +
|-
 +
| Completion Report Received
 +
| 1984-06-22
 +
| PLUGGED: 10/24/2000 R.I. 2-11-84
 +
|-
 +
| Revocation
 +
| 1989-05-11
 +
| PLUGGED: 10/24/2000 R.I. 2-11-84
 +
|-
 +
| CO
 +
| 1991-09-30
 +
| 213  LOMAK OPERATING CO  GeoDate  2/7/84
 +
|-
 +
| CO
 +
| 1992-07-14
 +
| 1634  NORTHWOOD ENERGY CORP  GeoDate  2/7/84
 +
|-
 +
| APP
 +
| 2000-08-17
 +
| Proposed Formations:CLINTON, Issued Date:8/17/00, Expired Date:8/17/01 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:TAAD, Proposed Well Class:
 +
|-
 +
| Construction Permit Expires
 +
| 2001-08-17
 +
| PLUGGED: 10/24/2000 R.I. 2-11-84
 +
|-
 +
| Plugged/Abandoned
 +
| 2002-06-04
 +
| PLUGGED: 10/24/2000 R.I. 2-11-84
 +
|-
 +
| Record Last Modified
 +
| 2019-04-03
 +
| PLUGGED: 10/24/2000 R.I. 2-11-84
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
| 2006-09-11
 +
| style="text-align: right;" | 3492
 +
| style="text-align: right;" | 3513
 +
| style="text-align: right;" | 12
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
== Stimulations Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Stimulation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Chemical Agent
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Fracking Fluid Volume
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
!scope="col" | OIL QUANTITY
+
!scope="col" style="text-align: center"| Fracking Company
!scope="col" | OIL PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 1984-0
 
| style="text-align:right;" | 3268.0
 
 
|  
 
|  
 +
| H2O
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 68500 Gal
 +
| style="text-align: right;" | 50000
 
|  
 
|  
|  
+
| FRAC;H2O,SAND
| style="text-align:right;" | 303.0
+
|-
|  
+
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 1984
 +
| [[WINDSOR ASSOCIATES INC]]
 +
| style="text-align: right;" | 3268
 +
| style="text-align: right;" | 303
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1985
 +
| [[WINDSOR ASSOCIATES INC]]
 +
| style="text-align: right;" | 4176
 +
| style="text-align: right;" | 282
 +
| style="text-align: right;" | 351
 +
|-
 +
| 1986
 +
| [[WINDSOR ASSOCIATES INC]]
 +
| style="text-align: right;" | 3289
 +
| style="text-align: right;" | 158
 +
| style="text-align: right;" | 349
 
|-
 
|-
 +
| 1987
 +
| [[WINDSOR ASSOCIATES INC]]
 +
| style="text-align: right;" | 2612
 +
| style="text-align: right;" | 162
 +
| style="text-align: right;" | 329
 
|-
 
|-
| 1985-0
+
| 1988
| style="text-align:right;" | 4176.0
+
| [[WINDSOR ASSOCIATES INC]]
|  
+
| style="text-align: right;" | 1383
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 325
| style="text-align:right;" | 282.0
 
|
 
 
|-
 
|-
 +
| 1989
 +
| [[WINDSOR ASSOCIATES INC]]
 +
| style="text-align: right;" | 1237
 +
| style="text-align: right;" | 64
 +
| style="text-align: right;" | 302
 
|-
 
|-
| 1986-0
+
| 1990
| style="text-align:right;" | 3289.0
+
| [[WINDSOR ASSOCIATES INC]]
|  
+
| style="text-align: right;" | 893
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 158.0
 
|
 
 
|-
 
|-
 +
| 1991
 +
| [[WINDSOR ASSOCIATES INC]]
 +
| style="text-align: right;" | 1000
 +
| style="text-align: right;" | 156
 +
| style="text-align: right;" | 260
 
|-
 
|-
| 1987-0
+
| 1992
| style="text-align:right;" | 2612.0
+
| [[NORTHWOOD ENERGY CORP]]
|  
+
| style="text-align: right;" | 766
|
+
| style="text-align: right;" | 61
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 162.0
 
|
 
 
|-
 
|-
 +
| 1993
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| style="text-align: right;" | 1119
 +
| style="text-align: right;" | 83
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1988-0
+
| 1994
| style="text-align:right;" | 1383.0
+
| [[NORTHWOOD ENERGY CORP]]
|  
+
| style="text-align: right;" | 1105
|
+
| style="text-align: right;" | 50
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1996
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| style="text-align: right;" | 97
 +
| style="text-align: right;" | 40
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1989-0
+
| 1997
| style="text-align:right;" | 1237.0
+
| [[NORTHWOOD ENERGY CORP]]
|  
+
| style="text-align: right;" | 78
|
+
| style="text-align: right;" | 2
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 64.0
 
|
 
 
|-
 
|-
 +
| 1998
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1990-0
+
| 1999
| style="text-align:right;" | 893.0
+
| [[NORTHWOOD ENERGY CORP]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2000
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1991-0
+
| 2001
| style="text-align:right;" | 1000.0
+
| [[NORTHWOOD ENERGY CORP]]
|  
+
| style="text-align: right;" | 104
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 156.0
 
|
 
 
|-
 
|-
 +
| 2002
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1992-0
+
|}
| style="text-align:right;" | 766.0
+
For data sources see<ref>{{cite web
|  
+
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
|  
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date =  2019-05-07
| style="text-align:right;" | 61.0
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
|
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
| 1984
 +
| [[WINDSOR ASSOCIATES INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1993-0
+
| 1985
| style="text-align:right;" | 1119.0
+
| [[WINDSOR ASSOCIATES INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 184
|
+
| style="text-align: right;" | 351
| style="text-align:right;" | 83.0
 
|
 
 
|-
 
|-
 +
| 1986
 +
| [[WINDSOR ASSOCIATES INC]]
 +
| Brine
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 349
 
|-
 
|-
| 1994-0
+
| 1987
| style="text-align:right;" | 1105.0
+
| [[WINDSOR ASSOCIATES INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 42
|
+
| style="text-align: right;" | 329
| style="text-align:right;" | 50.0
 
|
 
 
|-
 
|-
 +
| 1988
 +
| [[WINDSOR ASSOCIATES INC]]
 +
| Brine
 +
| style="text-align: right;" | 18
 +
| style="text-align: right;" | 325
 
|-
 
|-
| 1996-0
+
| 1989
| style="text-align:right;" | 97.0
+
| [[WINDSOR ASSOCIATES INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 5
|
+
| style="text-align: right;" | 302
| style="text-align:right;" | 40.0
 
|
 
 
|-
 
|-
 +
| 1990
 +
| [[WINDSOR ASSOCIATES INC]]
 +
| Brine
 +
| style="text-align: right;" | 29
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1997-0
+
| 1991
| style="text-align:right;" | 78.0
+
| [[WINDSOR ASSOCIATES INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 260
| style="text-align:right;" | 2.0
 
|
 
 
|-
 
|-
 +
| 1992
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 66
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1998-0
+
| 1993
| style="text-align:right;" | 0.0
+
| [[NORTHWOOD ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1994
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1999-0
+
| 1996
| style="text-align:right;" | 0.0
+
| [[NORTHWOOD ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 14
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1997
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 50
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2000-0
+
| 1998
|  
+
| [[NORTHWOOD ENERGY CORP]]
|  
+
| Brine
|  
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
|  
 
|  
 
 
|-
 
|-
 +
| 1999
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" |
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2001-0
+
| 2000
| style="text-align:right;" | 104.0
+
| [[NORTHWOOD ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" |  
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2001
 +
| [[NORTHWOOD ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" |
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2002-0
+
| 2002
| style="text-align:right;" | 0.0
+
| [[NORTHWOOD ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" |  
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2019-05-07
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2019-05-21 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
+
|-
!scope="col" | VIOLATION COMMENT
+
| 0001240i91
 +
| 2000-10-24
 +
| Plug / Plug Back
 +
| No Violations
 +
| ON SITE FOR PLUGGING GAVE PLUGS TO CEMENTORS .WILL BE LEAVEING SITE TO COVER SPILL CLEANUP.    BACK ON SITE COMPANY HAD RIPPED 4.5 2505 NOT WITNESSED SET RIP & LIME PLUG PULLING 4.5UP TO CASING PLUG  AT 470--320
 +
|-
 +
| 0001880046
 +
| 2002-05-31
 +
| Production Wells
 +
| No Violations
 +
| Drilling out well because of plug failure (gas leakage)
 
|-
 
|-
| 1.01533E+15
+
| 1015334934
 
| 2005-05-03
 
| 2005-05-03
|  
+
| Non Well
 +
| No Violations
 
| on site checked out sink hole at address 11785,11780,11795. Found the area at end of each drive at edge of wooded area.
 
| on site checked out sink hole at address 11785,11780,11795. Found the area at end of each drive at edge of wooded area.
Area at 11785 approx 15' Diam with two sinks approx 18 diam. At 11780 is behind house opposite of drive along the woods area about th
+
Area at 11785 approx 15 Diam with two sinks approx 18 diam. At 11780 is behind house opposite of drive along the woods area about th
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 1050460441
| 1.05046E+15
 
 
| 2005-06-29
 
| 2005-06-29
|  
+
| Orphan
 +
| No Violations
 
| needs work
 
| needs work
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 1108172471
| 1.10817E+14
 
 
| 2005-05-05
 
| 2005-05-05
|  
+
| Non Well
 +
| No Violations
 
| Met on site with Doug Bear with AML he looked at areas said it was a burial site for stumps wood material.He said he will look at water well logs and send letter out to landowner. Expling findings.
 
| Met on site with Doug Bear with AML he looked at areas said it was a burial site for stumps wood material.He said he will look at water well logs and send letter out to landowner. Expling findings.
  
 
Case closed
 
Case closed
|
 
|
 
|
 
|-
 
 
|-
 
|-
| 1.11444E+15
+
| 1114436289
 
| 2005-04-22
 
| 2005-04-22
|  
+
| Orphan
 +
| No Violations
 
| Inspected site found well 10 casing approx. 24 below ground level in pit dug by landowner he also hauled away soil from around well thinking it was contaminated also had tested. Gave I&O forms to get well P&A ASAP. Well leaking oil and gas
 
| Inspected site found well 10 casing approx. 24 below ground level in pit dug by landowner he also hauled away soil from around well thinking it was contaminated also had tested. Gave I&O forms to get well P&A ASAP. Well leaking oil and gas
 
and is appro
 
and is appro
|
 
|
 
|
 
|-
 
 
|-
 
|-
| 1.11565E+15
+
| 1115652045
 
| 2005-05-09
 
| 2005-05-09
|  
+
| Orphan
 +
| No Violations
 
| oil to approx 6 below top of pit.
 
| oil to approx 6 below top of pit.
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 1115920471
| 1.11592E+15
 
 
| 2005-05-11
 
| 2005-05-11
|  
+
| Orphan
 +
| No Violations
 
| Pit static oil to ground level
 
| Pit static oil to ground level
|
 
|
 
|
 
|-
 
 
|-
 
|-
| 1.11625E+15
+
| 1116254205
 
| 2005-05-03
 
| 2005-05-03
|  
+
| Orphan
 +
| No Violations
 
| checked site of pit still full of oil
 
| checked site of pit still full of oil
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 1207504990
| -1.2075E+15
 
 
| 2005-05-18
 
| 2005-05-18
|  
+
| Orphan
 +
| No Violations
 
| meeting on site with contractor.
 
| meeting on site with contractor.
|
 
|
 
|
 
|-
 
|-
 
| 1240i91
 
| 2000-10-24
 
|
 
| ON SITE FOR PLUGGING GAVE PLUGS TO CEMENTORS .WILL BE LEAVEING SITE TO COVER SPILL CLEANUP.    BACK ON SITE COMPANY HAD RIPPED 4.5 2505 NOT WITNESSED SET RIP & LIME PLUG PULLING 4.5UP TO CASING PLUG  AT 470'--320'
 
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1249537823
 
| 1249537823
 
| 2003-09-11
 
| 2003-09-11
 +
| Final Restoration
 +
| No Violations
 
|  
 
|  
|
 
|
 
|
 
|
 
|-
 
 
|-
 
|-
| -1.26384E+15
+
| 1263838795
 
| 2005-07-20
 
| 2005-07-20
|  
+
| Orphan
 +
| No Violations
 
| Cutting trees down for rig access and welding casing up to ground leval.
 
| Cutting trees down for rig access and welding casing up to ground leval.
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 1308134016
| -1.30813E+13
 
 
| 2005-07-20
 
| 2005-07-20
|  
+
| Orphan
 +
| No Violations
 
| On site with company doing work for contract to plug well welded casing to ground leval.
 
| On site with company doing work for contract to plug well welded casing to ground leval.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1551736400
 
| 1551736400
 
| 2006-07-14
 
| 2006-07-14
|  
+
| Final Restoration
 +
| No Violations
 
| well plugged and restored
 
| well plugged and restored
|
 
|
 
|
 
|-
 
 
|-
 
|-
| 1880046
+
| 3730038601
| 2002-05-31
 
|
 
| Drilling out well because of plug failure (gas leakage)
 
|
 
|
 
|
 
|-
 
|-
 
| 3.73004E+14
 
 
| 2005-05-18
 
| 2005-05-18
|  
+
| Orphan
 +
| No Violations
 
| meeting on site with contractor for bibing
 
| meeting on site with contractor for bibing
|
 
|
 
|
 
|-
 
 
|-
 
|-
| 4.60695E+14
+
| 4606952001
 
| 2005-05-19
 
| 2005-05-19
|  
+
| Orphan
 +
| No Violations
 
| meeting at site
 
| meeting at site
|
 
|
 
|
 
|-
 
 
|-
 
|-
| -6.57664E+14
+
| 6576640991
 
| 2005-05-17
 
| 2005-05-17
|  
+
| Orphan
 +
| No Violations
 
| well stil same from last inspection oil filling pit not flowing.
 
| well stil same from last inspection oil filling pit not flowing.
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 9169513201
| -9.16951E+14
 
 
| 2005-05-13
 
| 2005-05-13
|  
+
| Orphan
 +
| No Violations
 
| checking pit out
 
| checking pit out
|
 
|
 
|
 
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 15:32, 24 July 2019

Well Details

Well ID: 34-035-21200
Loading map...
Country: United States
State: Ohio
County: Cuyahoga
Municipality: Brecksville
Operator Name: NORTHWOOD ENERGY CORP
Well Pad ID:
Farm/Lease Name: GOODRICH B F
License Status: Final Restoration
License Date: 2003-09-11
Spud Date: 1984-02-20
Spud Drilling Contractor: NANCY DRLG
Final Drill Date: 1984-02-26
Well Total Depth: 3620 ft
Configuration: Vertical
Latitude: 41.289908487
Longitude: -81.61578448

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1983-07-20 Issued Date 7/20/83 Expired Date 1/16/84 Acres 0020000 Tool Type CRAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1984-02-07 1422 WINDSOR ASSOCIATES INC GeoDate 2/7/84
Oil and Gas 1984-02-07 Issued Date 2/7/84 Expired Date 8/5/84 Acres 0020000 Tool Type RTF Proposed Formation CLINTON Proposed Depth 03620 Proposed Drill Depth 03620
Original Spud 1984-02-20 PLUGGED: 10/24/2000 R.I. 2-11-84
Completed 1984-02-26 PLUGGED: 10/24/2000 R.I. 2-11-84
Reached Total Depth 1984-02-26 PLUGGED: 10/24/2000 R.I. 2-11-84
CO 1984-05-29 13 APPALACHIAN EXPL INC GeoDate 7/20/83
Completion Report Received 1984-06-22 PLUGGED: 10/24/2000 R.I. 2-11-84
Revocation 1989-05-11 PLUGGED: 10/24/2000 R.I. 2-11-84
CO 1991-09-30 213 LOMAK OPERATING CO GeoDate 2/7/84
CO 1992-07-14 1634 NORTHWOOD ENERGY CORP GeoDate 2/7/84
APP 2000-08-17 Proposed Formations:CLINTON, Issued Date:8/17/00, Expired Date:8/17/01 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:TAAD, Proposed Well Class:
Construction Permit Expires 2001-08-17 PLUGGED: 10/24/2000 R.I. 2-11-84
Plugged/Abandoned 2002-06-04 PLUGGED: 10/24/2000 R.I. 2-11-84
Record Last Modified 2019-04-03 PLUGGED: 10/24/2000 R.I. 2-11-84

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3492 3513 12

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 68500 Gal 50000 FRAC;H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 WINDSOR ASSOCIATES INC 3268 303 0
1985 WINDSOR ASSOCIATES INC 4176 282 351
1986 WINDSOR ASSOCIATES INC 3289 158 349
1987 WINDSOR ASSOCIATES INC 2612 162 329
1988 WINDSOR ASSOCIATES INC 1383 0 325
1989 WINDSOR ASSOCIATES INC 1237 64 302
1990 WINDSOR ASSOCIATES INC 893 0 365
1991 WINDSOR ASSOCIATES INC 1000 156 260
1992 NORTHWOOD ENERGY CORP 766 61 365
1993 NORTHWOOD ENERGY CORP 1119 83 365
1994 NORTHWOOD ENERGY CORP 1105 50 365
1996 NORTHWOOD ENERGY CORP 97 40 365
1997 NORTHWOOD ENERGY CORP 78 2 365
1998 NORTHWOOD ENERGY CORP 0 0 365
1999 NORTHWOOD ENERGY CORP 0 0 365
2000 NORTHWOOD ENERGY CORP 0 0 365
2001 NORTHWOOD ENERGY CORP 104 0 365
2002 NORTHWOOD ENERGY CORP 0 0 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 WINDSOR ASSOCIATES INC Brine 0 0
1985 WINDSOR ASSOCIATES INC Brine 184 351
1986 WINDSOR ASSOCIATES INC Brine 100 349
1987 WINDSOR ASSOCIATES INC Brine 42 329
1988 WINDSOR ASSOCIATES INC Brine 18 325
1989 WINDSOR ASSOCIATES INC Brine 5 302
1990 WINDSOR ASSOCIATES INC Brine 29 365
1991 WINDSOR ASSOCIATES INC Brine 0 260
1992 NORTHWOOD ENERGY CORP Brine 66 365
1993 NORTHWOOD ENERGY CORP Brine 0 365
1994 NORTHWOOD ENERGY CORP Brine 0 365
1996 NORTHWOOD ENERGY CORP Brine 14 365
1997 NORTHWOOD ENERGY CORP Brine 50 365
1998 NORTHWOOD ENERGY CORP Brine 0 365
1999 NORTHWOOD ENERGY CORP Brine 365
2000 NORTHWOOD ENERGY CORP Brine 365
2001 NORTHWOOD ENERGY CORP Brine 365
2002 NORTHWOOD ENERGY CORP Brine 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0001240i91 2000-10-24 Plug / Plug Back No Violations ON SITE FOR PLUGGING GAVE PLUGS TO CEMENTORS .WILL BE LEAVEING SITE TO COVER SPILL CLEANUP. BACK ON SITE COMPANY HAD RIPPED 4.5 2505 NOT WITNESSED SET RIP & LIME PLUG PULLING 4.5UP TO CASING PLUG AT 470--320
0001880046 2002-05-31 Production Wells No Violations Drilling out well because of plug failure (gas leakage)
1015334934 2005-05-03 Non Well No Violations on site checked out sink hole at address 11785,11780,11795. Found the area at end of each drive at edge of wooded area.

Area at 11785 approx 15 Diam with two sinks approx 18 diam. At 11780 is behind house opposite of drive along the woods area about th

1050460441 2005-06-29 Orphan No Violations needs work
1108172471 2005-05-05 Non Well No Violations Met on site with Doug Bear with AML he looked at areas said it was a burial site for stumps wood material.He said he will look at water well logs and send letter out to landowner. Expling findings.

Case closed

1114436289 2005-04-22 Orphan No Violations Inspected site found well 10 casing approx. 24 below ground level in pit dug by landowner he also hauled away soil from around well thinking it was contaminated also had tested. Gave I&O forms to get well P&A ASAP. Well leaking oil and gas

and is appro

1115652045 2005-05-09 Orphan No Violations oil to approx 6 below top of pit.
1115920471 2005-05-11 Orphan No Violations Pit static oil to ground level
1116254205 2005-05-03 Orphan No Violations checked site of pit still full of oil
1207504990 2005-05-18 Orphan No Violations meeting on site with contractor.
1249537823 2003-09-11 Final Restoration No Violations
1263838795 2005-07-20 Orphan No Violations Cutting trees down for rig access and welding casing up to ground leval.
1308134016 2005-07-20 Orphan No Violations On site with company doing work for contract to plug well welded casing to ground leval.
1551736400 2006-07-14 Final Restoration No Violations well plugged and restored
3730038601 2005-05-18 Orphan No Violations meeting on site with contractor for bibing
4606952001 2005-05-19 Orphan No Violations meeting at site
6576640991 2005-05-17 Orphan No Violations well stil same from last inspection oil filling pit not flowing.
9169513201 2005-05-13 Orphan No Violations checking pit out

For data sources see[9]

References