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− | __TOC__ | + | __TOC__ |
== Well Details == | == Well Details == | ||
{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-127-20965 | | Well ID: 34-127-20965 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 39.820192922, -82.18846896 | width=100% | height=100% }} |
|- | |- | ||
− | | | + | | Country: United States |
|- | |- | ||
− | | | + | | State: Ohio |
|- | |- | ||
− | | Operator Name: [[JEANIE | + | | County: [[Perry_County,_Ohio|Perry]] |
+ | |- | ||
+ | | Municipality: [[Clayton_Township,_Perry_County,_Ohio|Clayton Township]] | ||
+ | |- | ||
+ | | Operator Name: [[JEANIE ENTERPRISES LLC]] | ||
|- | |- | ||
| Well Pad ID: | | Well Pad ID: | ||
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: EMBREY JAMES E |
|- | |- | ||
− | | | + | | License Status: Producing |
|- | |- | ||
− | | | + | | License Date: 2006-09-12 |
|- | |- | ||
| Spud Date: 1947-06-12 | | Spud Date: 1947-06-12 | ||
|- | |- | ||
− | | | + | | Spud Drilling Contractor: |
+ | |- | ||
+ | | Final Drill Date: 1947-07-28 | ||
+ | |- | ||
+ | | Well Total Depth: 3360 ft | ||
|- | |- | ||
| Configuration: Vertical | | Configuration: Vertical | ||
|- | |- | ||
− | | | + | | Latitude: 39.820192922 |
|- | |- | ||
− | | | + | | Longitude: -82.18846896 |
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | == Well History == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Well Status | ||
+ | !scope="col" style="width: 15%;text-align: center"| Well Status Date | ||
+ | !scope="col" style="text-align: center"| Comment | ||
|- | |- | ||
− | | | + | | Original Spud |
+ | | 1947-06-12 | ||
+ | | | ||
|- | |- | ||
− | | | + | | Completed |
+ | | 1947-07-28 | ||
+ | | | ||
+ | |- | ||
+ | | Reached Total Depth | ||
+ | | 1947-07-28 | ||
+ | | | ||
+ | |- | ||
+ | | Change of Owner | ||
+ | | 2007-08-30 | ||
+ | | Operator changed from 456, SCHMELZER MARK to 8268, JEANIE ENTERPISES LLC | ||
+ | |- | ||
+ | | Record Last Modified | ||
+ | | 2013-10-03 | ||
+ | | | ||
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well and WellHistry Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | <!--== Perforation Treatments == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Perforation Date | ||
+ | !scope="col" style="text-align: center"| Interval Top (ft) | ||
+ | !scope="col" style="text-align: center"| Interval Base (ft) | ||
+ | !scope="col" style="text-align: center"| Number of Shots | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Job Start Date | ||
+ | !scope="col" style="text-align: center"| Job End Date | ||
+ | !scope="col" style="text-align: center"| True Vertical Depth (ft) | ||
+ | !scope="col" style="text-align: center"| Total Water Volume (gal) | ||
+ | !scope="col" style="text-align: center"| Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" style="width: 100%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Trade Name | ||
+ | !scope="col" style="text-align: center"| Supplier | ||
+ | !scope="col" style="text-align: center"| Purpose | ||
+ | !scope="col" style="text-align: center"| Ingredient Name | ||
+ | !scope="col" style="white-space: nowrap;text-align: center"| CAS Number | ||
+ | !scope="col" style="text-align: center"| Additive Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Job Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Mass Used (lb) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Stimulations Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Stimulation Date | ||
+ | !scope="col" style="text-align: center"| Chemical Agent | ||
+ | !scope="col" style="text-align: center"| Chemical Agent Concentration (%) | ||
+ | !scope="col" style="text-align: center"| Fracking Fluid Volume | ||
+ | !scope="col" style="text-align: center"| Mass of Proppant Used (lb) | ||
+ | !scope="col" style="text-align: center"| Fracking Company | ||
+ | !scope="col" style="text-align: center"| Comments | ||
+ | |- | ||
+ | |}--> | ||
== Production Data == | == Production Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Period |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Operator Name |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Gas Quantity (mcf) |
− | !scope="col" | + | !scope="col" style="text-align: center"| Oil Quantity (bbl) |
− | + | !scope="col" style="text-align: center"| Production Days | |
− | !scope="col" | ||
− | |||
|- | |- | ||
− | | 1995-0 | + | | 1995 |
− | | style="text-align:right;" | 0 | + | | [[SCHMELZER MARK]] |
− | | | + | | style="text-align: right;" | 0 |
− | | | + | | style="text-align: right;" | 227 |
− | | | + | | style="text-align: right;" | 365 |
− | | style="text-align:right;" | 227 | + | |- |
− | | | + | | 1996 |
+ | | [[SCHMELZER MARK]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 156 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 1997 | ||
+ | | [[SCHMELZER MARK]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 202 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 1998 | ||
+ | | [[SCHMELZER MARK]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 114 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 1999 | ||
+ | | [[SCHMELZER MARK]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 183 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2000 | ||
+ | | [[SCHMELZER MARK]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 191 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2001 | ||
+ | | [[SCHMELZER MARK]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 253 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2002 | ||
+ | | [[SCHMELZER MARK]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 215 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2003 | ||
+ | | [[SCHMELZER MARK]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 267 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2004 | ||
+ | | [[SCHMELZER MARK]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 227 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2005 | ||
+ | | [[SCHMELZER MARK]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 267 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
+ | | 2006 | ||
+ | | [[SCHMELZER MARK]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 160 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2007 |
− | | style="text-align:right;" | | + | | [[JEANIE ENTERPRISES LLC]] |
− | | | + | | style="text-align: right;" | 0 |
− | + | | style="text-align: right;" | 153 | |
− | | | + | | style="text-align: right;" | 365 |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2008 | ||
+ | | [[JEANIE ENTERPRISES LLC]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 220 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2009 |
− | | style="text-align:right;" | | + | | [[JEANIE ENTERPRISES LLC]] |
− | | | + | | style="text-align: right;" | 0 |
− | + | | style="text-align: right;" | 73 | |
− | | | + | | style="text-align: right;" | 0 |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2010 | ||
+ | | [[JEANIE ENTERPRISES LLC]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 108 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2011 |
− | | style="text-align:right;" | | + | | [[JEANIE ENTERPRISES LLC]] |
− | | | + | | style="text-align: right;" | 0 |
− | + | | style="text-align: right;" | 146 | |
− | | | + | | style="text-align: right;" | 365 |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2012 | ||
+ | | [[JEANIE ENTERPRISES LLC]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 99 | ||
+ | | style="text-align: right;" | 366 | ||
|- | |- | ||
− | | | + | | 2013 |
− | | style="text-align:right;" | | + | | [[JEANIE ENTERPRISES LLC]] |
− | | | + | | style="text-align: right;" | 0 |
− | + | | style="text-align: right;" | 65 | |
− | | | + | | style="text-align: right;" | 365 |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2014 | ||
+ | | [[JEANIE ENTERPRISES LLC]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 69 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2015 |
− | | style="text-align:right;" | | + | | [[JEANIE ENTERPRISES LLC]] |
− | | | + | | style="text-align: right;" | 0 |
− | + | | style="text-align: right;" | 71 | |
− | | | + | | style="text-align: right;" | 365 |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2016 | ||
+ | | [[JEANIE ENTERPRISES LLC]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 108 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2017 |
− | | style="text-align:right;" | | + | | [[JEANIE ENTERPRISES LLC]] |
− | | | + | | style="text-align: right;" | 0 |
− | + | | style="text-align: right;" | 0 | |
− | | | + | | style="text-align: right;" | 365 |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2018 | ||
+ | | [[JEANIE ENTERPRISES LLC]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | |} |
− | | style="text-align: | + | For data sources see<ref>{{cite web |
− | | | + | | title = Risk Based Data Management System - Production Table - Oil and Gas Data |
− | | | + | |publisher = [[Ohio Department of Natural Resources]] |
− | | | + | | date = 2019-05-07 |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | |
− | + | | accessdate = 2019-05-21 }}</ref> | |
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Oil and Gas Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | == Waste Data == | ||
+ | {| class="wikitable sortable" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Waste Type | ||
+ | !scope="col" style="text-align: center"| Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
|- | |- | ||
+ | | 1995 | ||
+ | | [[SCHMELZER MARK]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 70 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 1996 |
− | | style="text-align:right;" | | + | | [[SCHMELZER MARK]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 70 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 1997 | ||
+ | | [[SCHMELZER MARK]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 70 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 1998 |
− | | style="text-align:right;" | | + | | [[SCHMELZER MARK]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 70 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 1999 | ||
+ | | [[SCHMELZER MARK]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 70 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2000 |
− | | style="text-align:right;" | 0 | + | | [[SCHMELZER MARK]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2001 | ||
+ | | [[SCHMELZER MARK]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 70 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2002 |
− | | style="text-align:right;" | 0 | + | | [[SCHMELZER MARK]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2003 | ||
+ | | [[SCHMELZER MARK]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2004 |
− | | style="text-align:right;" | 0 | + | | [[SCHMELZER MARK]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2005 | ||
+ | | [[SCHMELZER MARK]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2006 |
− | | style="text-align:right;" | 0 | + | | [[SCHMELZER MARK]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2007 | ||
+ | | [[JEANIE ENTERPRISES LLC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2008 |
− | | style="text-align:right;" | 0 | + | | [[JEANIE ENTERPRISES LLC]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2009 | ||
+ | | [[JEANIE ENTERPRISES LLC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | | ||
|- | |- | ||
− | | 2010 | + | | 2010 |
− | | style="text-align:right;" | | + | | [[JEANIE ENTERPRISES LLC]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 4 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2011 | ||
+ | | [[JEANIE ENTERPRISES LLC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2012 |
− | | style="text-align:right;" | 0 | + | | [[JEANIE ENTERPRISES LLC]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 366 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2013 | ||
+ | | [[JEANIE ENTERPRISES LLC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2014 |
− | | style="text-align:right;" | 0 | + | | [[JEANIE ENTERPRISES LLC]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2015 | ||
+ | | [[JEANIE ENTERPRISES LLC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 65 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2016 |
− | | style="text-align:right;" | | + | | [[JEANIE ENTERPRISES LLC]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 18 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2017 | ||
+ | | [[JEANIE ENTERPRISES LLC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2018 |
− | + | | [[JEANIE ENTERPRISES LLC]] | |
− | + | | Brine | |
− | | | + | | style="text-align: right;" | 0 |
− | | | + | | style="text-align: right;" | 365 |
− | | style="text-align:right;" | | ||
− | | style="text-align:right;" | 365 | ||
|- | |- | ||
|} | |} | ||
For data sources see<ref>{{cite web | For data sources see<ref>{{cite web | ||
− | | title = Ohio Department of Natural Resources | + | | title = Risk Based Data Management System - Production Table - Brine Data |
− | | | + | |publisher = [[Ohio Department of Natural Resources]] |
− | | date = | + | | date = 2019-05-07 |
− | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources |
− | | accessdate = | + | | accessdate = 2019-05-21 }}</ref> |
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Brine Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
== Inspection Data == | == Inspection Data == | ||
+ | ==== Inspections Performed ==== | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection ID |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Date |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Type |
− | !scope="col" | + | !scope="col" style="text-align: center"| Inspection Result |
− | + | !scope="col" style="text-align: center"| Inspection Comments | |
− | !scope="col" | + | |- |
− | + | | 0179357614 | |
+ | | 2017-01-03 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | I was on location to do a field inspection on the Embrey J # 2 well. The well has a pumping unit on it with rods and 1.5 inch diameter tubing in it. The production valve is open at the wellhead. The identification for this well is located at the tank pad. There are no violations at this time. | ||
+ | |- | ||
+ | | 0392853840 | ||
+ | | 2007-11-19 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | No violations. | ||
+ | |- | ||
+ | | 0480030580 | ||
+ | | 2014-09-15 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | I returned to this well to do a follow-up inspection on the well. The company has put a pumping unit on the well and the well is back in production. No violations at this time. | ||
+ | |- | ||
+ | | 0580712831 | ||
+ | | 2018-11-15 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | I was on location to do a field inspection on this well. The well has a pumping unit on it with rods and 1.5 inch diameter tubing in it. The production valve is open from the wellhead to the tank pad. There is 2-100 barrel storage tanks for this well. The identification for this well is located at the tank pad. There are no violations at this time. | ||
+ | |- | ||
+ | | 0664145960 | ||
+ | | 2014-02-25 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | I did a follow-up on this well. The old standing derrick that was around the well has been torn down. There has been some work done around the well site. The pumping unit is still not on the well and the well appears not to be production yet. The compliance date for the violation is 7/7/2014. I will e-mail Jeanie Enterprises to see if they plan on putting the well back in production. | ||
|- | |- | ||
| 1219674842 | | 1219674842 | ||
| 2008-08-20 | | 2008-08-20 | ||
− | | | + | | Production Wells |
+ | | No Violations | ||
| No violations. | | No violations. | ||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1256665430 | | 1256665430 | ||
| 2009-10-13 | | 2009-10-13 | ||
− | | | + | | Production Wells |
− | | AN inspection of the tank battery revealed a production tanks has a hole in the heater tube which allowed approx 60 bbls of oil to flow into dike and near by creek. Approx. 2 bbls entered creek and traveled approx. | + | | Violations Noted |
− | + | | AN inspection of the tank battery revealed a production tanks has a hole in the heater tube which allowed approx 60 bbls of oil to flow into dike and near by creek. Approx. 2 bbls entered creek and traveled approx. 2500ft down stream. Company is cleaning spill up and has removed the leaking tank. | |
− | |||
− | |||
− | |||
|- | |- | ||
| 1256766769 | | 1256766769 | ||
| 2009-10-15 | | 2009-10-15 | ||
− | | | + | | Production Wells |
+ | | No Violations | ||
| Checked clean up on oil spill, appears most of the oil has been cleaned up and removed from creek area, will have company leave booms and pads in creek for a few days. | | Checked clean up on oil spill, appears most of the oil has been cleaned up and removed from creek area, will have company leave booms and pads in creek for a few days. | ||
− | |||
− | |||
− | |||
|- | |- | ||
− | | | + | | 1682691911 |
− | |||
| 2014-06-02 | | 2014-06-02 | ||
− | | | + | | Production Wells |
+ | | No Violations | ||
| I returned to this well to do a follow-up inspection on the well. It appears the company has had someone in here working on the well. The old standing derrick that was here is gone. They have removed all the old wood away from the well and had a dozer clean out the location. The flow line is hooked up to the wellhead but there is still no pumping unit. I called Danny Baker and left him a message to call me about the well. | | I returned to this well to do a follow-up inspection on the well. It appears the company has had someone in here working on the well. The old standing derrick that was here is gone. They have removed all the old wood away from the well and had a dozer clean out the location. The flow line is hooked up to the wellhead but there is still no pumping unit. I called Danny Baker and left him a message to call me about the well. | ||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1829250032 | | 1829250032 | ||
| 2011-11-01 | | 2011-11-01 | ||
− | | | + | | Production Wells |
+ | | No Violations | ||
| No violations at this time. | | No violations at this time. | ||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1865707870 | | 1865707870 | ||
| 2013-12-30 | | 2013-12-30 | ||
− | | | + | | Production Wells |
+ | | Violations Noted | ||
| During the inspection of this well I found the pumping unit has been pulled off of the well. The production valves are shut in on the wellhead making it incapable of production. The well will need to be put back in production within 90days or plugging is required within 180days. | | During the inspection of this well I found the pumping unit has been pulled off of the well. The production valves are shut in on the wellhead making it incapable of production. The well will need to be put back in production within 90days or plugging is required within 180days. | ||
− | |||
− | |||
− | |||
|- | |- | ||
+ | |} | ||
+ | ==== Violations Commited ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Inspection ID | ||
+ | !scope="col" style="text-align: center"| Violation ID | ||
+ | !scope="col" style="text-align: center"| Violation Date | ||
+ | !scope="col" style="text-align: center"| Violation Code | ||
+ | !scope="col" style="text-align: center"| Violation Comments | ||
|- | |- | ||
− | | | + | | 1256665430 |
− | | | + | | US-OH-106917 |
− | + | | 2009-10-27 | |
− | |||
− | |||
− | | | ||
| | | | ||
+ | | Well operation causing pollution and contamination | ||
|- | |- | ||
− | | | + | | 1256665430 |
− | | | + | | US-OH-106918 |
− | + | | 2009-10-27 | |
− | | | ||
− | |||
− | |||
− | |||
| | | | ||
+ | | No SPCC dike/or failure to keep dike free of water or oil | ||
|- | |- | ||
− | | | + | | 1865707870 |
− | | - | + | | US-OH-118689 |
− | | 2014- | + | | 2014-09-22 |
− | |||
− | |||
− | |||
− | |||
| | | | ||
+ | | Nonproduction; well shall be plugged or placed in temporary inactive status | ||
|- | |- | ||
|} | |} | ||
For data sources see<ref>{{cite web | For data sources see<ref>{{cite web | ||
− | | title = | + | | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables |
− | | publisher = [ | + | |publisher = [[Ohio Department of Natural Resources]] |
− | | date = | + | | date = 2019-05-07 |
− | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources |
− | | accessdate = | + | | accessdate = 2019-05-21 }}</ref> |
− | == References == | + | ==References== |
− | + | <references/> | |
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
− | [[Category:Wells]] | + | [[Category:Ohio Wells]] |
Well ID: 34-127-20965 | Loading map...
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Country: United States | |
State: Ohio | |
County: Perry | |
Municipality: Clayton Township | |
Operator Name: JEANIE ENTERPRISES LLC | |
Well Pad ID: | |
Farm/Lease Name: EMBREY JAMES E | |
License Status: Producing | |
License Date: 2006-09-12 | |
Spud Date: 1947-06-12 | |
Spud Drilling Contractor: | |
Final Drill Date: 1947-07-28 | |
Well Total Depth: 3360 ft | |
Configuration: Vertical | |
Latitude: 39.820192922 | |
Longitude: -82.18846896 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1947-06-12 | |
Completed | 1947-07-28 | |
Reached Total Depth | 1947-07-28 | |
Change of Owner | 2007-08-30 | Operator changed from 456, SCHMELZER MARK to 8268, JEANIE ENTERPISES LLC |
Record Last Modified | 2013-10-03 |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1995 | SCHMELZER MARK | 0 | 227 | 365 |
1996 | SCHMELZER MARK | 0 | 156 | 365 |
1997 | SCHMELZER MARK | 0 | 202 | 365 |
1998 | SCHMELZER MARK | 0 | 114 | 365 |
1999 | SCHMELZER MARK | 0 | 183 | 365 |
2000 | SCHMELZER MARK | 0 | 191 | 365 |
2001 | SCHMELZER MARK | 0 | 253 | 365 |
2002 | SCHMELZER MARK | 0 | 215 | 365 |
2003 | SCHMELZER MARK | 0 | 267 | 365 |
2004 | SCHMELZER MARK | 0 | 227 | 365 |
2005 | SCHMELZER MARK | 0 | 267 | 365 |
2006 | SCHMELZER MARK | 0 | 160 | 365 |
2007 | JEANIE ENTERPRISES LLC | 0 | 153 | 365 |
2008 | JEANIE ENTERPRISES LLC | 0 | 220 | 365 |
2009 | JEANIE ENTERPRISES LLC | 0 | 73 | 0 |
2010 | JEANIE ENTERPRISES LLC | 0 | 108 | 365 |
2011 | JEANIE ENTERPRISES LLC | 0 | 146 | 365 |
2012 | JEANIE ENTERPRISES LLC | 0 | 99 | 366 |
2013 | JEANIE ENTERPRISES LLC | 0 | 65 | 365 |
2014 | JEANIE ENTERPRISES LLC | 0 | 69 | 365 |
2015 | JEANIE ENTERPRISES LLC | 0 | 71 | 365 |
2016 | JEANIE ENTERPRISES LLC | 0 | 108 | 365 |
2017 | JEANIE ENTERPRISES LLC | 0 | 0 | 365 |
2018 | JEANIE ENTERPRISES LLC | 0 | 0 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1995 | SCHMELZER MARK | Brine | 70 | 365 |
1996 | SCHMELZER MARK | Brine | 70 | 365 |
1997 | SCHMELZER MARK | Brine | 70 | 365 |
1998 | SCHMELZER MARK | Brine | 70 | 365 |
1999 | SCHMELZER MARK | Brine | 70 | 365 |
2000 | SCHMELZER MARK | Brine | 0 | 365 |
2001 | SCHMELZER MARK | Brine | 70 | 365 |
2002 | SCHMELZER MARK | Brine | 0 | 365 |
2003 | SCHMELZER MARK | Brine | 0 | 365 |
2004 | SCHMELZER MARK | Brine | 0 | 365 |
2005 | SCHMELZER MARK | Brine | 0 | 365 |
2006 | SCHMELZER MARK | Brine | 0 | 365 |
2007 | JEANIE ENTERPRISES LLC | Brine | 0 | 365 |
2008 | JEANIE ENTERPRISES LLC | Brine | 0 | 365 |
2009 | JEANIE ENTERPRISES LLC | Brine | 0 | |
2010 | JEANIE ENTERPRISES LLC | Brine | 4 | 365 |
2011 | JEANIE ENTERPRISES LLC | Brine | 0 | 365 |
2012 | JEANIE ENTERPRISES LLC | Brine | 0 | 366 |
2013 | JEANIE ENTERPRISES LLC | Brine | 0 | 365 |
2014 | JEANIE ENTERPRISES LLC | Brine | 0 | 365 |
2015 | JEANIE ENTERPRISES LLC | Brine | 65 | 365 |
2016 | JEANIE ENTERPRISES LLC | Brine | 18 | 365 |
2017 | JEANIE ENTERPRISES LLC | Brine | 0 | 365 |
2018 | JEANIE ENTERPRISES LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0179357614 | 2017-01-03 | Production Wells | No Violations | I was on location to do a field inspection on the Embrey J # 2 well. The well has a pumping unit on it with rods and 1.5 inch diameter tubing in it. The production valve is open at the wellhead. The identification for this well is located at the tank pad. There are no violations at this time. |
0392853840 | 2007-11-19 | Production Wells | No Violations | No violations. |
0480030580 | 2014-09-15 | Production Wells | No Violations | I returned to this well to do a follow-up inspection on the well. The company has put a pumping unit on the well and the well is back in production. No violations at this time. |
0580712831 | 2018-11-15 | Production Wells | No Violations | I was on location to do a field inspection on this well. The well has a pumping unit on it with rods and 1.5 inch diameter tubing in it. The production valve is open from the wellhead to the tank pad. There is 2-100 barrel storage tanks for this well. The identification for this well is located at the tank pad. There are no violations at this time. |
0664145960 | 2014-02-25 | Production Wells | No Violations | I did a follow-up on this well. The old standing derrick that was around the well has been torn down. There has been some work done around the well site. The pumping unit is still not on the well and the well appears not to be production yet. The compliance date for the violation is 7/7/2014. I will e-mail Jeanie Enterprises to see if they plan on putting the well back in production. |
1219674842 | 2008-08-20 | Production Wells | No Violations | No violations. |
1256665430 | 2009-10-13 | Production Wells | Violations Noted | AN inspection of the tank battery revealed a production tanks has a hole in the heater tube which allowed approx 60 bbls of oil to flow into dike and near by creek. Approx. 2 bbls entered creek and traveled approx. 2500ft down stream. Company is cleaning spill up and has removed the leaking tank. |
1256766769 | 2009-10-15 | Production Wells | No Violations | Checked clean up on oil spill, appears most of the oil has been cleaned up and removed from creek area, will have company leave booms and pads in creek for a few days. |
1682691911 | 2014-06-02 | Production Wells | No Violations | I returned to this well to do a follow-up inspection on the well. It appears the company has had someone in here working on the well. The old standing derrick that was here is gone. They have removed all the old wood away from the well and had a dozer clean out the location. The flow line is hooked up to the wellhead but there is still no pumping unit. I called Danny Baker and left him a message to call me about the well. |
1829250032 | 2011-11-01 | Production Wells | No Violations | No violations at this time. |
1865707870 | 2013-12-30 | Production Wells | Violations Noted | During the inspection of this well I found the pumping unit has been pulled off of the well. The production valves are shut in on the wellhead making it incapable of production. The well will need to be put back in production within 90days or plugging is required within 180days. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1256665430 | US-OH-106917 | 2009-10-27 | Well operation causing pollution and contamination | |
1256665430 | US-OH-106918 | 2009-10-27 | No SPCC dike/or failure to keep dike free of water or oil | |
1865707870 | US-OH-118689 | 2014-09-22 | Nonproduction; well shall be plugged or placed in temporary inactive status |
For data sources see[7]