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Difference between revisions of "34-095-20079"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-095-20079
 
| Well ID: 34-095-20079
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.6541318, -83.39529969 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.654178975, -83.39523217 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Lucas County, Ohio|Lucas]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Lucas_County,_Ohio|Lucas]]
 +
|-
 +
| Municipality: [[Oregon,_Ohio|Oregon]]
 
|-
 
|-
 
| Operator Name: [[CLEARWATER WELL DRILLING]]
 
| Operator Name: [[CLEARWATER WELL DRILLING]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: TESCO
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2011-08-11
 
|-
 
|-
 
| Spud Date:  
 
| Spud Date:  
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:
 +
|-
 +
| Final Drill Date:
 +
|-
 +
| Well Total Depth:  
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Final Restoration
+
| Latitude: 41.654178975
 
|-
 
|-
| Violations: 0
+
| Longitude: -83.39523217
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 
|-
 
|-
| Latitude: 41.6541318
+
| APP
 +
| 2006-09-21
 +
| Proposed Formations:TRENTON, Issued Date:9/21/2006, Expired Date:9/21/2007 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
 
|-
 
|-
| Longitude: -83.39529969
+
| Plugged by Orphan Well Program
 +
| 2006-09-28
 +
| Plugged by Orphan Well Program
 +
|-
 +
| Plugged/Abandoned
 +
| 2006-09-28
 +
 +
|-
 +
| Construction Permit Expires
 +
| 2007-09-21
 +
 +
|-
 +
| Record Last Modified
 +
| 2013-03-14
 +
 
|-
 
|-
 
|}
 
|}
== Inspection Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Perforation Treatments ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Perforation Date
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Interval Top (ft)
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Interval Base (ft)
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Number of Shots
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
| 1159202284
+
|}-->
| 2006-09-25
+
<!--== Fracking Activities ==
|  
+
==== Fracking Jobs ====
| Remaining cement from plugging of well 34-095-20078-0000 was used to partially fill the annular space between the 6 inch and 12 inch casing. The operator will weld a control head on the well and begin removing rods and tubing tommorrow.
+
{| class="wikitable sortable" width="95%"
|  
+
!scope="col" style="text-align: center"| Job Number
|  
+
!scope="col" style="text-align: center"| Job Start Date
|  
+
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 
|-
 
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 
|-
 
|-
| 1159969989
+
|}-->
| 2006-10-03
+
<!--== Stimulations Data ==
|  
+
{| class="wikitable sortable" width="95%"
| Phone call from Bob Harpster on 9/28/06 reported that cement poured into well on 9/27/06 had settled in the pipe to a depth of approximately 100 feet. Two additional yards of 9 sack grout were ordered to complete plugging of the well. The well casing was filled to the surface and the well has been cut off below ground with ID plate attached to well according to Bob. There was no sign of the well during inspection and the site was covered with gravel. Bob is sending cement ticket to inspector.
+
!scope="col" style="text-align: center"| Stimulation Date
|  
+
!scope="col" style="text-align: center"| Chemical Agent
|  
+
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
|  
+
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
 +
|}-->
 +
<!--== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 1366189179
+
|}-->
| 2006-09-27
+
<!--== Waste Data ==
|  
+
{| class="wikitable sortable"
| On site for plugging of well. Operator Bob Harpster estimated the depth of the well at 1340 feet. The operator ordered 9 yards of 9 sack grout to fill the well casing. Grout was poured into the 6 inch casing as well as the annular space between the 6 inch and 12 inch casing. Cement filled to the top of both casings but settled 10 -20 feet by the time inspection was completed. Bob said he would let cement set up overnight and then check depth in morning and top off well with cement as needed.
+
!scope="col" style="text-align: center"| Period
|  
+
!scope="col" style="text-align: center"| Operator Name
|  
+
!scope="col" style="text-align: center"| Waste Type
|  
+
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
|}-->
 +
== Inspection Data ==
 +
==== Inspections Performed ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Inspection Date
 +
!scope="col" style="text-align: center"| Inspection Type
 +
!scope="col" style="text-align: center"| Inspection Result
 +
!scope="col" style="text-align: center"| Inspection Comments
 
|-
 
|-
| -543977568
+
| 0543977568
 
| 2011-08-11
 
| 2011-08-11
|  
+
| Final Restoration
 +
| No Violations
 
| Well pluugged on 10/27/2006. No sign of well. Final Restoration Passed
 
| Well pluugged on 10/27/2006. No sign of well. Final Restoration Passed
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 0614597117
| 614597117
 
 
| 2006-09-22
 
| 2006-09-22
|  
+
| Production Wells
 +
| No Violations
 
| Inspect well. 10 inch casing, 6 inch casing. Rods and tubing. Well head bent at grade.
 
| Inspect well. 10 inch casing, 6 inch casing. Rods and tubing. Well head bent at grade.
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 0992465586
| 992465586
 
 
| 2006-09-13
 
| 2006-09-13
|  
+
| Orphan
 +
| No Violations
 
| Received phone call from Dave Barndt of Clearwater Drilling about abandoned wells on property that is proposed for develpoment. The wells are located at 6401 Seaman Road, Oregon, Ohio. The landowner, Noel Graham wants the wells plugged due to a proposed development project. Mr. Graham said he spoke to an ODNR inspector 5-10 years ago and had the wells submitted to the I&O program but has never been contacted about having the wells plugged. He has owned the property 38 years and has not produced the wells. Mr. Graham will pay to have the wells plugged. Clearwater is applying for the permits to plug the wells.
 
| Received phone call from Dave Barndt of Clearwater Drilling about abandoned wells on property that is proposed for develpoment. The wells are located at 6401 Seaman Road, Oregon, Ohio. The landowner, Noel Graham wants the wells plugged due to a proposed development project. Mr. Graham said he spoke to an ODNR inspector 5-10 years ago and had the wells submitted to the I&O program but has never been contacted about having the wells plugged. He has owned the property 38 years and has not produced the wells. Mr. Graham will pay to have the wells plugged. Clearwater is applying for the permits to plug the wells.
|  
+
|-
|  
+
| 1159202284
|  
+
| 2006-09-25
 +
| Orphan
 +
| No Violations
 +
| Remaining cement from plugging of well 34-095-20078-0000 was used to partially fill the annular space between the 6 inch and 12 inch casing. The operator will weld a control head on the well and begin removing rods and tubing tommorrow.
 +
|-
 +
| 1159969989
 +
| 2006-10-03
 +
| Orphan
 +
| No Violations
 +
| Phone call from Bob Harpster on 9/28/06 reported that cement poured into well on 9/27/06 had settled in the pipe to a depth of approximately 100 feet. Two additional yards of 9 sack grout were ordered to complete plugging of the well. The well casing was filled to the surface and the well has been cut off below ground with ID plate attached to well according to Bob. There was no sign of the well during inspection and the site was covered with gravel. Bob is sending cement ticket to inspector.
 +
|-
 +
| 1366189179
 +
| 2006-09-27
 +
| Orphan
 +
| No Violations
 +
| On site for plugging of well. Operator Bob Harpster estimated the depth of the well at 1340 feet. The operator ordered 9 yards of 9 sack grout to fill the well casing. Grout was poured into the 6 inch casing as well as the annular space between the 6 inch and 12 inch casing. Cement filled to the top of both casings but settled 10 -20 feet by the time inspection was completed. Bob said he would let cement set up overnight and then check depth in morning and top off well with cement as needed.
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 19:31, 24 July 2019

Well Details

Well ID: 34-095-20079
Loading map...
Country: United States
State: Ohio
County: Lucas
Municipality: Oregon
Operator Name: CLEARWATER WELL DRILLING
Well Pad ID:
Farm/Lease Name: TESCO
License Status: Final Restoration
License Date: 2011-08-11
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 41.654178975
Longitude: -83.39523217

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2006-09-21 Proposed Formations:TRENTON, Issued Date:9/21/2006, Expired Date:9/21/2007 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged by Orphan Well Program 2006-09-28 Plugged by Orphan Well Program
Plugged/Abandoned 2006-09-28
Construction Permit Expires 2007-09-21
Record Last Modified 2013-03-14

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0543977568 2011-08-11 Final Restoration No Violations Well pluugged on 10/27/2006. No sign of well. Final Restoration Passed
0614597117 2006-09-22 Production Wells No Violations Inspect well. 10 inch casing, 6 inch casing. Rods and tubing. Well head bent at grade.
0992465586 2006-09-13 Orphan No Violations Received phone call from Dave Barndt of Clearwater Drilling about abandoned wells on property that is proposed for develpoment. The wells are located at 6401 Seaman Road, Oregon, Ohio. The landowner, Noel Graham wants the wells plugged due to a proposed development project. Mr. Graham said he spoke to an ODNR inspector 5-10 years ago and had the wells submitted to the I&O program but has never been contacted about having the wells plugged. He has owned the property 38 years and has not produced the wells. Mr. Graham will pay to have the wells plugged. Clearwater is applying for the permits to plug the wells.
1159202284 2006-09-25 Orphan No Violations Remaining cement from plugging of well 34-095-20078-0000 was used to partially fill the annular space between the 6 inch and 12 inch casing. The operator will weld a control head on the well and begin removing rods and tubing tommorrow.
1159969989 2006-10-03 Orphan No Violations Phone call from Bob Harpster on 9/28/06 reported that cement poured into well on 9/27/06 had settled in the pipe to a depth of approximately 100 feet. Two additional yards of 9 sack grout were ordered to complete plugging of the well. The well casing was filled to the surface and the well has been cut off below ground with ID plate attached to well according to Bob. There was no sign of the well during inspection and the site was covered with gravel. Bob is sending cement ticket to inspector.
1366189179 2006-09-27 Orphan No Violations On site for plugging of well. Operator Bob Harpster estimated the depth of the well at 1340 feet. The operator ordered 9 yards of 9 sack grout to fill the well casing. Grout was poured into the 6 inch casing as well as the annular space between the 6 inch and 12 inch casing. Cement filled to the top of both casings but settled 10 -20 feet by the time inspection was completed. Bob said he would let cement set up overnight and then check depth in morning and top off well with cement as needed.

For data sources see[3]

References