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Difference between revisions of "34-127-26589"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-127-26589
 
| Well ID: 34-127-26589
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.87516438, -82.39461486 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.875012860, -82.39442507 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Perry County, Ohio|Perry]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Perry_County,_Ohio|Perry]]
 +
|-
 +
| Municipality: [[Thorn_Township,_Perry_County,_Ohio|Thorn Township]]
 
|-
 
|-
 
| Operator Name: [[NGO DEVELOPMENT CORP.]]
 
| Operator Name: [[NGO DEVELOPMENT CORP.]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: ODGEN
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2019-01-31
 
|-
 
|-
 
| Spud Date: 1985-03-21
 
| Spud Date: 1985-03-21
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:  
 +
|-
 +
| Final Drill Date: 1985-04-18
 +
|-
 +
| Well Total Depth: 2727 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Producing
+
| Latitude: 39.875012860
 
|-
 
|-
| Violations: 0
+
| Longitude: -82.39442507
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 
|-
 
|-
| Latitude: 39.87516438
+
| CO
 +
| 1985-02-27
 +
| 1111  MERIDIAN ENERGY COMPANY  GeoDate  2/27/85
 
|-
 
|-
| Longitude: -82.39461486
+
| Oil and Gas
 +
| 1985-02-27
 +
| Issued Date 2/27/85 Expired Date 8/26/85 Acres 0020000 Tool Type CT Proposed Formation CLINTON Proposed Depth 02727 Proposed Drill Depth 02727
 +
|-
 +
| Original Spud
 +
| 1985-03-21
 +
| GMM CHANGED PLUG STATUS PER PLUG REPORT
 +
|-
 +
| Completed
 +
| 1985-04-18
 +
| GMM CHANGED PLUG STATUS PER PLUG REPORT
 +
|-
 +
| Reached Total Depth
 +
| 1985-04-18
 +
| GMM CHANGED PLUG STATUS PER PLUG REPORT
 +
|-
 +
| Completion Report Received
 +
| 1986-01-01
 +
| GMM CHANGED PLUG STATUS PER PLUG REPORT
 +
|-
 +
| CO
 +
| 1993-01-26
 +
| 424  NATIONAL PRODUCTION CORP  GeoDate  2/27/85
 +
|-
 +
| CO
 +
| 1996-03-04
 +
| 98  NGO DEVELOPMENT CORP.  GeoDate  2/27/85
 +
|-
 +
| APP
 +
| 2017-08-25
 +
| Proposed Formations:CLINTON, Issued Date:8/25/2017, Expired Date:8/25/2019 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:HAD, Proposed Well Class:
 +
|-
 +
| Plugged/Abandoned
 +
| 2017-11-02
 +
| GMM CHANGED PLUG STATUS PER PLUG REPORT
 +
|-
 +
| Record Last Modified
 +
| 2019-06-05
 +
| GMM CHANGED PLUG STATUS PER PLUG REPORT
 +
|-
 +
| Construction Permit Expires
 +
| 2019-08-25
 +
| GMM CHANGED PLUG STATUS PER PLUG REPORT
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 
== Production Data ==
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Period
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Operator Name
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Gas Quantity (mcf)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Oil Quantity (bbl)
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Production Days
!scope="col" | OIL QUANTITY
+
|-
!scope="col" | OIL PRODUCTION DAYS
+
| 1985
 +
| [[MERIDIAN ENERGY COMPANY]]
 +
| style="text-align: right;" | 22138
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1986
 +
| [[MERIDIAN ENERGY COMPANY]]
 +
| style="text-align: right;" | 9115
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1987
 +
| [[MERIDIAN ENERGY COMPANY]]
 +
| style="text-align: right;" | 9421
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1988
 +
| [[MERIDIAN ENERGY COMPANY]]
 +
| style="text-align: right;" | 893
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1993
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| style="text-align: right;" | 2892
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1994
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| style="text-align: right;" | 6645
 +
| style="text-align: right;" | 87
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1995
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| style="text-align: right;" | 1004
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1985-0
+
| 1996
| style="text-align:right;" | 22138.0
+
| [[NGO DEVELOPMENT CORP.]]
|  
+
| style="text-align: right;" | 1548
|  
+
| style="text-align: right;" | 163
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
+
|-
|  
+
| 1997
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| style="text-align: right;" | 1595
 +
| style="text-align: right;" | 87
 +
| style="text-align: right;" | 365
 
|-
 
|-
 +
| 1998
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| style="text-align: right;" | 2344
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1986-0
+
| 1999
| style="text-align:right;" | 9115.0
+
| [[NGO DEVELOPMENT CORP.]]
|  
+
| style="text-align: right;" | 1279
|
+
| style="text-align: right;" | 157
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2000
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| style="text-align: right;" | 329
 +
| style="text-align: right;" | 123
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1987-0
+
| 2001
| style="text-align:right;" | 9421.0
+
| [[NGO DEVELOPMENT CORP.]]
|  
+
| style="text-align: right;" | 476
|
+
| style="text-align: right;" | 60
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2002
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| style="text-align: right;" | 308
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1988-0
+
| 2003
| style="text-align:right;" | 893.0
+
| [[NGO DEVELOPMENT CORP.]]
|  
+
| style="text-align: right;" | 66
|
+
| style="text-align: right;" | 83
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2004
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| style="text-align: right;" | 21
 +
| style="text-align: right;" | 46
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1993-0
+
| 2005
| style="text-align:right;" | 2892.0
+
| [[NGO DEVELOPMENT CORP.]]
|  
+
| style="text-align: right;" | 70
|
+
| style="text-align: right;" | 33
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2006
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| style="text-align: right;" | 59
 +
| style="text-align: right;" | 53
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1994-0
+
| 2007
| style="text-align:right;" | 6645.0
+
| [[NGO DEVELOPMENT CORP.]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 43
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 87.0
 
|
 
 
|-
 
|-
 +
| 2008
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| style="text-align: right;" | 8
 +
| style="text-align: right;" | 52
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1995-0
+
| 2009
| style="text-align:right;" | 1004.0
+
| [[NGO DEVELOPMENT CORP.]]
|  
+
| style="text-align: right;" | 18
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2010
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| style="text-align: right;" | 83
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1996-0
+
| 2011
| style="text-align:right;" | 1548.0
+
| [[NGO DEVELOPMENT CORP.]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 163.0
 
|
 
 
|-
 
|-
 +
| 2012
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 366
 
|-
 
|-
| 1997-0
+
| 2013
| style="text-align:right;" | 1595.0
+
| [[NGO DEVELOPMENT CORP.]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 87.0
 
|
 
 
|-
 
|-
 +
| 2014
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1998-0
+
| 2015
| style="text-align:right;" | 2344.0
+
| [[NGO DEVELOPMENT CORP.]]
|  
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
|
 
|  
 
 
|-
 
|-
 +
| 2016
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 36
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1999-0
+
| 2017
| style="text-align:right;" | 1279.0
+
| [[NGO DEVELOPMENT CORP.]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 306
| style="text-align:right;" | 157.0
 
|
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 2000-0
+
| 1985
| style="text-align:right;" | 329.0
+
| [[MERIDIAN ENERGY COMPANY]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 123.0
 
|
 
 
|-
 
|-
 +
| 1986
 +
| [[MERIDIAN ENERGY COMPANY]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2001-0
+
| 1987
| style="text-align:right;" | 476.0
+
| [[MERIDIAN ENERGY COMPANY]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 60.0
 
|
 
 
|-
 
|-
 +
| 1988
 +
| [[MERIDIAN ENERGY COMPANY]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2002-0
+
| 1993
| style="text-align:right;" | 308.0
+
| [[NGO DEVELOPMENT CORP.]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1994
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2003-0
+
| 1995
| style="text-align:right;" | 66.0
+
| [[NGO DEVELOPMENT CORP.]]
|
+
| Brine
|
+
| style="text-align: right;" | 54
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 83.0
 
|
 
 
|-
 
|-
 +
| 1996
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2004-0
+
| 1997
| style="text-align:right;" | 21.0
+
| [[NGO DEVELOPMENT CORP.]]
|
+
| Brine
|
+
| style="text-align: right;" | 13
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 46.0
 
|
 
 
|-
 
|-
 +
| 1998
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| Brine
 +
| style="text-align: right;" | 35
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2005-0
+
| 1999
| style="text-align:right;" | 70.0
+
| [[NGO DEVELOPMENT CORP.]]
|
+
| Brine
|
+
| style="text-align: right;" | 136
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 33.0
 
|
 
 
|-
 
|-
 +
| 2000
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| Brine
 +
| style="text-align: right;" | 10
 +
| style="text-align: right;" |
 
|-
 
|-
| 2006-0
+
| 2001
| style="text-align:right;" | 59.0
+
| [[NGO DEVELOPMENT CORP.]]
|
+
| Brine
|
+
| style="text-align: right;" | 37
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 53.0
 
|
 
 
|-
 
|-
 +
| 2002
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2007-0
+
| 2003
| style="text-align:right;" | 0.0
+
| [[NGO DEVELOPMENT CORP.]]
|
+
| Brine
|
+
| style="text-align: right;" | 45
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 43.0
 
|
 
 
|-
 
|-
 +
| 2004
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| Brine
 +
| style="text-align: right;" | 31
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2008-0
+
| 2005
| style="text-align:right;" | 8.0
+
| [[NGO DEVELOPMENT CORP.]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 52.0
 
|
 
 
|-
 
|-
 +
| 2006
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| Brine
 +
| style="text-align: right;" | 25
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2009-0
+
| 2007
| style="text-align:right;" | 18.0
+
| [[NGO DEVELOPMENT CORP.]]
|
+
| Brine
|
+
| style="text-align: right;" | 35
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2008
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| Brine
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2010-0
+
| 2009
| style="text-align:right;" | 83.0
+
| [[NGO DEVELOPMENT CORP.]]
|
+
| Brine
|
+
| style="text-align: right;" | 90
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2010
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| Brine
 +
| style="text-align: right;" | 40
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2011-0
+
| 2011
| style="text-align:right;" | 0.0
+
| [[NGO DEVELOPMENT CORP.]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2012
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 366
 
|-
 
|-
| 2012-0
+
| 2013
| style="text-align:right;" | 0.0
+
| [[NGO DEVELOPMENT CORP.]]
|
+
| Brine
|
+
| style="text-align: right;" | 26
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2014
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2013-0
+
| 2015
| style="text-align:right;" | 0.0
+
| [[NGO DEVELOPMENT CORP.]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2016
 +
| [[NGO DEVELOPMENT CORP.]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2014-0
+
| 2017
| style="text-align:right;" | 0.0
+
| [[NGO DEVELOPMENT CORP.]]
| style="text-align:right;" | 365.0
+
| Brine
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 306
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 365.0
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2019-05-07
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2019-05-21 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
| -1923965150
+
| 0000PL6642
| 2006-05-03
 
|
 
| No violations.
 
|
 
|
 
 
|  
 
|  
 +
| Preliminary Restoration
 +
| No Violations
 +
| Preliminary Restoration  done information from Data Point
 +
|-
 +
| 0371702305
 +
| 2017-10-27
 +
| Plug / Plug Back
 +
| No Violations
 +
| Knox Energy has moved their service rig in on this well to plug it. Today they pulled out the rods and tubing from the well and they will start plugging the well on Monday.
 
|-
 
|-
 +
| 0577837154
 +
| 2019-01-31
 +
| Final Restoration
 +
| No Violations
 +
| I was on location today to complete the final restoration on this well. The final restoration meets 1509.072(B) requirements.
 
|-
 
|-
| 629534659
+
| 0629534659
 
| 2014-03-20
 
| 2014-03-20
|  
+
| Production Wells
 +
| No Violations
 
| This well is capable of production. The well has a pumping unit on it with rods and 2 tubing. The production valves are open from the wellhead to the tank pad. The identification for the well is located on the tank. There are no violations at this time.
 
| This well is capable of production. The well has a pumping unit on it with rods and 2 tubing. The production valves are open from the wellhead to the tank pad. The identification for the well is located on the tank. There are no violations at this time.
|
 
|
 
|
 
 
|-
 
|-
 +
| 1494683576
 +
| 2017-10-30
 +
| Plug / Plug Back
 +
| No Violations
 +
| I am on location today to witness the plugging operations  of this well. Today the bottom plug was bullheaded through the 4.5 inch diameter casing using 30 sacks of Class A cement. The rig crew then got setup to run their 4 inch ripping tools in the well. They were able to find free pipe and rip the 4.5 inch casing off at 1910 feet. After the casing was ripped the rig crew pulled out 1 joint to make sure the pipe was free before pumping the Big Lime plug. The plug was set from 1890-1690 feet. After the plug was set the 4.5 inch casing was then removed from the well.
 +
|-
 +
| 1700498778
 +
| 2018-06-15
 +
| Final Restoration
 +
| No Violations
 +
| I was on location today to do the final restoration on this well. At this time I was unable to pass the final restoration because the landowner told me they are waiting on some topsoil to be brought in to finish reclaiming the location. I gave her my business card and she will contact me when everything is complete.
 +
|-
 +
| 1896063330
 +
| 2017-11-02
 +
| Plug / Plug Back
 +
| No Violations
 +
| I have returned to this well today to witness the plugging of it. The rig crew has ripped the 7 inch casing at 719 feet and set a plug from 709-559 feet. They then pulled the 7 inch casing from the well.  A bottom of the surface plug was pumped for the 8 inch at 435-235 feet before the 8 inch casing was ripped at 160 feet and removed from the well. The rig crew topped the well off with a 100 foot surface plug. The cement stayed at the surface and did not settle. The well is plugged.
 
|-
 
|-
| PL6642
+
| 1923965150
|  
+
| 2006-05-03
|  
+
| Annular Disposal
| Preliminary Restoration  done information from Data Point
+
| No Violations
|
+
| No violations.
|
 
|  
 
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 02:01, 25 July 2019

Well Details

Well ID: 34-127-26589
Loading map...
Country: United States
State: Ohio
County: Perry
Municipality: Thorn Township
Operator Name: NGO DEVELOPMENT CORP.
Well Pad ID:
Farm/Lease Name: ODGEN
License Status: Final Restoration
License Date: 2019-01-31
Spud Date: 1985-03-21
Spud Drilling Contractor:
Final Drill Date: 1985-04-18
Well Total Depth: 2727 ft
Configuration: Vertical
Latitude: 39.875012860
Longitude: -82.39442507

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1985-02-27 1111 MERIDIAN ENERGY COMPANY GeoDate 2/27/85
Oil and Gas 1985-02-27 Issued Date 2/27/85 Expired Date 8/26/85 Acres 0020000 Tool Type CT Proposed Formation CLINTON Proposed Depth 02727 Proposed Drill Depth 02727
Original Spud 1985-03-21 GMM CHANGED PLUG STATUS PER PLUG REPORT
Completed 1985-04-18 GMM CHANGED PLUG STATUS PER PLUG REPORT
Reached Total Depth 1985-04-18 GMM CHANGED PLUG STATUS PER PLUG REPORT
Completion Report Received 1986-01-01 GMM CHANGED PLUG STATUS PER PLUG REPORT
CO 1993-01-26 424 NATIONAL PRODUCTION CORP GeoDate 2/27/85
CO 1996-03-04 98 NGO DEVELOPMENT CORP. GeoDate 2/27/85
APP 2017-08-25 Proposed Formations:CLINTON, Issued Date:8/25/2017, Expired Date:8/25/2019 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:HAD, Proposed Well Class:
Plugged/Abandoned 2017-11-02 GMM CHANGED PLUG STATUS PER PLUG REPORT
Record Last Modified 2019-06-05 GMM CHANGED PLUG STATUS PER PLUG REPORT
Construction Permit Expires 2019-08-25 GMM CHANGED PLUG STATUS PER PLUG REPORT

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 MERIDIAN ENERGY COMPANY 22138 0 0
1986 MERIDIAN ENERGY COMPANY 9115 0 365
1987 MERIDIAN ENERGY COMPANY 9421 0 365
1988 MERIDIAN ENERGY COMPANY 893 0 365
1993 NGO DEVELOPMENT CORP. 2892 0 365
1994 NGO DEVELOPMENT CORP. 6645 87 365
1995 NGO DEVELOPMENT CORP. 1004 0 365
1996 NGO DEVELOPMENT CORP. 1548 163 365
1997 NGO DEVELOPMENT CORP. 1595 87 365
1998 NGO DEVELOPMENT CORP. 2344 0 365
1999 NGO DEVELOPMENT CORP. 1279 157 365
2000 NGO DEVELOPMENT CORP. 329 123 0
2001 NGO DEVELOPMENT CORP. 476 60 365
2002 NGO DEVELOPMENT CORP. 308 0 365
2003 NGO DEVELOPMENT CORP. 66 83 365
2004 NGO DEVELOPMENT CORP. 21 46 365
2005 NGO DEVELOPMENT CORP. 70 33 365
2006 NGO DEVELOPMENT CORP. 59 53 365
2007 NGO DEVELOPMENT CORP. 0 43 365
2008 NGO DEVELOPMENT CORP. 8 52 365
2009 NGO DEVELOPMENT CORP. 18 0 365
2010 NGO DEVELOPMENT CORP. 83 0 365
2011 NGO DEVELOPMENT CORP. 0 0 365
2012 NGO DEVELOPMENT CORP. 0 0 366
2013 NGO DEVELOPMENT CORP. 0 0 365
2014 NGO DEVELOPMENT CORP. 0 0 365
2015 NGO DEVELOPMENT CORP. 0 0 365
2016 NGO DEVELOPMENT CORP. 0 36 365
2017 NGO DEVELOPMENT CORP. 0 0 306

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 MERIDIAN ENERGY COMPANY Brine 0 0
1986 MERIDIAN ENERGY COMPANY Brine 0 365
1987 MERIDIAN ENERGY COMPANY Brine 0 365
1988 MERIDIAN ENERGY COMPANY Brine 0 365
1993 NGO DEVELOPMENT CORP. Brine 0 365
1994 NGO DEVELOPMENT CORP. Brine 0 365
1995 NGO DEVELOPMENT CORP. Brine 54 365
1996 NGO DEVELOPMENT CORP. Brine 0 365
1997 NGO DEVELOPMENT CORP. Brine 13 365
1998 NGO DEVELOPMENT CORP. Brine 35 365
1999 NGO DEVELOPMENT CORP. Brine 136 365
2000 NGO DEVELOPMENT CORP. Brine 10
2001 NGO DEVELOPMENT CORP. Brine 37 365
2002 NGO DEVELOPMENT CORP. Brine 0 365
2003 NGO DEVELOPMENT CORP. Brine 45 365
2004 NGO DEVELOPMENT CORP. Brine 31 365
2005 NGO DEVELOPMENT CORP. Brine 0 365
2006 NGO DEVELOPMENT CORP. Brine 25 365
2007 NGO DEVELOPMENT CORP. Brine 35 365
2008 NGO DEVELOPMENT CORP. Brine 15 365
2009 NGO DEVELOPMENT CORP. Brine 90 365
2010 NGO DEVELOPMENT CORP. Brine 40 365
2011 NGO DEVELOPMENT CORP. Brine 0 365
2012 NGO DEVELOPMENT CORP. Brine 0 366
2013 NGO DEVELOPMENT CORP. Brine 26 365
2014 NGO DEVELOPMENT CORP. Brine 0 365
2015 NGO DEVELOPMENT CORP. Brine 0 365
2016 NGO DEVELOPMENT CORP. Brine 0 365
2017 NGO DEVELOPMENT CORP. Brine 0 306

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0000PL6642 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0371702305 2017-10-27 Plug / Plug Back No Violations Knox Energy has moved their service rig in on this well to plug it. Today they pulled out the rods and tubing from the well and they will start plugging the well on Monday.
0577837154 2019-01-31 Final Restoration No Violations I was on location today to complete the final restoration on this well. The final restoration meets 1509.072(B) requirements.
0629534659 2014-03-20 Production Wells No Violations This well is capable of production. The well has a pumping unit on it with rods and 2 tubing. The production valves are open from the wellhead to the tank pad. The identification for the well is located on the tank. There are no violations at this time.
1494683576 2017-10-30 Plug / Plug Back No Violations I am on location today to witness the plugging operations of this well. Today the bottom plug was bullheaded through the 4.5 inch diameter casing using 30 sacks of Class A cement. The rig crew then got setup to run their 4 inch ripping tools in the well. They were able to find free pipe and rip the 4.5 inch casing off at 1910 feet. After the casing was ripped the rig crew pulled out 1 joint to make sure the pipe was free before pumping the Big Lime plug. The plug was set from 1890-1690 feet. After the plug was set the 4.5 inch casing was then removed from the well.
1700498778 2018-06-15 Final Restoration No Violations I was on location today to do the final restoration on this well. At this time I was unable to pass the final restoration because the landowner told me they are waiting on some topsoil to be brought in to finish reclaiming the location. I gave her my business card and she will contact me when everything is complete.
1896063330 2017-11-02 Plug / Plug Back No Violations I have returned to this well today to witness the plugging of it. The rig crew has ripped the 7 inch casing at 719 feet and set a plug from 709-559 feet. They then pulled the 7 inch casing from the well. A bottom of the surface plug was pumped for the 8 inch at 435-235 feet before the 8 inch casing was ripped at 160 feet and removed from the well. The rig crew topped the well off with a 100 foot surface plug. The cement stayed at the surface and did not settle. The well is plugged.
1923965150 2006-05-03 Annular Disposal No Violations No violations.

For data sources see[7]

References