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Difference between revisions of "34-019-22230"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-019-22230
 
| Well ID: 34-019-22230
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.49779315, -81.07939332 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.497729031, -81.07957346 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Carroll County, Ohio|Carroll]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Carroll_County,_Ohio|Carroll]]
 +
|-
 +
| Municipality: [[Union_Township,_Carroll_County,_Ohio|Union Township]]
 
|-
 
|-
 
| Operator Name: [[CHESAPEAKE EXPLORATION LLC]]
 
| Operator Name: [[CHESAPEAKE EXPLORATION LLC]]
 
|-
 
|-
| Well Pad ID:  
+
| Well Pad ID: [[US-OH-000319]]
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: BRUNK 32-13-5
 
|-
 
|-
| First Permit Date:  
+
| License Status: Producing
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2012-12-20
 
|-
 
|-
 
| Spud Date: 2012-12-23
 
| Spud Date: 2012-12-23
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor: [[PATTERSON DRILLING]]
|-
 
| Configuration: Vertical
 
 
|-
 
|-
| Well Status: Producing
+
| Final Drill Date: 2013-01-04
 
|-
 
|-
| Violations: 0
+
| Well Total Depth: 13477 ft
 
|-
 
|-
| Latitude: 40.49779315
+
| Configuration: Horizontal
 
|-
 
|-
| Longitude: -81.07939332
+
| Latitude: 40.497729031
 
|-
 
|-
 +
| Longitude: -81.07957346
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Well Status
!scope="col" | GAS QUANTITY
+
!scope="col" style="width: 15%;text-align: center"| Well Status Date
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comment
!scope="col" | CONDENSATE QUANTITY
 
!scope="col" | CONDENSATE PRODUCTION DAYS
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
 
|-
 
|-
| 2013-12
+
| APP
| style="text-align:right;" | 112140.0
+
| 2012-10-01
|  
+
| Proposed Formations:TRENTON/BLACK RIVER, Issued Date:10/1/2012, Expired Date:10/1/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT
|
 
|
 
| style="text-align:right;" | 6729.0
 
|
 
 
|-
 
|-
 +
| APP
 +
| 2012-12-20
 +
| Proposed Formations:POINT PLEASANT, Issued Date:12/20/2012, Expired Date:12/20/2014 12:00:00 PM, Drilling unit acres:134.35, Proposed Well Type:OG, Proposed Well Class:EDPW
 
|-
 
|-
| 2013-6
+
| Reached Total Depth
| style="text-align:right;" | 18587.0
+
| 2013-01-04
|
 
|
 
|
 
| style="text-align:right;" | 540.0
 
 
|  
 
|  
 
|-
 
|-
 +
| Correction to Well
 +
| 2013-05-31
 +
| CORRECTION TO TARGET INFORMATION (FOOTAGE & X,Y COORDINATES) FROM AS DRILLED SURVEY PLAT.  TARGET TOWNSHIP CHANGED TO PERRY.  UNIT SIZE CHANGED TO 363.61 ACRES.
 
|-
 
|-
| 2013-9
+
| Completion Report Received
| style="text-align:right;" | 139532.0
+
| 2013-08-22
|
 
|
 
|
 
| style="text-align:right;" | 11433.0
 
 
|  
 
|  
 
|-
 
|-
|-
+
| Construction Permit Expires
| 2014-1
+
| 2014-12-20
| style="text-align:right;" | 97854.0
 
| style="text-align:right;" | 82.0
 
 
|  
 
|  
|
 
| style="text-align:right;" | 5583.0
 
| style="text-align:right;" | 82.0
 
|-
 
 
|-
 
|-
| 2014-4
+
| Record Last Modified
| style="text-align:right;" | 15246.0
+
| 2017-10-23
| style="text-align:right;" | 31.0
 
|
 
 
|  
 
|  
| style="text-align:right;" | 1143.0
 
| style="text-align:right;" | 31.0
 
|-
 
|-
 
| 2014-2
 
| style="text-align:right;" | 96931.0
 
| style="text-align:right;" | 88.0
 
|
 
|
 
| style="text-align:right;" | 4484.0
 
| style="text-align:right;" | 88.0
 
|-
 
|-
 
| 2014-3
 
| style="text-align:right;" | 81575.0
 
| style="text-align:right;" | 91.0
 
|
 
|
 
| style="text-align:right;" | 3512.0
 
| style="text-align:right;" | 91.0
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 
|-
 
|-
| 2015-1
+
| 2013-09-16
| style="text-align:right;" | 51414.0
+
| style="text-align: right;" | 8655
| style="text-align:right;" | 89.0
+
| style="text-align: right;" | 13314
|
+
| style="text-align: right;" | 700
|
 
| style="text-align:right;" | 4056.0
 
| style="text-align:right;" | 89.0
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Perfs Table
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== Inspection Data ==
+
== Fracking Activities ==
 +
==== Fracking Jobs ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Job Number
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Job Start Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Job End Date
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| True Vertical Depth (ft)
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Total Water Volume (gal)
!scope="col" | VIOLATION CODE
+
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
| 1356365406
+
| 1
| 2012-12-24
+
| 04/05/2013
|  
+
| 04/07/2013
| I was on site to witness the cementing of the 13 3/8 casing. My inspection revealed that Patterson Rig# 328 has drilled a 17.5 hole to a total depth of 605'. They ran 589' of 13 3/8 casing (54.5 pound per foot) and installed six bowspring centralizers on joints 1,2,3,6,9,12. O-TEX cemented the casing with 540 sacks of Class H cement with 2% CaCl ; .27% Cello-Flake; and 4/10% C-41P. They pumped 115.41 barrels of cement slurry with a density of 15.6 pounds per gallon, 1.2 yield cubic feet per sack, and 5.25 gallons of mix water per sack. They displaced the plug with 84 barrels of water and bumped the plug at 11:14 am with 275 PSI. There was good circulation throughout the job and 24 barrels of cement was circulated to surface. They conducted the casing test at 1100 PSI for 5 minutes and the casing test approved. Inspection of the well site revealed no violations at this time. Note: Drilling rig had trouble with pumps being frozen and steel pits being filled to maximum capacity. The drilling rig had to wait on a roll off tank before O-TEX could conduct the cement job.
+
| style="text-align: right;" | 7947
|  
+
| style="text-align: right;" | 3,838,130.0
|
+
| style="text-align: right;" | 325127
|  
 
 
|-
 
|-
 +
|}
 +
==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 
|-
 
|-
| 1356590650
+
|- valign="top"
| 2012-12-26
+
| rowspan="36"| 1
|  
+
| rowspan="1"| Fresh Water
| I was on site to witness the cementing of the 9 5/8 intermediate casing. My inspection revealed that Patterson Rig # 328 has drilled a 12 1/4 hole to a total depth of 2240'. They ran 2222' of (40# per foot) 9 5/8 casing and installed 15 bowspring centralizers on joints 1,2,3,6,9,12,15,18,21,24,27,30,33,36,39. O-TEX cemented the casing with 790 sacks of Class H cement with 10% NaCl; .27% Cello-Flake; 4/10% C-41P (powder defoamer); 1/10% C35 (dispersant). The cement had a density of 15.6 pounds per gallon, a yield of 1.24 cubic feet per sack, and they used 5.48 gallons per sack of mix water. O-TEX pumped 162 barrels of freshwater to displace the plug. There was good circulation throughout the job and 33 barrels of cement was circulated to surface. They landed the plug at 7:26pm with 960 PSI and went straight into the casing test with 1470 PSI. Casing test was conducted for 5 minutes at 1470 PSI and the test was approved. My inspection of the well site revealed no violations at this time.
+
| rowspan="1"| CHESAPEAKE ENERGY
|
+
| rowspan="1"| Carrier/Base Fluid
|
+
| Water
|  
+
| 007732-18-5
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 79.5092
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
|- valign="top"
 +
| rowspan="1"| Recycled Produced Water
 +
| rowspan="1"| CHESAPEAKE ENERGY
 +
| rowspan="1"| Carrier/Base Fluid
 +
| Water
 +
| 007732-18-5
 +
| style="text-align: right;" | 100
 +
| style="text-align: right;" | 4.13702
 +
| style="text-align: right;" | 0
 
|-
 
|-
| -225703457
+
|- valign="top"
| 2013-01-03
+
| rowspan="34"| Acid, Hydrochloric 15pct, A264
|  
+
B244, B317, J218, J475, J580
| I inspected this drill site on 1/3/2013. Patterson Drilling's Rig # 328 was found to be drilling at 8978' during the curve section of the hole. Hole size was 8.75. All operations observed were in compliance.
+
J609, J610, L058, L071, 100 Mesh Sand
|  
+
Northern White Sand
|  
+
| rowspan="34"| SCHLUMBERGER
|  
+
| rowspan="34"| Acid, Anti-Bacterial Agent, Breaker, Corrosion Inhibitor, Cross Linker, Friction Reducer, Gelling Agent, Iron Control Agent, KCl Substitute, Scale Inhibitor, Proppant - Natural
 +
| Sodium erythorbate
 +
| 6381-77-7
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00071
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| Decamethyl cyclopentasiloxane
 +
| 541-02-6
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00001000
 +
| style="text-align: right;" | 0
 
|-
 
|-
| -474897550
+
| Polymer of 2-acrylamido-2-methylpropanesulfonic acid sodium salt and methyl acrylate
| 2014-04-08
+
| 136793-29-8
|
+
| style="text-align: right;" | 0
| I inspected the well site and found the well head to be constructed with a Christmas tree valve and piping. There are six wells at this site. The condensate tanks and piping runs were all intact with no leaks. The spray lined steel containment around the condensate tanks had rain water in it with no visible contamination. The diesel power unit was found to have excess oil in the spill containment under the engine. The pre-heater unit had no visible issues. While I was finishing my inspection, the contractor was there to clean up the oil under the diesel engine. No oil reached the ground. The lease road is stable condition and the site is well secured with two locked gates. No violations were found.
+
| style="text-align: right;" | 0.00059
|
+
| style="text-align: right;" | 0
|
 
|
 
|-
 
|}
 
For data sources see<ref>{{cite web
 
| title = Ohio Department of Natural Resources RBDMS
 
| publisher = [http://oilandgas.ohiodnr.gov/]
 
| date = 2015-06-19
 
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 
| accessdate = 2015-06-20 }}</ref>
 
[[Category:Has Chemical Data]]
 
==Chemical Data==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | HF Fluid Concentration
 
!scope="col" | Ingredient
 
!scope="col" | Additive Concentration
 
!scope="col" | Trade Name
 
!scope="col" | Purpose
 
!scope="col" | CAS number
 
!scope="col" | Supplier
 
 
|-
 
|-
| 4.13702
 
 
| Water
 
| Water
| 100.0
 
| Recycled Produced Water
 
| Carrier/Base Fluid
 
 
| 007732-18-5
 
| 007732-18-5
| CHESAPEAKE ENERGY
+
| style="text-align: right;" | 4.58
 +
| style="text-align: right;" | 0.75012
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| Trisodium ortho phosphate
 +
| 7601-54-9
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00073
 +
| style="text-align: right;" | 0
 +
|-
 +
| Magnesium silicate hydrate (talc)
 +
| 14807-96-6
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00003000
 +
| style="text-align: right;" | 0
 +
|-
 +
| Crystalline silica
 +
| 14808-60-7
 +
| style="text-align: right;" | 97.74
 +
| style="text-align: right;" | 15.2504
 +
| style="text-align: right;" | 0
 +
|-
 +
| Fatty acids, tall-oil
 +
| 61790-12-3
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00037
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 0.00029
+
| Cholinium chloride
| Non-crystalline silica
+
| 67-48-1
| 0.0
+
| style="text-align: right;" | 0.43
| Acid
+
| style="text-align: right;" | 0.06712
| A264
+
| style="text-align: right;" | 0
| 7631-86-9
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| Guar gum
 +
| 9000-30-0
 +
| style="text-align: right;" | 0.57
 +
| style="text-align: right;" | 0.08831
 +
| style="text-align: right;" | 0
 +
|-
 +
| Potassium borate
 +
| 1332-77-0
 +
| style="text-align: right;" | 0.08
 +
| style="text-align: right;" | 0.01207
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 0.00036
 
 
| Urea
 
| Urea
| 0.0
 
| Acid
 
|  A264
 
 
| 57-13-6
 
| 57-13-6
| Hydrochloric 15pct
+
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00036
 +
| style="text-align: right;" | 0
 
|-
 
|-
 +
| Dodecamethylcyclohexasiloxane
 +
| 540-97-6
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00001000
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 9e-05
+
| Alcohols, C14-15, ethoxylated (7EO)
| Prop-2-yn-1-ol
+
| 68951-67-7
| 0.0
+
| style="text-align: right;" | 0
| Acid
+
| style="text-align: right;" | 0.00014
| A264
+
| style="text-align: right;" | 0
| 107-19-7
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| Octamethylcyclotetrasiloxane
 +
| 556-67-2
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00001000
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 0.00307
+
| Alkenes, C>10 a-
| Diammonium peroxidisulphate
+
| 64743-02-8
| 0.02
+
| style="text-align: right;" | 0
| Acid
+
| style="text-align: right;" | 0.00006000
| A264
+
| style="text-align: right;" | 0
| 7727-54-0
 
|  Hydrochloric 15pct
 
 
|-
 
|-
 +
| Prop-2-yn-1-ol
 +
| 107-19-7
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00009000
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 0.0
+
| Acrylamide, 2-acrylamido-2-methylpropanesulfonic acid, sodium salt polymer
| Ethane-1
+
| 38193-60-1
| 107.0
+
| style="text-align: right;" | 0.04
| Acid
+
| style="text-align: right;" | 0.0055
| A264
+
| style="text-align: right;" | 0
| 2-diol
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| Ammonium sulfate
 +
| 7783-20-2
 +
| style="text-align: right;" | 0.03
 +
| style="text-align: right;" | 0.00519
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1e-05
+
| Methanol
| Dimethyl siloxanes and silicones
+
| 67-56-1
| 0.0
+
| style="text-align: right;" | 0
| Acid
+
| style="text-align: right;" | 0.0005
| A264
+
| style="text-align: right;" | 0
| 63148-62-9
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| Vinylidene chloride/methylacrylate copolymer
 +
| 25038-72-6
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00049
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 0.00073
+
| Potassium hydroxide
| Trisodium ortho phosphate
+
| 1310-58-3
| 0.0
+
| style="text-align: right;" | 0.03
| Acid
+
| style="text-align: right;" | 0.00394
| A264
+
| style="text-align: right;" | 0
| 7601-54-9
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| Non-crystalline silica
 +
| 7631-86-9
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00029
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1e-05
+
| Glycerol
| Decamethyl cyclopentasiloxane
+
| 56-81-5
| 0.0
+
| style="text-align: right;" | 0.03
| Acid
+
| style="text-align: right;" | 0.00394
| A264
+
| style="text-align: right;" | 0
| 541-02-6
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| Thiourea, polymer with formaldehyde and 1-phenylethanone
 +
| 68527-49-1
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.0003
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 0.0
+
| Glutaraldehyde
| Thiourea
+
| 111-30-8
| 68527.0
+
| style="text-align: right;" | 0.04
| Acid
+
| style="text-align: right;" | 0.00546
| A264
+
| style="text-align: right;" | 0
| polymer with formal
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| Sodium hydroxide
 +
| 1310-73-2
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00001000
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 0.0005
+
| Ethane-1,2-diol
| Methanol
+
| 107-21-1
| 0.0
+
| style="text-align: right;" | 0
| Acid
+
| style="text-align: right;" | 0.00021
| A264
+
| style="text-align: right;" | 0
| 67-56-1
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| Hydrogen chloride
 +
| 7647-01-0
 +
| style="text-align: right;" | 1.02
 +
| style="text-align: right;" | 0.15901
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 0.00049
+
| Tetrasodium ethylenediaminetetraacetate
| Vinylidene chloride/methylacrylate copolymer
+
| 64-02-8
| 0.0
+
| style="text-align: right;" | 0
| Acid
+
| style="text-align: right;" | 0.00001000
| A264
+
| style="text-align: right;" | 0
| 25038-72-6
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| Diammonium peroxidisulphate
 +
| 7727-54-0
 +
| style="text-align: right;" | 0.02
 +
| style="text-align: right;" | 0.00307
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1e-05
+
| Sodium sulfate
| Dodecamethylcyclohexasiloxane
+
| 7757-82-6
| 0.0
+
| style="text-align: right;" | 0.01
| Acid
+
| style="text-align: right;" | 0.00224
| A264
+
| style="text-align: right;" | 0
| 540-97-6
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| Siloxanes and Silicones, di-Me, reaction products with silica
 +
| 67762-90-7
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00001000
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 0.00071
+
| Dimethyl siloxanes and silicones
| Sodium erythorbate
+
| 63148-62-9
| 0.0
+
| style="text-align: right;" | 0
| Acid
+
| style="text-align: right;" | 0.00001000
| A264
+
| style="text-align: right;" | 0
| 6381-77-7
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = FracFocus Fracking Chemicals Database
 +
| date = 2019-04-02
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-06-19 }}</ref>
 +
== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 68951.0
+
| 2013-04-07
| Alcohols
+
| H2O
| 0.0
+
| style="text-align: right;" | 15
| Acid
+
| style="text-align: right;" | 6161 Bbl
| A264
+
| style="text-align: right;" | 404081
| C14-15
+
| [[Schlumberger]]
| Hydrochloric 15pct
+
| STAGE 14
 +
50 SHOTS
 
|-
 
|-
 +
| 2013-04-05
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 5755 Bbl
 +
| style="text-align: right;" | 407300
 +
| [[Schlumberger]]
 +
| STAGE 1
 +
50 SHOTS
 
|-
 
|-
| 38193.0
+
| 2013-04-05
| Acrylamide
+
| H2O
| 0.0
+
| style="text-align: right;" | 15
| Acid
+
| style="text-align: right;" | 5920 Bbl
| A264
+
| style="text-align: right;" | 407361
| 2-acrylamido-2-meth
+
| [[Schlumberger]]
|  Hydrochloric 15pct
+
| STAGE 2
 +
50 SHOTS
 
|-
 
|-
 +
| 2013-04-05
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 6056 Bbl
 +
| style="text-align: right;" | 405061
 +
| [[Schlumberger]]
 +
| STAGE 4
 +
50 SHOTS
 
|-
 
|-
| 0.0
+
| 2013-04-06
| Fatty acids
+
| H2O
| 61790.0
+
| style="text-align: right;" | 15
| Acid
+
| style="text-align: right;" | 6071 Bbl
| A264
+
| style="text-align: right;" | 408781
| tall-oil
+
| [[Schlumberger]]
| Hydrochloric 15pct
+
| STAGE 7
 +
50 SHOTS
 
|-
 
|-
 +
| 2013-04-06
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 6370 Bbl
 +
| style="text-align: right;" | 405981
 +
| [[Schlumberger]]
 +
| STAGE 11
 +
50 SHOTS
 
|-
 
|-
| 0.15901
+
| 2013-04-06
| Hydrogen chloride
+
| H2O
| 1.02
+
| style="text-align: right;" | 15
| Acid
+
| style="text-align: right;" | 5909 Bbl
| A264
+
| style="text-align: right;" | 406571
| 7647-01-0
+
| [[Schlumberger]]
| Hydrochloric 15pct
+
| STAGE 6
 +
50 SHOTS
 
|-
 
|-
 +
| 2013-04-06
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 6380 Bbl
 +
| style="text-align: right;" | 409401
 +
| [[Schlumberger]]
 +
| STAGE 9
 +
50 SHOTS
 
|-
 
|-
| 67762.0
+
| 2013-04-05
| Siloxanes and Silicones
+
| H2O
| 0.0
+
| style="text-align: right;" | 15
| Acid
+
| style="text-align: right;" | 5825 Bbl
| A264
+
| style="text-align: right;" | 4091800
| di-Me
+
| [[Schlumberger]]
| Hydrochloric 15pct
+
| STAGE 5
 +
50 SHOTS
 
|-
 
|-
 +
| 2013-04-07
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 5930 Bbl
 +
| style="text-align: right;" | 402440
 +
| [[Schlumberger]]
 +
| STAGE 13
 +
50 SHOTS
 
|-
 
|-
| 0.00224
+
| 2013-04-05
| Sodium sulfate
+
| H2O
| 0.01
+
| style="text-align: right;" | 15
| Acid
+
| style="text-align: right;" | 5996 Bbl
| A264
+
| style="text-align: right;" | 407321
| 7757-82-6
+
| [[Schlumberger]]
| Hydrochloric 15pct
+
| STAGE 3
|-
+
50 SHOTS
 
|-
 
|-
| 1e-05
+
| 2013-04-06
| Sodium hydroxide
+
| H2O
| 0.0
+
| style="text-align: right;" | 15
| Acid
+
| style="text-align: right;" | 6417 Bbl
| A264
+
| style="text-align: right;" | 405161
| 1310-73-2
+
| [[Schlumberger]]
| Hydrochloric 15pct
+
| STAGE 12
 +
50 SHOTS
 
|-
 
|-
 +
| 2013-04-06
 +
| H2O
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 6027 Bbl
 +
| style="text-align: right;" | 408011
 +
| [[Schlumberger]]
 +
| STAGE 8
 +
50 SHOTS
 
|-
 
|-
| 1e-05
+
| 2013-04-06
| Tetrasodium ethylenediaminetetraacetate
+
| H2O
| 0.0
+
| style="text-align: right;" | 15
| Acid
+
| style="text-align: right;" | 6341 Bbl
| A264
+
| style="text-align: right;" | 411141
| 64-02-8
+
| [[Schlumberger]]
| Hydrochloric 15pct
+
| STAGE 10
 +
50 SHOTS
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 0.75012
+
| 2013
| Water
+
| [[CHESAPEAKE EXPLORATION LLC]]
| 4.58
+
| style="text-align: right;" | 270259
| Acid
+
| style="text-align: right;" | 18702
| A264
+
| style="text-align: right;" | 181
| 007732-18-5
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| 2014
 +
| [[CHESAPEAKE EXPLORATION LLC]]
 +
| style="text-align: right;" | 291606
 +
| style="text-align: right;" | 14722
 +
| style="text-align: right;" | 292
 
|-
 
|-
| 0.00059
+
| 2015
| Polymer of 2-acrylamido-2-methylpropanesulfonic acid sodium salt and methyl acrylate
+
| [[CHESAPEAKE EXPLORATION LLC]]
| 0.0
+
| style="text-align: right;" | 174486
| Acid
+
| style="text-align: right;" | 10844
| A264
+
| style="text-align: right;" | 362
| 136793-29-8
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| 2016
 +
| [[CHESAPEAKE EXPLORATION LLC]]
 +
| style="text-align: right;" | 155988
 +
| style="text-align: right;" | 6614
 +
| style="text-align: right;" | 366
 
|-
 
|-
| 0.00546
+
| 2017
| Glutaraldehyde
+
| [[CHESAPEAKE EXPLORATION LLC]]
| 0.04
+
| style="text-align: right;" | 131427
| Acid
+
| style="text-align: right;" | 4316
| A264
+
| style="text-align: right;" | 349
| 111-30-8
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| 2018
 +
| [[CHESAPEAKE EXPLORATION LLC]]
 +
| style="text-align: right;" | 115338
 +
| style="text-align: right;" | 3629
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 0.08831
+
| 2019
| Guar gum
+
| [[CHESAPEAKE EXPLORATION LLC]]
| 0.57
+
| style="text-align: right;" | 26651
| Acid
+
| style="text-align: right;" | 797
| A264
+
| style="text-align: right;" | 90
| 9000-30-0
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 1e-05
+
| 2013
| Octamethylcyclotetrasiloxane
+
| [[CHESAPEAKE EXPLORATION LLC]]
| 0.0
+
| Brine
| Acid
+
| style="text-align: right;" | 7770
| A264
+
| style="text-align: right;" | 181
| 556-67-2
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| 2014
 +
| [[CHESAPEAKE EXPLORATION LLC]]
 +
| Brine
 +
| style="text-align: right;" | 6638
 +
| style="text-align: right;" | 292
 
|-
 
|-
| 0.01207
+
| 2015
| Potassium borate
+
| [[CHESAPEAKE EXPLORATION LLC]]
| 0.08
+
| Brine
| Acid
+
| style="text-align: right;" | 9221
| A264
+
| style="text-align: right;" | 362
| 1332-77-0
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| 2016
 +
| [[CHESAPEAKE EXPLORATION LLC]]
 +
| Brine
 +
| style="text-align: right;" | 2607
 +
| style="text-align: right;" | 366
 
|-
 
|-
| 0.00394
+
| 2017
| Potassium hydroxide
+
| [[CHESAPEAKE EXPLORATION LLC]]
| 0.03
+
| Brine
| Acid
+
| style="text-align: right;" | 2011
| A264
+
| style="text-align: right;" | 349
| 1310-58-3
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| 2018
 +
| [[CHESAPEAKE EXPLORATION LLC]]
 +
| Brine
 +
| style="text-align: right;" | 1454
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 0.00394
+
| 2019
| Glycerol
+
| [[CHESAPEAKE EXPLORATION LLC]]
| 0.03
+
| Brine
| Acid
+
| style="text-align: right;" | 363
| A264
+
| style="text-align: right;" | 90
| 56-81-5
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Inspection Data ==
 +
==== Inspections Performed ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Inspection Date
 +
!scope="col" style="text-align: center"| Inspection Type
 +
!scope="col" style="text-align: center"| Inspection Result
 +
!scope="col" style="text-align: center"| Inspection Comments
 
|-
 
|-
| 0.0
+
| 0225703457
| Alkenes
+
| 2013-01-03
| 64743.0
+
| Drill / Deepen / Reopen
| Acid
+
| No Violations
A264
+
| I inspected this drill site on 1/3/2013. Patterson Drillings Rig # 328 was found to be drilling at 8978 during the curve section of the hole. Hole size was 8.75. All operations observed were in compliance.
| C>10 a-
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| 0474897550
 +
| 2014-04-08
 +
| Production Wells
 +
| No Violations
 +
| I inspected the well site and found the well head to be constructed with a Christmas tree valve and piping. There are six wells at this site. The condensate tanks and piping runs were all intact with no leaks. The spray lined steel containment around the condensate tanks had rain water in it with no visible contamination. The diesel power unit was found to have excess oil in the spill containment under the engine. The pre-heater unit had no visible issues. While I was finishing my inspection, the contractor was there to clean up the oil under the diesel engine. No oil reached the ground. The lease road is stable condition and the site is well secured with two locked gates. No violations were found.
 
|-
 
|-
| 0.00519
+
| 1062334224
| Ammonium sulfate
+
| 2018-04-25
| 0.03
+
| Production Wells
| Acid
+
| No Violations
A264
+
| I conducted a follow-up inspection to complaint #5646 regarding noise from the pad. The surface/intermediate and intermediate/production annular gauges displayed readings of zero psi.    No anomalies were observed on the pad. Sound barriers were still installed around the compressor units. The complaint will be closed.
| 7783-20-2
 
| Hydrochloric 15pct
 
 
|-
 
|-
 +
| 1356365406
 +
| 2012-12-24
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| I was on site to witness the cementing of the 13 3/8 casing. My inspection revealed that Patterson Rig# 328 has drilled a 17.5 hole to a total depth of 605. They ran 589 of 13 3/8 casing (54.5 pound per foot) and installed six bowspring centralizers on joints 1,2,3,6,9,12. O-TEX cemented the casing with 540 sacks of Class H cement with 2% CaCl ; .27% Cello-Flake; and 4/10% C-41P. They pumped 115.41 barrels of cement slurry with a density of 15.6 pounds per gallon, 1.2 yield cubic feet per sack, and 5.25 gallons of mix water per sack. They displaced the plug with 84 barrels of water and bumped the plug at 11:14 am with 275 PSI. There was good circulation throughout the job and 24 barrels of cement was circulated to surface. They conducted the casing test at 1100 PSI for 5 minutes and the casing test approved. Inspection of the well site revealed no violations at this time. Note: Drilling rig had trouble with pumps being frozen and steel pits being filled to maximum capacity. The drilling rig had to wait on a roll off tank before O-TEX could conduct the cement job.
 
|-
 
|-
| 3e-05
+
| 1356590650
| Magnesium silicate hydrate (talc)
+
| 2012-12-26
| 0.0
+
| Drill / Deepen /  Reopen
| Acid
+
| No Violations
A264
+
I was on site to witness the cementing of the 9 5/8 intermediate casing. My inspection revealed that Patterson Rig # 328 has drilled a 12 1/4 hole to a total depth of 2240. They ran 2222 of (40# per foot) 9 5/8 casing and installed 15 bowspring centralizers on joints 1,2,3,6,9,12,15,18,21,24,27,30,33,36,39. O-TEX cemented the casing with 790 sacks of Class H cement with 10% NaCl; .27% Cello-Flake; 4/10% C-41P (powder defoamer); 1/10% C35 (dispersant). The cement had a density of 15.6 pounds per gallon, a yield of 1.24 cubic feet per sack, and they used 5.48 gallons per sack of mix water. O-TEX pumped 162 barrels of freshwater to displace the plug. There was good circulation throughout the job and 33 barrels of cement was circulated to surface. They landed the plug at 7:26pm with 960 PSI and went straight into the casing test with 1470 PSI. Casing test was conducted for 5 minutes at 1470 PSI and the test was approved. My inspection of the well site revealed no violations at this time.
| 14807-96-6
 
|  Hydrochloric 15pct
 
 
|-
 
|-
 +
| 1385767521
 +
| 2017-07-26
 +
| Production Wells
 +
| No Violations
 +
| I followed-up in response to complaint #5646 regarding noise issues on the pad.  Sound barriers had been installed and were present around the two compressors on the east side of the pad.  No other changes were made to the well or pad since my last inspection.
 
|-
 
|-
| 79.5092
+
| 1419681860
| Water
+
| 2015-10-26
| 100.0
+
| Preliminary Restoration
| Fresh Water
+
| No Violations
| Carrier/Base Fluid
+
| I was on location to conduct a preliminary restoration inspection.  The well is equipped with a plunger lift unit.  Jersey barriers were installed around the wellhead.  The well is properly identified with a clear, legibly-marked well identification sign.  The tank battery consisted of eight, 400 BBL production tanks and was diked. The tanks are located within a spray-lined and sealed secondary containment.  There are e-stops outside the barriers, and the tanks are grounded, and have static dissipators.  There is a truck grounding area for trucks collecting condensate and/or produced water.  Lightning protection and a windsock are installed on top of the production tanks.  Other production equipment on the well pad consisted of:
| 007732-18-5
+
 
| CHESAPEAKE ENERGY
+
 
 +
 
 +
 
 +
Jersey barriers are installed around the production equipment.  The entire well pad is enclosed with a six-foot high, chain link fence with three-strand barbed wire and the man doors were locked.  Along the interior of the chain link fence there is an earthen berm and it was stable. The soil stockpile is well-stabilized with vegetation.  Drainage and erosion controls at the pad are in place and functioning.  A closed-loop, above-ground drilling pit system was used, so there are no earthen pits requiring closure.  The pad has a crushed limestone surface, and is in good repair.  The lease road is stable and drivable.  Preliminary restoration passed.
 
|-
 
|-
 
|}
 
|}
For data sources see<ref>{{cite web | title = FracFocus Chemical Disclosure Registry |publisher = [http://www.fracfocusdata.org/DisclosureSearch/]| date = 2015-08-10 | url = http://wellwiki.org/wiki/Well_Chemicals_Data_Sources | accessdate = 2015-08-10 }}</ref>
+
<!--==== Violations Commited ====
== References ==
+
{| class="wikitable sortable" width="95%"
{{reflist}}
+
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
==References==
 +
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]
 +
[[Category:FracFocus]]

Revision as of 07:54, 31 July 2019

Well Details

Well ID: 34-019-22230
Loading map...
Country: United States
State: Ohio
County: Carroll
Municipality: Union Township
Operator Name: CHESAPEAKE EXPLORATION LLC
Well Pad ID: US-OH-000319
Farm/Lease Name: BRUNK 32-13-5
License Status: Producing
License Date: 2012-12-20
Spud Date: 2012-12-23
Spud Drilling Contractor: PATTERSON DRILLING
Final Drill Date: 2013-01-04
Well Total Depth: 13477 ft
Configuration: Horizontal
Latitude: 40.497729031
Longitude: -81.07957346

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2012-10-01 Proposed Formations:TRENTON/BLACK RIVER, Issued Date:10/1/2012, Expired Date:10/1/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT
APP 2012-12-20 Proposed Formations:POINT PLEASANT, Issued Date:12/20/2012, Expired Date:12/20/2014 12:00:00 PM, Drilling unit acres:134.35, Proposed Well Type:OG, Proposed Well Class:EDPW
Reached Total Depth 2013-01-04
Correction to Well 2013-05-31 CORRECTION TO TARGET INFORMATION (FOOTAGE & X,Y COORDINATES) FROM AS DRILLED SURVEY PLAT. TARGET TOWNSHIP CHANGED TO PERRY. UNIT SIZE CHANGED TO 363.61 ACRES.
Completion Report Received 2013-08-22
Construction Permit Expires 2014-12-20
Record Last Modified 2017-10-23

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2013-09-16 8655 13314 700

For data sources see[3]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 04/05/2013 04/07/2013 7947 3,838,130.0 325127

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 Fresh Water CHESAPEAKE ENERGY Carrier/Base Fluid Water 007732-18-5 100 79.5092 0
Recycled Produced Water CHESAPEAKE ENERGY Carrier/Base Fluid Water 007732-18-5 100 4.13702 0
Acid, Hydrochloric 15pct, A264
B244, B317, J218, J475, J580
J609, J610, L058, L071, 100 Mesh Sand
Northern White Sand
SCHLUMBERGER Acid, Anti-Bacterial Agent, Breaker, Corrosion Inhibitor, Cross Linker, Friction Reducer, Gelling Agent, Iron Control Agent, KCl Substitute, Scale Inhibitor, Proppant - Natural Sodium erythorbate 6381-77-7 0 0.00071 0
Decamethyl cyclopentasiloxane 541-02-6 0 0.00001000 0
Polymer of 2-acrylamido-2-methylpropanesulfonic acid sodium salt and methyl acrylate 136793-29-8 0 0.00059 0
Water 007732-18-5 4.58 0.75012 0
Trisodium ortho phosphate 7601-54-9 0 0.00073 0
Magnesium silicate hydrate (talc) 14807-96-6 0 0.00003000 0
Crystalline silica 14808-60-7 97.74 15.2504 0
Fatty acids, tall-oil 61790-12-3 0 0.00037 0
Cholinium chloride 67-48-1 0.43 0.06712 0
Guar gum 9000-30-0 0.57 0.08831 0
Potassium borate 1332-77-0 0.08 0.01207 0
Urea 57-13-6 0 0.00036 0
Dodecamethylcyclohexasiloxane 540-97-6 0 0.00001000 0
Alcohols, C14-15, ethoxylated (7EO) 68951-67-7 0 0.00014 0
Octamethylcyclotetrasiloxane 556-67-2 0 0.00001000 0
Alkenes, C>10 a- 64743-02-8 0 0.00006000 0
Prop-2-yn-1-ol 107-19-7 0 0.00009000 0
Acrylamide, 2-acrylamido-2-methylpropanesulfonic acid, sodium salt polymer 38193-60-1 0.04 0.0055 0
Ammonium sulfate 7783-20-2 0.03 0.00519 0
Methanol 67-56-1 0 0.0005 0
Vinylidene chloride/methylacrylate copolymer 25038-72-6 0 0.00049 0
Potassium hydroxide 1310-58-3 0.03 0.00394 0
Non-crystalline silica 7631-86-9 0 0.00029 0
Glycerol 56-81-5 0.03 0.00394 0
Thiourea, polymer with formaldehyde and 1-phenylethanone 68527-49-1 0 0.0003 0
Glutaraldehyde 111-30-8 0.04 0.00546 0
Sodium hydroxide 1310-73-2 0 0.00001000 0
Ethane-1,2-diol 107-21-1 0 0.00021 0
Hydrogen chloride 7647-01-0 1.02 0.15901 0
Tetrasodium ethylenediaminetetraacetate 64-02-8 0 0.00001000 0
Diammonium peroxidisulphate 7727-54-0 0.02 0.00307 0
Sodium sulfate 7757-82-6 0.01 0.00224 0
Siloxanes and Silicones, di-Me, reaction products with silica 67762-90-7 0 0.00001000 0
Dimethyl siloxanes and silicones 63148-62-9 0 0.00001000 0

For data sources see[4]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2013-04-07 H2O 15 6161 Bbl 404081 Schlumberger STAGE 14

50 SHOTS

2013-04-05 H2O 15 5755 Bbl 407300 Schlumberger STAGE 1

50 SHOTS

2013-04-05 H2O 15 5920 Bbl 407361 Schlumberger STAGE 2

50 SHOTS

2013-04-05 H2O 15 6056 Bbl 405061 Schlumberger STAGE 4

50 SHOTS

2013-04-06 H2O 15 6071 Bbl 408781 Schlumberger STAGE 7

50 SHOTS

2013-04-06 H2O 15 6370 Bbl 405981 Schlumberger STAGE 11

50 SHOTS

2013-04-06 H2O 15 5909 Bbl 406571 Schlumberger STAGE 6

50 SHOTS

2013-04-06 H2O 15 6380 Bbl 409401 Schlumberger STAGE 9

50 SHOTS

2013-04-05 H2O 15 5825 Bbl 4091800 Schlumberger STAGE 5

50 SHOTS

2013-04-07 H2O 15 5930 Bbl 402440 Schlumberger STAGE 13

50 SHOTS

2013-04-05 H2O 15 5996 Bbl 407321 Schlumberger STAGE 3

50 SHOTS

2013-04-06 H2O 15 6417 Bbl 405161 Schlumberger STAGE 12

50 SHOTS

2013-04-06 H2O 15 6027 Bbl 408011 Schlumberger STAGE 8

50 SHOTS

2013-04-06 H2O 15 6341 Bbl 411141 Schlumberger STAGE 10

50 SHOTS

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2013 CHESAPEAKE EXPLORATION LLC 270259 18702 181
2014 CHESAPEAKE EXPLORATION LLC 291606 14722 292
2015 CHESAPEAKE EXPLORATION LLC 174486 10844 362
2016 CHESAPEAKE EXPLORATION LLC 155988 6614 366
2017 CHESAPEAKE EXPLORATION LLC 131427 4316 349
2018 CHESAPEAKE EXPLORATION LLC 115338 3629 365
2019 CHESAPEAKE EXPLORATION LLC 26651 797 90

For data sources see[6] [7]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2013 CHESAPEAKE EXPLORATION LLC Brine 7770 181
2014 CHESAPEAKE EXPLORATION LLC Brine 6638 292
2015 CHESAPEAKE EXPLORATION LLC Brine 9221 362
2016 CHESAPEAKE EXPLORATION LLC Brine 2607 366
2017 CHESAPEAKE EXPLORATION LLC Brine 2011 349
2018 CHESAPEAKE EXPLORATION LLC Brine 1454 365
2019 CHESAPEAKE EXPLORATION LLC Brine 363 90

For data sources see[8] [9]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0225703457 2013-01-03 Drill / Deepen / Reopen No Violations I inspected this drill site on 1/3/2013. Patterson Drillings Rig # 328 was found to be drilling at 8978 during the curve section of the hole. Hole size was 8.75. All operations observed were in compliance.
0474897550 2014-04-08 Production Wells No Violations I inspected the well site and found the well head to be constructed with a Christmas tree valve and piping. There are six wells at this site. The condensate tanks and piping runs were all intact with no leaks. The spray lined steel containment around the condensate tanks had rain water in it with no visible contamination. The diesel power unit was found to have excess oil in the spill containment under the engine. The pre-heater unit had no visible issues. While I was finishing my inspection, the contractor was there to clean up the oil under the diesel engine. No oil reached the ground. The lease road is stable condition and the site is well secured with two locked gates. No violations were found.
1062334224 2018-04-25 Production Wells No Violations I conducted a follow-up inspection to complaint #5646 regarding noise from the pad. The surface/intermediate and intermediate/production annular gauges displayed readings of zero psi. No anomalies were observed on the pad. Sound barriers were still installed around the compressor units. The complaint will be closed.
1356365406 2012-12-24 Drill / Deepen / Reopen No Violations I was on site to witness the cementing of the 13 3/8 casing. My inspection revealed that Patterson Rig# 328 has drilled a 17.5 hole to a total depth of 605. They ran 589 of 13 3/8 casing (54.5 pound per foot) and installed six bowspring centralizers on joints 1,2,3,6,9,12. O-TEX cemented the casing with 540 sacks of Class H cement with 2% CaCl ; .27% Cello-Flake; and 4/10% C-41P. They pumped 115.41 barrels of cement slurry with a density of 15.6 pounds per gallon, 1.2 yield cubic feet per sack, and 5.25 gallons of mix water per sack. They displaced the plug with 84 barrels of water and bumped the plug at 11:14 am with 275 PSI. There was good circulation throughout the job and 24 barrels of cement was circulated to surface. They conducted the casing test at 1100 PSI for 5 minutes and the casing test approved. Inspection of the well site revealed no violations at this time. Note: Drilling rig had trouble with pumps being frozen and steel pits being filled to maximum capacity. The drilling rig had to wait on a roll off tank before O-TEX could conduct the cement job.
1356590650 2012-12-26 Drill / Deepen / Reopen No Violations I was on site to witness the cementing of the 9 5/8 intermediate casing. My inspection revealed that Patterson Rig # 328 has drilled a 12 1/4 hole to a total depth of 2240. They ran 2222 of (40# per foot) 9 5/8 casing and installed 15 bowspring centralizers on joints 1,2,3,6,9,12,15,18,21,24,27,30,33,36,39. O-TEX cemented the casing with 790 sacks of Class H cement with 10% NaCl; .27% Cello-Flake; 4/10% C-41P (powder defoamer); 1/10% C35 (dispersant). The cement had a density of 15.6 pounds per gallon, a yield of 1.24 cubic feet per sack, and they used 5.48 gallons per sack of mix water. O-TEX pumped 162 barrels of freshwater to displace the plug. There was good circulation throughout the job and 33 barrels of cement was circulated to surface. They landed the plug at 7:26pm with 960 PSI and went straight into the casing test with 1470 PSI. Casing test was conducted for 5 minutes at 1470 PSI and the test was approved. My inspection of the well site revealed no violations at this time.
1385767521 2017-07-26 Production Wells No Violations I followed-up in response to complaint #5646 regarding noise issues on the pad. Sound barriers had been installed and were present around the two compressors on the east side of the pad. No other changes were made to the well or pad since my last inspection.
1419681860 2015-10-26 Preliminary Restoration No Violations I was on location to conduct a preliminary restoration inspection. The well is equipped with a plunger lift unit. Jersey barriers were installed around the wellhead. The well is properly identified with a clear, legibly-marked well identification sign. The tank battery consisted of eight, 400 BBL production tanks and was diked. The tanks are located within a spray-lined and sealed secondary containment. There are e-stops outside the barriers, and the tanks are grounded, and have static dissipators. There is a truck grounding area for trucks collecting condensate and/or produced water. Lightning protection and a windsock are installed on top of the production tanks. Other production equipment on the well pad consisted of:



Jersey barriers are installed around the production equipment. The entire well pad is enclosed with a six-foot high, chain link fence with three-strand barbed wire and the man doors were locked. Along the interior of the chain link fence there is an earthen berm and it was stable. The soil stockpile is well-stabilized with vegetation. Drainage and erosion controls at the pad are in place and functioning. A closed-loop, above-ground drilling pit system was used, so there are no earthen pits requiring closure. The pad has a crushed limestone surface, and is in good repair. The lease road is stable and drivable. Preliminary restoration passed.

For data sources see[10]

References